05000293/LER-1981-043-01, /01T-0:on 810713,outer Drywell Personnel Access Door Discovered to Have Leak Rate Exceeding Tech Spec Limits During Sp.Caused by Leaking Seal Due to Normal Inservice Degradation.Leak Rate Test Procedures Revised

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/01T-0:on 810713,outer Drywell Personnel Access Door Discovered to Have Leak Rate Exceeding Tech Spec Limits During Sp.Caused by Leaking Seal Due to Normal Inservice Degradation.Leak Rate Test Procedures Revised
ML20010G277
Person / Time
Site: Pilgrim
Issue date: 09/03/1981
From: Whitney G
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010G262 List:
References
LER-81-043-01T, LER-81-43-1T, NUDOCS 8109150515
Download: ML20010G277 (2)


LER-1981-043, /01T-0:on 810713,outer Drywell Personnel Access Door Discovered to Have Leak Rate Exceeding Tech Spec Limits During Sp.Caused by Leaking Seal Due to Normal Inservice Degradation.Leak Rate Test Procedures Revised
Event date:
Report date:
2931981043R01 - NRC Website

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U. 5. NUCLE AR REGULATORY COMMISSloN NRC FORM 366 *

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60 El DOCKET NUMBEp 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h to l2l l On July 13, 1981 during reactor startup, while conducting surveillance procedure l

No. 8.7.1.7, the outer drywell personnel access door was discovered to have a leak l

lo lal l g o l4 j l rate in excess of T.S. limits. The inner door seal had been proven to be intact.

l The seal was replaced in-kind and a satisfactory leak rate test c.onducted at 1335 l

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40 44 42 43 44 47 CAUSE DESCRIPT3ON AND CORRECTIVE ACTIONS 47 l 3 g o l l The cause of the seal leakage has been determined to be normal in-service seal l

, ;i j l degradation. A change to procedure 2.1.1, which requires a local leak rate test priori to Reactor C ulant Temperature exceeding 212 F. has been made to preclude recurrence l i Ii 12 I I gi;3; l of this event.

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DOCKET NO. 50-293 Attachment to LER 81-043/01T-0 On July 15, 1981, the Operations Review Committee (ORC) determined that degradation of the outer drywell access door seal was-reportable per 10 CFR 50 Appendix J.

This determination was based on available information. However, the ORC re-quested the On-site Safety Group Leader to prepare a detailed report of the criteria for testing the drywell door seals. On August 19, 1981 the ORC reviewed this report and determined an immediate event report be issued since operating procedure 2.1.1 permitted (and operating personnel performed) a drywell entrance for a routine, scheduled inspection after reactor coolant temperature exceeded 2120 F and before a satisfactory surveillance test of the drywell access.

door seals. To preclude a recurrence of this event, procedure 2.1.1 has been

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revised to require a local leak rate test of the door seals prior to a coolant temperature in excess of 2120F as well as after the required drywell inspection.

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