ML19352B206

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LER 80-067/01X-1:on 801107,tritium Concentration Exceeded Limits in Unrestricted Area Following Radioactive Liquid Waste Release.Caused by Inadequate Procedure Failing to Avoid Problems of Reactor Bldg Sump Discharge Sys
ML19352B206
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 04/30/1981
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19352B184 List:
References
LER-80-067-01X, LER-80-67-1X, NUDOCS 8106030341
Download: ML19352B206 (1)


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40 81 DOCKET NUMeER EVENT OESCRIPTION AND PROSABLE CONSEQUENCES h

[TTT] l On Friday, November 7,1980, at 0740 hours0.00856 days <br />0.206 hours <br />0.00122 weeks <br />2.8157e-4 months <br /> , it was determined that the concentration l rypq l cf tritium in an unrestricted area following a radioactive liquid wasta release that l I o 14 I [ was made on October 23, 1980, exceeded the limit specified in LCO 4.8.2(a). Re . l

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g l avoid problems arising from the design of the reactor building sumo discharge system. I g l Sypass installed around the oil separator in the reactor building sumo discharge sys-l ii64i l tem on February 8,1981. System operating procedure and surveillance requirement l 7 e 9 amended to provide for use of bypgs during liquid waate releases, flush of remainingo

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