05000293/LER-1979-011-03, /03L-0 on 790307:fire Water Shortage Tanks Volume Was Less than 240,000 Gallons in Each Tank.Caused by Failure to Ensure Levels Maintained within Tech Spec Limits. Procedures Revised

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/03L-0 on 790307:fire Water Shortage Tanks Volume Was Less than 240,000 Gallons in Each Tank.Caused by Failure to Ensure Levels Maintained within Tech Spec Limits. Procedures Revised
ML19282C608
Person / Time
Site: Pilgrim
Issue date: 03/26/1979
From: Mathis C
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19282C605 List:
References
LER-79-011-03L, LER-79-11-3L, NUDOCS 7903300382
Download: ML19282C608 (1)


LER-1979-011, /03L-0 on 790307:fire Water Shortage Tanks Volume Was Less than 240,000 Gallons in Each Tank.Caused by Failure to Ensure Levels Maintained within Tech Spec Limits. Procedures Revised
Event date:
Report date:
2931979011R03 - NRC Website

text

. NRC FORM 366 (7 77)

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8 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES O'o l On March 7,1979, the ORC concurred.with findir.gs of the QA Department's review of l

o 2 the Nuclear Plant Operator's Tour Forms (OPER-08) from February 1-15, 1970, which l

, 3 g 240.000 gallons in g l indicated that the fire water storage tanks volume was less than l cach tank with the exception of one day. This is contrary to the requirements of l

o 3 Section 4.12.B.1.a of the PNPS Technical Specifications.

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44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g l This event occurred because of lack of followup to ensure levels being maintained l

were within limits. Calculations were performed to determine minimum instrument g

l values, setpoints for annunciators were changed to alarm before minimum levels are l

g l exceeded, controls fo fill valves were adjusted to maintain required levels, and l

l l procedures were revised.

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