ML19340B894

From kanterella
Jump to navigation Jump to search
LER 80-062/01L-0:on 801021,isolation Valve for a Purification Train Would Not Close Either Electrically or by Handjack.Cause Unknown.Valve Will Be Tested & Evaluated When Plant Conditions Permit
ML19340B894
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 11/05/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19340B891 List:
References
LER-80-062-01L, LER-80-62-1L, NUDOCS 8011120529
Download: ML19340B894 (1)


Text

. _

NRC FORM 066 U. S. leUCLEAR REGULATOQV COMMISSION s (7 771 LICENSEE EVENT REPORT CONTROL SLOCC l I  ! l l l lh e

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo t il8 9I C t UCENSEE 7

o ! r ICC36 s lv l1 t@lo14 's lo I- 10 uCENSE lo lo wveEllo lo l- 10 lo l@l4 25 ;e 11ucENSE 11 l2 lo l@lSi TYPE JO I

CATsd lg CON'T f

loIil 7 6

[-]"f 1@lo l 5 l0 lOCCKET 60 61 0 loNUV8gq l 2 l 617 @l1 l0EVENT 68 69 l2 l1 D ATE l 8 l0 @l il il REPORT 74 75 Ol 51 CATE 8l Ol@ 30 EVENT OESCAIPTION AND PROS A8LE CONSEQUENCES h l o 1 : 1 l While operating at 47' thermal power and 144 We, it was determined that the isolation l g o i 31 l valve for the A purification train (HV-2301) would not close either electrically or I l o 14 ; l by handjack and was therefore considered inoperable at that time. At 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> on (

o;3i i 10-22-30, the valve was made operable on the handiack and the valve was manually ]
3 ;5 i } closed. There was no effect on public health or safety. Reportable per rort St. l l3l-l l Vrain Technical Specification AC 7.5.2(a)9. l t o In i I I a3 80 SYSTEM CAUSE CALSE COMP. VALV E CCCE COCE SUSCODE COVPONENT C00E SLSCOCE SUSCCCE jojg}

< 4 l C lG 9 to l@ l3 l@ l Al@ l Vl Al Ll Vl 0l Pl@ l Al@ l Z l@

11 12 13 '8 'd 20 SE QU E N TI 4;. OCCURRENCE AEPORT MEVisiCN gge aC E RE80RT NO. CODE Tv PE No,

@ ,asg lVENivE 8l 0] AR l-l l ol 6! 2l l/l lol1l lLl l-l l ol

_2' 22 23 24 26 27 IS ;9 Ju 31 32 TA EN AYT N CN P T MCOAS S SMIT FCA 8. SP IE VAN FACTUREA lx l@l xi@ i zl@ h l@ l of ol oi 01 I Yl@ l sl@ l4JNI@ la 13 17 l847l@

33 24 35 le 3J 40 41 42 44 CAUSE c2SCRI ATICN AND CORRECTIVE ACTIONS h i ! J ! IT%e a-tual c ause of tha vae 6 fin-= mann* kg da*e-4-od ,* e4fc *4-a. '? tire vitt f 11 il I lhe tested and eval".ated when olant cond**fnas ne-f * . A F4m1 -av-* v41' 1- a ek-***nh l' i r l lat that time. The valve ooerator is a Rotork. Model 12A(SO virh manini override. I te 13l l sealed bellows. The Nuclear Pro 4ect Decar rent will be asked to investicate rossible !

i i4 1 1 further modifications to lessen chanees of inocerabilitv.  !

a a ao f actuTv STATw3 %PCWE4 oTHE957ATLS C Q VETwCOCA SISCCvEnv 3lSCOVEAY CESCRIPT:GN 32 l' i 5 l l E l@ l0 !4 l7l@lN/A l lA lhl '8ocerator Observaticn l i ,jm,7, C'R7gyr 'l *d 45 ao aft 4Sto Ca attEASE taCATioN CF aELEA3E h l I6l l Zl@ Id @ l N/A AvouNT es ACTiv'TY 7 j 9 10 it 44 l N/A @ l 45 go l

  • ERSONNE., E XPOSua ES NLM9EM TYDE *:E SCRI AC N -

1i I 7 I I o I o I o l@l Z l@l N/A l

~

5,5cNNd' NJES

a NuvsEa CESCaieTicN@

li h i'l 'o l 0 I o"!@l N/A l LOSS CF OA OAVACE T3 FACluTY D* "'

W a TvPE O E SCAIPTIO N N/A ##' *' :s

.II 13llZl@

l 7 4 "1 0 30 Pb8 u CITV i m 'i'n'f@f"'"TA

~ 8011120 TJ f , ,,,, ""' 7'" "'l , , l j l N4M,CA.,E,AnE M83,4-Dzdr4. Gahm

,wcN E. 0 785-2223 1

- ~

l