05000293/LER-1979-049-03, /03L-0:on 791129,after Completing Surveillance Testing of Diesel Generator A,Auxiliary Trip Relay Annunciator Did Not Clear.Cause Undetermined.Phase a Target & Differential Lockout Reset

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/03L-0:on 791129,after Completing Surveillance Testing of Diesel Generator A,Auxiliary Trip Relay Annunciator Did Not Clear.Cause Undetermined.Phase a Target & Differential Lockout Reset
ML19256G552
Person / Time
Site: Pilgrim
Issue date: 12/28/1979
From: Mathis C
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19256G551 List:
References
LER-79-049-03L, LER-79-49-3L, NUDOCS 7912310454
Download: ML19256G552 (1)


LER-1979-049, /03L-0:on 791129,after Completing Surveillance Testing of Diesel Generator A,Auxiliary Trip Relay Annunciator Did Not Clear.Cause Undetermined.Phase a Target & Differential Lockout Reset
Event date:
Report date:
2931979049R03 - NRC Website

text

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