ML19341A733

From kanterella
Jump to navigation Jump to search
LER 80-116/03L-0:on 801231,pressure Switch 2-E11-PS-N010A Actuated Outside Tech Spec Limits.Caused by Instrument Drift.Switch Recalibr
ML19341A733
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/23/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19341A731 List:
References
LER-80-116-03L, LER-80-116-3L, NUDOCS 8101270807
Download: ML19341A733 (1)


Text

- - . . . - _ .....

MRCCORM l

  • "' l.lCENSEE EVENT REPORT l

, (PLEASE PRINT OP, TYPE ALL REEU1;E3 INFOIMATIONI CONTROL SLOCK: l I

l l l l l 6

lh lSdl@

l M l 8N9 l C LICENSEE 7

lBlE CODE l P lto 2 l@l 15 0 l 0 l - l 0 LaCENSE l 0 l NuwsEH 0 l 0 l 0 l -l 25 0 Jol 0 LsCENSE l@l 4 TYPEl 1Jo l 137l GAT 1 1 l@l CONT IIII} 3oul"c' l L @ l 0l5l0l-l0l3l2l4 @l1l2l3 11lgl0 @l0l1l2l3l8l1l@

6d 69 EVENT DATE 14 76 RSPORT DATE 80 7 8 60 61 DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h g l During the performance of ADS High Drywell Pressure Channel Calibration and Functional]

l g ; Test, PT 11.1.4PC, 2-E11-PS-N010A, model no. D28-M18SS, actuated at 2.1 psig while f

fsTTl I the reportable limit is > 2.0 psig. All other pressure switches actuated within (377] , specifications. This event did not affect the health or safety of the public. l i

1.nsj 1 l

fETTl l

,ogg, g Technical Specifications 4.3.3.1, 6.9.1.9b 80 l

SUSC DE S E Coo'E *[OiE SuEOSE COM ONENT CODE g

y

! Il B l@ l Xl@ l Z l@ l Il Nl S] TlR lU l@ l Sl@ l 20Z, [@

9 10 ?t 12 13 18 19 8 REPORT REVISION SEQUEh TI AL CCCURRENCE REPOR1 mG. COOE TYPE No.

LER Ro EVENT YEAR

@ ,asg,ar I 81 O! l-l 11 1116 l l-l l013l ltl l-l l 0l u 22 23 24 26 27 23 29 30 31 32 21 HOURS S8 i POR 8. SUPPLIE MANUPACTURER K N AC O O PLANT ME W @ l34Zl @ ]Zl@ l36Z l@ l 0 l 0l 0l Ol 3e 40 lNl@

4

[42 Yl@ lNl@ lBl0l6l9l@

43 44 47 33 35 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS h lThe pressure switch was out of calibration due to instrument drift. It was recali- .I i o I

g l brated according to the PT and returned to satisfactory operation. This instrument m l has a history of reliable operation; however, performance of other similar instruments l l

g l will be reviewed in accordance with their PT schedule to ensure there are no failure I

g l trends. 80 7 8 9 STA  % POWER OTHER STATUS ISCO RY DISCOVERY 0ESCRIPTION NA l Periodic Test l y lFl@ l0l4l0l@l "

lBl@l

8 A8TiviTY CO'0 TENT cEi.EAsto OP RELEASE LOCATION OP RELEASE @

3 1 6

@lZl l AMouNTOP NA ACTIVITY 44 l NA 45 hl 80 l

7 8 9 10 tI PERSONNEL EXPOSURES NuuSE R TYPE CESCRIPTION NA l l i I 71 l 0 l 0 l 0 l@l Z l@l '

' PERSONNEt iN;uZES NuM8ER oESCRiPTiON@ NA l l 7 i a 8 9 l0l0l0l@l 11 12 80 LOSS OP CR OAMACE To PACILITY Tvet DESCRIPTION "A I i Lu9.1lZl@l 7 8 9 IQ 80 D

NA l llllllllll lll}

7 2 O 8 9 ISSUE]8l Ls 10 ESCRIPTION 68 69 80. Z NAME OF PREPARER

' PHONE:

8102 m go 7