LER-1981-034, /01T-0:on 810328,two Snubbers & Two Pipe Guides Were Found Damaged on HPCI Injection Line.Caused by Water Hammer in Sys.Supports Repaired & Strengthened |
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(71H 1.lCENSEE EVENT REPORT CONTROL BLOCK. l l
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REPORT o ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o 121 lWhile performing a review of the pipe supports on the HPCI iniection line, four i
lo lal l supports (2 snubbers and 2 pipe guides) were found damaged. As a result of this dis-l any other possible
.j I o 141 icovery, all ECCS lines on both units were inspected to identify la lsl Idamage. The enclosed table identifies the problems found.. Th:~
event did not affect I lo l6 l I the health or saf ety of the public.
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g l All damaged supports were atributed either directly or indirectly to water hammer in i
g ltheir respective system. All supports were repaired and strengthened as required. An l gattempt is being made to determine the cause of the water hammer events so that perma i g lnent corrective action can be determined and implemented.
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LER l-81-34 ATTAC10!ENT Facility: BSEP Unit Nos.1 and 2 Date: 3-28-81 Following the discovery of four supports on the HPCI injection line damaged due to a water hammer event, a decision was made.to examine the lines of all ECCS Systems on both units to verify the condition of the pipe.
During this inspection various supports and snubbers were found with deficiencies. All damaged supports were repaired and/or redesigned to provide additional strength. Damaged or nonfunctional snubbers were either rebuilt or replaced.
Additional NDE was performed in areas of suspected high stress supports.
Folicwing the completion of the inspection and repair work, all ECCS Systems were tested, with no excessive line motion noted, and declared fully operable and the units were returned to power operation.
The cause for these damaged supports and snubbers was one or several water hammer events on their respective system. These systems have been operated on a routine basis to perform operability checks and to perform designed operations (s/d cooling, HPCI injection on Low Level No. 2 following some scrams, etc.) No known or observed water hammer events have occurred on these lines during the operation of these systems.
It is believed that the keep-fill system which maintains the ECCS System lines full of water and possible system leakage is the cause for these events. In an effort to prevent future water hammer events and to correct the cause for the past events, several actions have been or are being taken:
1.
The Daily Surveillance Report for both units has been revised to require daily venting of all ECCS Systems to verify that the system is full. This periodicity may be changed depending on a review of the results of this venting.
~2.
Core Spray and HPCI operability periodic test have been revised to require observation of the lines when the pumps are started to detect any pipe
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movement. Also, after an auto initiation of an ECCS System, the lines will
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be inspected to assure no damage.
3.
Evaluate and modify as necessary the minimum flow valves on the ECCS Systems to ensure that they do not allow leakage which could create a water void in the system.
4.
Evaluate and modify as necessary the keep-fill system to promote its proper l
operation in maintaining the ECCS System lines full.
It is believed that these actions will provide assurance that water hammer events in the future will be prevected and ECCS line integrity assured.
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UNIT NO. 1 ECCS WALK-OFF SUPPORT NO.
LINE FAILURE DESCRIPTION REASON FOR FAILURE
CORRECTIVE ACTION
IE21-6SS42 12" CS Pump "B" Pipe clamp slipped Water hammer or system Fixed by maintenance, discharge transient IEll-18SS40 20" outlet from Insufficient weld Initial construction Redesigned and upgraded heat exch. "lA" (could have failed deficiency (added gusset plates) in seismic event).
No existing damage.
IE11-49SS 331 12" HPCI steam Slipped clamp Water hammer or system Repaired by maintenance.
cond. to RHR transient heat exch. "B" 1E41-60SS101 14" HPCI injection Broken shaft Water hammer / system Rebuilt and tested by transient maintenance IE41-60SS102 14" HPCI injection Anchor bolts pulled Water hammer / system Repaired and upgaaded per from wall transient redesign IE41-60PG55 14" HPCI injection Cracked weld on steel Water hammer / system Repaired transient IE41-60PG57 14" HPCI injection Damaged support steel Water hammer / system Repaired and upgraded per transient redesign
'1E11-2PG152 20" suction for Excessive gap between Initial construction Repaired (not a general shutdown cooling sliding surfaces on deficiency problem) steel and guide plates IE11-47CH325 12" HPCI cond.
Trapeze slipped from System transient Welded trapeze to support IE11-47CH327 to RHR heat underneath the pipe plate.
t (Spring trapeze) exch. "1A" 1E20-6PG35 CS pump "1-B" Pipe guide failed Water hammer / system Repaired and upgraded per discharge (elongated) transient new design 1E21-6PC37 CS pump "1-B" Cracked weld Water hammer / system Repaired and upgraded per discharge transient new design IE11-49PG420 12" HPCI steam Pipe clamp Clamp not tight and Repaired by maintenance.
cond, to "B" RHR slipped system transient heat exch It
UNIT NO. 2 ECCS WAI.K-OFF SUPPORT No.
l.I NE Fall.URE DESCRIPT20N REASON FOR FAII.URE
CORRECTIVE ACTION
Service condition Pumped up - not a generic 2 Ell-90SS283 4" llead Spray Low fluid problem.
2E11-95SS22 16" to RilR leat Broken bracket System transient Repaired exch. "2B" Repaired and upgraded per 2 E41-60SS102 14" llPCI injec-Bent steel Water hammer l
redesign.
tion 1
i Fluid reservoir Bad inacallation Repaired - no further action 2B32-SSB1 Recirc pump by vendor or necessary.
upside down maintenance.
Repaired and upgraded.
2 E41-60PG57 14" HPCI injec-Failed weld Water hammer (Rigid strut tion and bent pin initial weld lacked fusion.
restraint) 2E11-47CH325 12" liPCI cond.
Trapeze slipped System transient Welded trapeze to support i
plate.
line to RHR from underneath l
the pipe 2E11-47CH326 Spring supports 2E11-20FS29 20" RHR pump Approximately 3/16" Line movement during Added shim. No further action needed. Not a j
(Deadweight
- disch, gap between support plant operation and steel or poor installation' generic problem.
support) 2E11-128PG358 16" x 12" Broken pipe guide Line vibration due Support repaired. Noise to F068A throttling reducing trim shall be Pipe guide reducer installed in F068A valve.
4 upstream of 2 Ell-F068A l
Water hammer / system Repaired and upgraded per 2E21-6P637 12" CS pump Bent steel redesign transient disch. "B" CS injection 12" CS pump Broken guide seal Water hammer / system Replaced 1
transient I
link seal disch. "B" in sleeve Water hammer / system Support was operable but re-2E21-6PG35 12" CS pump Slightly bent paired and upgraded per transient disch. "B"
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redesign because Unit No. I support was inoperable.
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| 05000325/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000325/LER-1981-001-01, /01T-0:on 810103,feed Pump Tripped on High Vessel Level Due to safety-relief Valve B21-F013G,Model 67F,lift. Caused by High Second Stage & Pilot Leakage in Valve.Pilot Valve Temporarily Replaced Until Next Scheduled Outage | /01T-0:on 810103,feed Pump Tripped on High Vessel Level Due to safety-relief Valve B21-F013G,Model 67F,lift. Caused by High Second Stage & Pilot Leakage in Valve.Pilot Valve Temporarily Replaced Until Next Scheduled Outage | | | 05000324/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000324/LER-1981-001-03, /03L-0:on 810129,during Surveillance Testing, HPCI Sys Initiation Reactor Level Switch Actuated at Simulated Level Above Tech Spec.Caused by Components Slipping Due to Loose Set Screws on Actuator Pointers | /03L-0:on 810129,during Surveillance Testing, HPCI Sys Initiation Reactor Level Switch Actuated at Simulated Level Above Tech Spec.Caused by Components Slipping Due to Loose Set Screws on Actuator Pointers | | | 05000325/LER-1981-002-03, /03L-0:on 810114 & 0212,reactor Protection Sys Logic relays,C71-K3D & K3E,did Not de-energize When MSIV 1-B21-F028B Was Closed.Caused by Sticking Valve Position Limit Switch Actuator Arm Cam.Switch Replaced | /03L-0:on 810114 & 0212,reactor Protection Sys Logic relays,C71-K3D & K3E,did Not de-energize When MSIV 1-B21-F028B Was Closed.Caused by Sticking Valve Position Limit Switch Actuator Arm Cam.Switch Replaced | | | 05000325/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000324/LER-1981-002-03, /03L-0:on 810104,vacuum Breaker X-18A Had Dual open-close Position Indication While in Open Position. Probably Caused by Problem W/Vacuum Breaker Position Limit Switches.Problem Will Be Resolved During Next Outage | /03L-0:on 810104,vacuum Breaker X-18A Had Dual open-close Position Indication While in Open Position. Probably Caused by Problem W/Vacuum Breaker Position Limit Switches.Problem Will Be Resolved During Next Outage | | | 05000324/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000324/LER-1981-003-03, /03L-0:on 810108,suppression Pool Level Exceeded Specs.Caused by Valve Operator Torque Switch Out of Adjustment Allowing Leakage Into Suppression Pool.Switch Repaired | /03L-0:on 810108,suppression Pool Level Exceeded Specs.Caused by Valve Operator Torque Switch Out of Adjustment Allowing Leakage Into Suppression Pool.Switch Repaired | | | 05000324/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000325/LER-1981-003-03, /03L-0:control Rod 26-35 on 810103,18-51 on 810113,38-31 & 22-15 on 810114 Showed Inaccurate Position Indications.Caused by Buffer Card Failure on 26-35;defective Reed Switches in Others.Card Replaced,Switches Repaired | /03L-0:control Rod 26-35 on 810103,18-51 on 810113,38-31 & 22-15 on 810114 Showed Inaccurate Position Indications.Caused by Buffer Card Failure on 26-35;defective Reed Switches in Others.Card Replaced,Switches Repaired | | | 05000325/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000324/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000324/LER-1981-004-03, /03L-0:on 810110,during Startup,Intermediate Range Monitor a Did Not Respond to Changes in Input Signal.Monitor C Indicated Downscale When on Range 7.On 810111 Monitor E Indicated Downscale While Monitor C Still Inoperable | /03L-0:on 810110,during Startup,Intermediate Range Monitor a Did Not Respond to Changes in Input Signal.Monitor C Indicated Downscale When on Range 7.On 810111 Monitor E Indicated Downscale While Monitor C Still Inoperable | | | 05000325/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000325/LER-1981-004-03, /03L-0:on 810118,during Control Rod Operability Check,Pt 14.1,rod 26-07 Would Not Select.Caused by Loose Solder Joint in Rod Select Switch Due to Frequent Use of Switch.New Solder Joint Made | /03L-0:on 810118,during Control Rod Operability Check,Pt 14.1,rod 26-07 Would Not Select.Caused by Loose Solder Joint in Rod Select Switch Due to Frequent Use of Switch.New Solder Joint Made | | | 05000325/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000325/LER-1981-005-03, /03L-0:on 810101,during Normal Surveillance, Discovered Secondary Containment 20 Ft Elevation Inner Air Lock Door Inoperable Due to Missing Gasket Sealing Matl. Caused by High Personnel Traffic.Gasket Replaced | /03L-0:on 810101,during Normal Surveillance, Discovered Secondary Containment 20 Ft Elevation Inner Air Lock Door Inoperable Due to Missing Gasket Sealing Matl. Caused by High Personnel Traffic.Gasket Replaced | | | 05000324/LER-1981-005-03, /03L-0:on 810113,during Normal Surveillance, Secondary Containment 20-ft Elevation Outer Air Lock Personnel Door Found Not Sealing.Caused by Heavy Personnel Traffic Through Door.Gasket Repaired | /03L-0:on 810113,during Normal Surveillance, Secondary Containment 20-ft Elevation Outer Air Lock Personnel Door Found Not Sealing.Caused by Heavy Personnel Traffic Through Door.Gasket Repaired | | | 05000324/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000324/LER-1981-006-03, /03L-0:on 810115,when Main Steam Line Isolation Valve F028C Reopened During Test P.T.1.3.1P-2,main Steam Line C Indicated Min Flow.Cause Undetermined.Investigation Will Be Performed During Future Outage | /03L-0:on 810115,when Main Steam Line Isolation Valve F028C Reopened During Test P.T.1.3.1P-2,main Steam Line C Indicated Min Flow.Cause Undetermined.Investigation Will Be Performed During Future Outage | | | 05000324/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000325/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000325/LER-1981-006-03, /03L-0:on 810101,containment Atmospheric Monitor, 1-CAC-ATH-1259-2 Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Returned to Svc | /03L-0:on 810101,containment Atmospheric Monitor, 1-CAC-ATH-1259-2 Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Returned to Svc | | | 05000324/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000325/LER-1981-007-03, /03L-0:on 810220,observed 2-inch Discrepancy Between Level Indicators of Suppression Pool Level Transmitters 1-CAC-LT-2601 & 2602.Caused by Insufficient Venting of 2602 Transmitter High Side Sensing Line | /03L-0:on 810220,observed 2-inch Discrepancy Between Level Indicators of Suppression Pool Level Transmitters 1-CAC-LT-2601 & 2602.Caused by Insufficient Venting of 2602 Transmitter High Side Sensing Line | | | 05000325/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000324/LER-1981-007-03, /03L-0:on 810115,Group 1 Isolation Signal Received on Reactor Protection Sys Trip Channel B.Caused by Failure of Relay Coil,Model P/N 12HFAS1A49F Due to Insulation Breakdown.Coil Replaced | /03L-0:on 810115,Group 1 Isolation Signal Received on Reactor Protection Sys Trip Channel B.Caused by Failure of Relay Coil,Model P/N 12HFAS1A49F Due to Insulation Breakdown.Coil Replaced | | | 05000325/LER-1981-008-03, /03L-0:on 810106,while Performing Primary Containment Leak Rate Testing of Personnel Airlock Doors, Discovered That Drywell Exterior Airlock Door Leakage Rate Exceeded Limits.Caused by Tubing Fitting Lodged in Door | /03L-0:on 810106,while Performing Primary Containment Leak Rate Testing of Personnel Airlock Doors, Discovered That Drywell Exterior Airlock Door Leakage Rate Exceeded Limits.Caused by Tubing Fitting Lodged in Door | | | 05000325/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000324/LER-1981-009-04, /04T-0:on 810128,radwaste Sys Liquid Effluent Discharge High Range Indicator/Recorder Found to Have Recorded Release Rate Less than Actual,Causing Tech Spec Limit to Be Exceeded.Caused by Loose Mechanical Linkage | /04T-0:on 810128,radwaste Sys Liquid Effluent Discharge High Range Indicator/Recorder Found to Have Recorded Release Rate Less than Actual,Causing Tech Spec Limit to Be Exceeded.Caused by Loose Mechanical Linkage | | | 05000325/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000325/LER-1981-009-03, /03L-0:on 810115,sys Oil Cooler Inlet Isolation Valve 1-E51-F046 Would Not Open from RTGB Resulting in Reactor Core Isolation Cooling Inoperability.Caused by Incorrect Motor Control Ctr Key Lock Switch Position | /03L-0:on 810115,sys Oil Cooler Inlet Isolation Valve 1-E51-F046 Would Not Open from RTGB Resulting in Reactor Core Isolation Cooling Inoperability.Caused by Incorrect Motor Control Ctr Key Lock Switch Position | | | 05000324/LER-1981-009, Forwards LER 81-009/04T-0 | Forwards LER 81-009/04T-0 | | | 05000325/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000325/LER-1981-010-03, /03L-0:on 810120,upon Auto Initiation After Reactor Scram,Rcic Turbine Failed to Accelerate to Idle Speed,Making RCIC Inoperable.Caused by Dirty Contacts in Turbine Steam Inlet Supply Valve 1-E51-F045.Contacts Cleaned | /03L-0:on 810120,upon Auto Initiation After Reactor Scram,Rcic Turbine Failed to Accelerate to Idle Speed,Making RCIC Inoperable.Caused by Dirty Contacts in Turbine Steam Inlet Supply Valve 1-E51-F045.Contacts Cleaned | | | 05000324/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000324/LER-1981-010-03, /03L-0:on 810120,RHR Svc Water Subsys a Suction valve,2-SW-V101,would Not Open Fully.Caused by Two Hex Nuts on Input Shaft of Valve Motor Operator,Model H3BC-SMB-00, Freezing to Shaft.Nuts & Shaft Reworked & Lubricated | /03L-0:on 810120,RHR Svc Water Subsys a Suction valve,2-SW-V101,would Not Open Fully.Caused by Two Hex Nuts on Input Shaft of Valve Motor Operator,Model H3BC-SMB-00, Freezing to Shaft.Nuts & Shaft Reworked & Lubricated | | | 05000324/LER-1981-011-03, /03L-0:on 810120 & 0123,actual Pool Level Determined in Excess of Upper Tech Spec Limit.Caused by Improper Calibr Data & Calibr Procedure Inadequacy.Procedure Revision Underway & Indicators Correctly Calibr | /03L-0:on 810120 & 0123,actual Pool Level Determined in Excess of Upper Tech Spec Limit.Caused by Improper Calibr Data & Calibr Procedure Inadequacy.Procedure Revision Underway & Indicators Correctly Calibr | | | 05000324/LER-1981-011, Forewards LER 81-011/03L-0 | Forewards LER 81-011/03L-0 | | | 05000325/LER-1981-011-03, /03L-0:on 810121,during Routine Shutdown Operation,Seat Leakage Discovered on Reactor Recirculation Sample Inboard Isolation Valve 1-B32-F019.Cause Unknown. Valve Will Be Inspected & Repaired During Next Outage | /03L-0:on 810121,during Routine Shutdown Operation,Seat Leakage Discovered on Reactor Recirculation Sample Inboard Isolation Valve 1-B32-F019.Cause Unknown. Valve Will Be Inspected & Repaired During Next Outage | | | 05000325/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000324/LER-1981-012-03, /03L-0:on 810320,wiring Deficiency Associated W/ Actuation Switch Discovered That Prevented Switch Operation. Caused by Improper Writing of Field Revision to Plant Mods Requiring Installation of Switches | /03L-0:on 810320,wiring Deficiency Associated W/ Actuation Switch Discovered That Prevented Switch Operation. Caused by Improper Writing of Field Revision to Plant Mods Requiring Installation of Switches | | | 05000325/LER-1981-012-03, /03L-0:on 810122,rod 26-35 Did Not Have Position Indication at Position 03 & Rod 34-35 Did Not Have Position Indication at Position 02.Caused by Defective Rod Position Indication Reed Switches.Corrective Maint Will Be Comple | /03L-0:on 810122,rod 26-35 Did Not Have Position Indication at Position 03 & Rod 34-35 Did Not Have Position Indication at Position 02.Caused by Defective Rod Position Indication Reed Switches.Corrective Maint Will Be Completed | | | 05000325/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000324/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000324/LER-1981-013-03, /03L-0:on 810119,HPCI Sys Component Test Tp 9.3.a Could Not Be Completed.Caused by Failed Motor on CST Suction Valve F004.Motor Sent to Svc Contractor to Be Repaired | /03L-0:on 810119,HPCI Sys Component Test Tp 9.3.a Could Not Be Completed.Caused by Failed Motor on CST Suction Valve F004.Motor Sent to Svc Contractor to Be Repaired | | | 05000324/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000325/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000325/LER-1981-013-03, /03L-0:on 810122,rod Worth Minimizer Sys Rod Blocks Were Received W/Proper Adherence to Control Rod Pattern Pull Sheet.Caused by Inadequate Procedures.Rods Pulled to Correct Position | /03L-0:on 810122,rod Worth Minimizer Sys Rod Blocks Were Received W/Proper Adherence to Control Rod Pattern Pull Sheet.Caused by Inadequate Procedures.Rods Pulled to Correct Position | |
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