ML19257D864

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LER 80-003/03L-0:on 800103,during Reactor Startup,Vessel Conductivity Exceeded 2 Umho for 31-h.Caused by Auxiliary Boilers Being Isolated for Months & Supply Lines Containing Stagnant,High Conductivity Water
ML19257D864
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/29/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257D856 List:
References
LER-80-003-03L, LER-80-3-3L, NUDOCS 8002060635
Download: ML19257D864 (2)


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n 7 During a normal reactor startup, vessel conductivity exceeded 2 pmho for 31 hours3.587963e-4 days <br />0.00861 hours <br />5.125661e-5 weeks <br />1.17955e-5 months <br />, j l

, 9 The highest value recorded was 6.29 pmho and chloride concentration remained 10w. j

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44 4-CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l The high conductivity came from the auxiliary b311er which was being used ta supplv 1

, ,  ; gland scaling stear. . The auxiliary boilers had been isolated for a number of months l

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,,,,,; stagnant,high conductivity water, resulting from the long period of boiler wet lay-up.l 3'

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. POWER OTHER STATUS blSCO RY DISCOVERY DESCRIPTION i 5 ] @ l0l0l3l@[, NA l lAl@l Coolant Sampling j A itVI T Y CONTENT RELE ASED C8 AE LE ASE AYOUNT OF ACTIVITY LOCATION OF RELEASE F

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A. C. Tollison, Jr. 919-457-9521 o NAME OF PitEPAHLH PHONE: ",

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or LER CONTINUATION -- RO# 2-80-3 Facility: 15SEP Unit #2 Event Date 1-3-80 This is the origin of the vessel high conductivity. Scaling steam was swi'ched to reactor steam and the vessel was cleaned up with RWCU. General Plant Opera-ting l'rocedure GP-1 is being revised to ensure that the auxiliary boiler steam lines are sampled before using auxiliary steam.

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