05000325/LER-1980-005-03, /03L-0:on 800113,while Performing Control Rod Operability Check,Control Rod 42-35 Had No Position Indication at Notch 47.Caused by Fault in Reed Switch in Prototypic Inlet Piping Probe

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/03L-0:on 800113,while Performing Control Rod Operability Check,Control Rod 42-35 Had No Position Indication at Notch 47.Caused by Fault in Reed Switch in Prototypic Inlet Piping Probe
ML19257D805
Person / Time
Site: Brunswick 
Issue date: 01/28/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257D801 List:
References
LER-80-005-03L, LER-80-5-3L, NUDOCS 8002060507
Download: ML19257D805 (1)


LER-1980-005, /03L-0:on 800113,while Performing Control Rod Operability Check,Control Rod 42-35 Had No Position Indication at Notch 47.Caused by Fault in Reed Switch in Prototypic Inlet Piping Probe
Event date:
Report date:
3251980005R03 - NRC Website

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