05000293/LER-1979-004-03, /03L-0 on 790120:plant Stack Process Radiation Monitoring Sys Failed.Caused by Sample Line Freezing

From kanterella
(Redirected from ML19259B493)
Jump to navigation Jump to search
/03L-0 on 790120:plant Stack Process Radiation Monitoring Sys Failed.Caused by Sample Line Freezing
ML19259B493
Person / Time
Site: Pilgrim
Issue date: 02/12/1979
From: Mathis C
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19259B492 List:
References
LER-79-004-03L, LER-79-4-3L, NUDOCS 7902260410
Download: ML19259B493 (1)


LER-1979-004, /03L-0 on 790120:plant Stack Process Radiation Monitoring Sys Failed.Caused by Sample Line Freezing
Event date:
Report date:
2931979004R03 - NRC Website

text

' '

17 77)

LICENSEE EVENT REPORT CONTROtetOcc1 l

l l

1 I th (PLEASE PRWT OR TYPE ALL REQUIRED WFORMATIOM 1

e lo lil I MI ^l PI P l Sl 1l@l010l0l0l0l0l0l0l0l0

@l4l1 1l1 1 @l l@

0 7

8 9 LICENSEE Cone 14 15 LICENSE NUMUEH 2D

/t2 LICE NSE T YPE Ju Sl t. A l bd CON'T

"$ $ l L @l 015 l 0 l - 10 l 2 l 9 l 1 l@[0 ] I i 7 ! 0 l 7 l 9 lh 0 l 2 l 1 2 l 7 l 9 l@

o i

7 8

6u bl DOCK ET NUVUEH M

03 EVEN T D ATE 14 7's HEPORT DA T E

'40 EVENT DFSCRIPTION AND PROHACLE CONSEQUENCES h lo l2l l On January 29, 1979 at 1220 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.6421e-4 months <br />. the Plant Stact: Precessm"utdiati nn unnitoritw I

System failed as ir.dicated by "Ai/Lo Suc tion Flow to Stack Gas Sample Pomp" an-nunciation i.n the Control Room.

Repairs were instituted immediately and when af ter j one hour repairs hel not been completed, a controlled shutdown was initiated as j

l o I61 L_equired by T.S. and terminated when the sample system was returned to service.

r j

O 7

l 0

8 l

l SYSTEM

CAUSE

CAUSE COVP.

VALVE CCOE CODC SU8 CODE COYPONENT CODE SU8 CODE SUSCODE l0l9l lM lC l@ lC lh lZ lh l II Nl Sl Tl Rl Ulh l R lh W h 7

8 9

10 11 12 13 18 IJ 20 SEQUENTI AL OCCURRENCE REPORT REVISION LER RO EVENT YEAR R EPORT NO.

CODE TYPE NO.

@,ay.o,a; I 71 91 l-l 10 10 14 1 1/

101al itI l-l 01 21 22 23 74 26 21 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHVENT NPR D.4 PRIVE COYP.

CCYPONENT TAKEN ACitON ONFLANT YETHOD HOURS SUBMITTED FORMSUB.

SUPP LI E R MANUFACTURER IB l@l F @

lZ l@

l Z l h

_/ 0 0l 0l nl bj@

y@

{@

lc l 0 gl nl@

33 J4 Jb 36 J

A0 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l Investigation revealed the sanole line was frozen. The sannle line was fraed with i

o heat and system returned to normal. Heat tape has been annlied to rho m ~,1n linn i i to prevent future occurrences.

1 3 l

l li l 41 1 I

7 8 9 80 STA S

% POW 8iR OTHER STATUS DISCO RY DISCOVERY DESCRIPTION I1 l 5 l [E__jh l 1 l 0 l O lhl N.A.

l W hl Onor,rinn,1 Frone l

ACTIVITY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELE ASE y @ l Z l@]

N.A.

l l

N.A.

l i o 7

8 9 10 11 44 45 80 PERSONNEL EXPowHES NUMBER TYPE DE SCRIPTION LLL7J l i

I l@lzl@l N.A.

l 80 PERSONNE L INJU 1ES NUMBE R D E SCRIP it ON l0 0l0l@[

i a y,g, 7

8 9 11 17 gg LOSS OF CH DAMAGE ro FACILITY TYPE D E SC HIP 110N lZl@l N.A.

1 9 7

8 9 10 80

,sso,'f@llScn,,,,0@

790226Oto

= v NHC USE ONLY [N_

N.A.

l llllllllI llllf 2 o 7

R 9 10 68 69 80 g a es his pgang;617-756-7900 NAME OF PHEPAHEH