05000293/LER-1979-006-03, /03L-0 on 790206:reactor Water Conductivity Increased to 30 umho/cm2 After Placing D Condensate Demineralizer in Svc.Caused by Broken Lower Laterals & Bent Resin Inlet Line & Flange of Post Strainer

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/03L-0 on 790206:reactor Water Conductivity Increased to 30 umho/cm2 After Placing D Condensate Demineralizer in Svc.Caused by Broken Lower Laterals & Bent Resin Inlet Line & Flange of Post Strainer
ML19308A283
Person / Time
Site: Pilgrim
Issue date: 02/20/1979
From: Fulton J
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19308A281 List:
References
LER-79-006-03L, LER-79-6-3L, NUDOCS 7903020341
Download: ML19308A283 (1)


LER-1979-006, /03L-0 on 790206:reactor Water Conductivity Increased to 30 umho/cm2 After Placing D Condensate Demineralizer in Svc.Caused by Broken Lower Laterals & Bent Resin Inlet Line & Flange of Post Strainer
Event date:
Report date:
2931979006R03 - NRC Website

text

87 7M A REGULATORY COMMISSION LICENSEE EVENT REPORT h(CONTROL BLOCK: l l

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  • .8 69 EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PROUABLE CONSEQUENCES h pl On February 6, 1979, at 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br />, reactor water conductivity increased to 30 l

umho/cm2 af ter placing "D" condensate demineralizer in service.

,o,3, An OPER #5 was I

g, ; initiated, reactor power was immediately reduced and "D" condensate demineralizer i

was removed from service. Reactor water conductivity was reduced to less than 10 l

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ggjoyy unho/cm by 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br /> and the controlled shutdown was terminated.

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o l Investigation revealed that the lower laterals on "D" condo,c,to dominnr.1 N r vorn l

l i l i ] l broken, the resin inlet line was bent and the f1,-o on % nner ce*,4,n-

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  • 1 IiI7Ilallowing resin to enter the reactor. The laterals were ren1, cod in Tr 4 ~1.

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, 3 g demineralizer was inspected for generic problems. No problems were discovered.

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