05000298/LER-1981-014-03, /03L-0:on 810608,during Testing,Hpci Pump Turbine Tripped on Overspeed Prior to Reaching Rated Sys Flow.Sys Declared Inoperable.Caused by Improper Valve line-up Procedure.Valve Throttled & Tested

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/03L-0:on 810608,during Testing,Hpci Pump Turbine Tripped on Overspeed Prior to Reaching Rated Sys Flow.Sys Declared Inoperable.Caused by Improper Valve line-up Procedure.Valve Throttled & Tested
ML20009F033
Person / Time
Site: Cooper Entergy icon.png
Issue date: 06/24/1981
From: Flannigan R
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20009F026 List:
References
LER-81-014-03L, LER-81-14-3L, NUDOCS 8107280619
Download: ML20009F033 (1)


LER-1981-014, /03L-0:on 810608,during Testing,Hpci Pump Turbine Tripped on Overspeed Prior to Reaching Rated Sys Flow.Sys Declared Inoperable.Caused by Improper Valve line-up Procedure.Valve Throttled & Tested
Event date:
Report date:
2981981014R03 - NRC Website

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60 61 DOCKET NUMBE R 68 69 EVENT DATE 14 76 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lDuring routine surveillance testing, the HPCI pump turbine tripped on overspeed l

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