05000325/LER-1980-020-03, /03L-0:on 800206,during Normal Shift Turnover, Discovered RIP Valves for Containment Particulate & Gaseous Radioactivity Monitoring Sys Closing.Caused by Isolation of Valves During Penetrant Test

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/03L-0:on 800206,during Normal Shift Turnover, Discovered RIP Valves for Containment Particulate & Gaseous Radioactivity Monitoring Sys Closing.Caused by Isolation of Valves During Penetrant Test
ML19296D358
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/22/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19296D357 List:
References
LER-80-020-03L-01, LER-80-20-3L-1, NUDOCS 8003030594
Download: ML19296D358 (2)


LER-1980-020, /03L-0:on 800206,during Normal Shift Turnover, Discovered RIP Valves for Containment Particulate & Gaseous Radioactivity Monitoring Sys Closing.Caused by Isolation of Valves During Penetrant Test
Event date:
Report date:
3251980020R03 - NRC Website

text

U. S. NUCLEAR REGULATORY COMMISSION NRC FORM 366 (7 71)

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60 68 OOCKET NUMBER tW 69 EVENT DATE 74 7S R E POR T D A T E 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 l During a normal shif t turnover, it was discovered that the RIP valves for the conrnin l l ment particulate and gaseous radioactivity monitoring system, CAC-AQH-1260,1261 and i

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10 I 4 I i 1262 were closed. The containment sump flow integrating system was still operable.

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33 34 JS 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l The valves were immediately reopened and the system returned to normal.

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li j i j l that these valves isolated earlier in the day when a Group 6 isolation PT was per-I

[ ; T-I l formed. This PT was revised to notif y the operator that these RIP valves must be I

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919-457-9521 NAME OF PREPARER PHONE:

f LER CONTINUATION -- RO# 1-80-20 Facility: BSEP Unit #1 Event Date February 6, 1980 The engineering procedure for plant modifications has recently been revised to require that all procedure changes required as a result of the modification be identified and revised before the plant modification is made operational. All other PT's that give a Group 6 isolation will be reviewed and revised as re-quired to ensure that total operability is achieved following the PT.