ML20010G277

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LER 81-043/01T-0:on 810713,outer Drywell Personnel Access Door Discovered to Have Leak Rate Exceeding Tech Spec Limits During Sp.Caused by Leaking Seal Due to Normal Inservice Degradation.Leak Rate Test Procedures Revised
ML20010G277
Person / Time
Site: Pilgrim
Issue date: 09/03/1981
From: Whitney G
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010G262 List:
References
LER-81-043-01T, LER-81-43-1T, NUDOCS 8109150515
Download: ML20010G277 (2)


Text

U. 5. NUCLE AR REGULATORY COMMISSloN NRC FORM 366 (7 77) -

LICENSEE EVENT REPORT (PLE ASE PRINT oR TYPE ALL R EoulRED INFoRMATioN)

CONTROL BLOCK: l l l l l l lh lo l1l lM l 7 8 9 lP lP lS l 1l@l 0 l0 l- l 0 l0 LICENSEE CODE 14 15 l0 l0 l 0 l -l 0l 0 l@[

LICENSE NUMBER 25 4 l 1LICENSE 26 l 1 l TYPE1 l JO 1 l@[ l b8lg 57 CAT CON'T lolil 7 8 s$ReE 60 dl 01510 DOCKET El l- 101219 NUMBEp l3 @l 68 Ol69 71EVENT Il 3lDATE 811 @l 0 l 9 lREPORT 74 75 013DATE l 8 l1 80}@

EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h to l2l l On July 13, 1981 during reactor startup, while conducting surveillance procedure l No. 8.7.1.7, the outer drywell personnel access door was discovered to have a leak l lo lal l l

g o l4 j l rate in excess of T.S. limits. The inner door seal had been proven to be intact.

g o l5l j The seal was replaced in-kind and a satisfactory leak rate test c.onducted at 1335 l lo is l l hrs. the same day. See Attachment l l

lc l7l l 1

l 0 l8 l l 80 E CODE SUSC E COMPONENT CODE SLB ODE SU E loisl 'l S I A lhft_[Ejh [Bjh l V I E l S l S l E l L lh dh W h 32 13 18 19 20 7 8 9 10 REVISION SiOUE NTI AL OCCURRENCE REPORT r_ CODE TYPE N O.

EVENTYEAR st EPORT NO.

LE R/RO h ,aEg [- _j l 0l 4l 3l26 l/l l0 l1 l lTl l---] J V

_ l218l 1l22 23 24 27 28 29 30 31 32 MET D HOURS $8 1 D FOR 8. SUPPLI R MAN FAC URER A N ACT ON ON PL NT Q{34G_j@ d@

35

(_Z_jh 36 3l7 Ol01010l 40

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44 lN 42 l@' l Nl@ lCl3l11Ol@

43 44 47 33 CAUSE DESCRIPT3ON AND CORRECTIVE ACTIONS 47 l 3 g o l l The cause of the seal leakage has been determined to be normal in-service seal l

, ;i j l degradation. A change to procedure 2.1.1, which requires a local leak rate test priori to Reactor C ulant Temperature exceeding 212 F. has been made to preclude recurrence l i Ii 12 I I l

gi;3; l of this event.

I l1 lAll 7 8 9

% POWER OTHER STATUS 5O RY DISCOVERY DESCRIPTION STA 1 5 [_XJ h l 01 Ol 1l h l Startuo I

W hl surveillnnce Test l

A.CTivlTY CO TENT Q LOCATION OF RELE ASE RELEASED OF RELE ASE AMOUNT OF ACTIVITY D l1 l6 l [ Z_] h 10[Zj@l N.A. l l N.A. l 44 45 80 7 8 9 11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION N.A. l l 1 l 71 l 0 l 0 l 0 lhl Z hl PE RSONNE L INJURIES NUMBER oEsCRiPriON@

N.A. l l1 l 8 l l 0 l 0 l 011l@l12 80 7 8 9 LOSS OF OR DAM AGE TO FACILITY TYPE DESCr8PTION 1 9 [_Z_jhl

  • N.A. l 80 7 8 9 10 l **"' NRC USE ONLY

'$ "'"'" @ 8109150515 810903 N.A. l lllllllllllll l2l0l 10 hDRADOCK05000 68 69 80 3 7 8 9 G. G. Witney PHONE:

617-746-7900 NAME OF PREPARER

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'.s BOSTON EDISON COMPANY PILGRIM NUCLEAR POWER STATION l' DOCKET NO. 50-293 Attachment to LER 81-043/01T-0 On July 15, 1981, the Operations Review Committee (ORC) determined that

This determination was based on available information. However, the ORC re-quested the On-site Safety Group Leader to prepare a detailed report of the criteria for testing the drywell door seals. On August 19, 1981 the ORC reviewed this report and determined an immediate event report be issued since operating procedure 2.1.1 permitted (and operating personnel performed) a drywell $

entrance for a routine, scheduled inspection after reactor coolant temperature exceeded 2120 F and before a satisfactory surveillance test of the drywell access.

door seals. To preclude a recurrence of this event, procedure 2.1.1 has been [;

revised to require a local leak rate test of the door seals prior to a coolant temperature in excess of 2120F as well as after the required drywell inspection.

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