05000325/LER-1980-027-03, /03L-0:on 800319,during Normal Plant Operation, Standby Gas Treatment Sys 1B Would Not Reset.Caused by Tripped Control Power Circuit Breaker.Breaker Was Reset, Closed & Standby Gas Treatment Sys Was Successfully Run

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/03L-0:on 800319,during Normal Plant Operation, Standby Gas Treatment Sys 1B Would Not Reset.Caused by Tripped Control Power Circuit Breaker.Breaker Was Reset, Closed & Standby Gas Treatment Sys Was Successfully Run
ML19309E511
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 04/16/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19309E506 List:
References
LER-80-027-03L, LER-80-27-3L, NUDOCS 8004220547
Download: ML19309E511 (1)


LER-1980-027, /03L-0:on 800319,during Normal Plant Operation, Standby Gas Treatment Sys 1B Would Not Reset.Caused by Tripped Control Power Circuit Breaker.Breaker Was Reset, Closed & Standby Gas Treatment Sys Was Successfully Run
Event date:
Report date:
3251980027R03 - NRC Website

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NRC FIRM 36g U.S. NUCLE AR REGULATORY COMMISSION (7 77)

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EVENT 0 ATE 74 75 REPORT DATE NO EVENT DESCRIPTION AND PRO 9 ABLE CONSEQUENCES h lol2l [

During normal plant operation, the control operator noted the "SBGT 1B Not Reset" l

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CAUSE DESC AIPTION AND COP AEtTIVE ACTIONS h j'joll The control power circuit breaker was found tripped.

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