ML19257D818

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Supplemental LER 79-104/03L-1:on 791206,while Performing Flow Rate Test,Hpci Sys Isolated Due to High Suction Pressure Signal Which Tripped HPCI Turbine Stop Valve. Caused by Leakage of Diaphragm on 1E41-PSH-N031
ML19257D818
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/29/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257D812 List:
References
LER-79-104-03L, LER-79-104-3L, NUDOCS 8002060534
Download: ML19257D818 (1)


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I 8 f,0 61 DOCnET NUYbE R EVENT QESCRIPTION AND PROBAULE LO4 SEQUENCES h a 2 i While performing PT 9.5, HPCI 1000i! Flow Rate Test, the HPCI system isolated due to o 3 1 a high suction pressure signal from lE41-PSH-N031 which tripped the HPCI turbine l stop valve, j o a i l

o s I o c l a17 i o 8 i Technical Specifications 3.5.1, 6.9.1.9b I a.

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[i g i ; j pressure signal. The diaphragm was replaced end returned to service satisfsetorily. [

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