05000325/LER-1980-049-03, /03L-0:on 800516,during Routine Surveillance, Position 08 for Rod 14-15 Did Not Indicate.Probably Caused by Ground in Prototypic Inlet Piping.Problem Under Investigation

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/03L-0:on 800516,during Routine Surveillance, Position 08 for Rod 14-15 Did Not Indicate.Probably Caused by Ground in Prototypic Inlet Piping.Problem Under Investigation
ML19312E680
Person / Time
Site: Brunswick 
Issue date: 06/03/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19312E678 List:
References
LER-80-049-03L, LER-80-49-3L, NUDOCS 8006090398
Download: ML19312E680 (1)


LER-1980-049, /03L-0:on 800516,during Routine Surveillance, Position 08 for Rod 14-15 Did Not Indicate.Probably Caused by Ground in Prototypic Inlet Piping.Problem Under Investigation
Event date:
Report date:
3251980049R03 - NRC Website

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