05000325/LER-1980-017-03, /03L-0:on 800227,during Normal Plant Operation, Discovered Primary Containment Gaseous Monitor Model 5C-2B, Has Unexplained Shift from 1,000 Cpm to 60 Cpm.Caused by Water in Detector Chamber.Detector Dried & Recalibr

From kanterella
(Redirected from ML19305C741)
Jump to navigation Jump to search
/03L-0:on 800227,during Normal Plant Operation, Discovered Primary Containment Gaseous Monitor Model 5C-2B, Has Unexplained Shift from 1,000 Cpm to 60 Cpm.Caused by Water in Detector Chamber.Detector Dried & Recalibr
ML19305C741
Person / Time
Site: Brunswick 
Issue date: 03/24/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19305C740 List:
References
LER-80-017-03L, LER-80-17-3L, NUDOCS 8003310350
Download: ML19305C741 (1)


LER-1980-017, /03L-0:on 800227,during Normal Plant Operation, Discovered Primary Containment Gaseous Monitor Model 5C-2B, Has Unexplained Shift from 1,000 Cpm to 60 Cpm.Caused by Water in Detector Chamber.Detector Dried & Recalibr
Event date:
Report date:
3251980017R03 - NRC Website

text

_-

i (777)

LICENSEE EVENT REPORT CDNTROL OLOCK: l l

l l

l l

l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

,'~

s 1

6 lo lil l N i c ! B i r l p l i l@l o l o l l o l o l o l o l o l-lo l o l@l 4 l 111 l 1 l 1 l@l l

l@

LICEN' k T YPL JO

$ 7 L A f bd 3

8 9 LICkNSEE CODE 14 15 LiCLN;t NuvisEH J'J 2b a

CON'T lo t ij

'%,"c' I L l@l o l 5 l o l - 10131215 l@l o 1212171810 l@l_o 1312141810 l@

S i

8 60 61 DOCK E T NUf "J E H 64 69 EVENT DATE 14 75 HEPORT DAT E B0 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h ITTil looring normal plant operation, the control operator noticed that the primary contain-l 1013 l Iment gaseous monitor CAC-AQll-1260-3, model SC-2B, had an unexplained shift from 1000 l

101dI lcpm to 60 cpm.

The gaseous monitors CAC-AQll-1261-3 and 1262-3 were also inoperable.

I lo isi !

i loisiI i

10171 l i

1olRl ITechnical Specifications 3.4.3.lc, 6.9.1.9.b I

SYSTEM

CAUSE

C A L,SE COMP.

VALVE CODE LODE SUGCODE COVPONENT CODE SUBCODE SUSCOOs lol9l l Cl Ilh Wh l E lh l Il Nl S l Tl R l U lh l E lh lZ lh 7

8 9

10 11 IJ 13 ul 19

/J SE oOENTI A L oCCUHRENCE REPORT REVISION

,_ EVENT YE AR RFPORT No.

CODE TYPE No.

@,a=i R Ro18101 l-l 1011171 1-1 10131 IL I l-l 101 L

_ 21 22 23 24 sh 21 28 23 JO 31 J2 TAKEN ACTC oN PL NT MET HoVRS S B IT I FoR 4 UB.

SvPP IEli MAN FA T ER (J_J@lxl@

lzl@

I z l@

l0101olol I N l@

l Y l@

Nl@

l N l 3 l 0 l 5 j({

l 33 24 35 36,

3/

40 41 42 43 44 di CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h I i l o l l k'ater was found in the detector chamber. The detector was dried, recalibrated, and l

[iIil I returned to service satisfactorily.

Engineering is investigating a solution to l

2 l correct the sample flow inoisture problem or to replace the instruments with a more l

[il3)) dependable type, as this is a recurring problem. These monitors undergo calibration l l i 14 I l and preventative maintenance every two weeks.

l 7

8 9 80 STA S

% POWER oTHER STATUS IS Ov RY DISCOVERY DESCRIPTION R l E l@ l 0 l 9 l 9 lhi N/A l

l A l@l Operator Surveillance l

ACTIVITY CONTENT AuouNT or AcuviTY @ l LoCAUoN oF REMASE @

REtEAsEa or aELEAsE N/A l

N/A l1 l6 l W @ WQl 7

8 9 10 11 44 45 80 PERSoWEL E'XPoSUMES NUM8E R

DESCRIPTION

l i l il l O l 0 l o lhlTYPEZlhl N/A l

PER$owt t iniu'Jits oESCmPTioN@

NuvaER lol0101@l N/A l

i R 7

8 9 11 12 80 LOSS OF on oAMAGE To F ActLiTY TYPt DE SCniP floN R lZl@l N/A l

7 M 3 10 80 e

[3_1_n.] [_N]E @ DESCRIPTION ISSU l N/A l

lllllll1ll1ll) 8 9 10 GB 69

80. T.

(919) 457-9521 2,

A.

C. Tollison. Jr.

PHONE:

NAME OF PREPAHER

'SSO:

soonau