05000325/LER-1979-106-03, /03L-0:on 791207,during Core Spray Sys,Component Test, Core Spray/Rhr Pump Running Annunciator Not Received.Caused by Shut Root Valves Not Returned to Normal Position After Testing on 791130

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/03L-0:on 791207,during Core Spray Sys,Component Test, Core Spray/Rhr Pump Running Annunciator Not Received.Caused by Shut Root Valves Not Returned to Normal Position After Testing on 791130
ML19256G185
Person / Time
Site: Brunswick 
Issue date: 12/14/1979
From:
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19256G180 List:
References
LER-79-106-03L, LER-79-106-3L, NUDOCS 7912270571
Download: ML19256G185 (2)


LER-1979-106, /03L-0:on 791207,during Core Spray Sys,Component Test, Core Spray/Rhr Pump Running Annunciator Not Received.Caused by Shut Root Valves Not Returned to Normal Position After Testing on 791130
Event date:
Report date:
3251979106R03 - NRC Website

text

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LICENSEE EVENT REPORT CONTROL BLOCK:.l l

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7 8 9 LICENSEE CODE 14 15 LICENSE hbM8EH

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60 61 00CK ET Nuv8 ER tid 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h o

2 l While performira PT 7.1.8 Core Spray Svstem Cemeenert Test. the " Core Sorav/

I El RRR pump running" annunciator was not received.

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a l Technicil Specifiestin, 1.1.3.

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40 43 42 43 44 47 43 CAUSE CESCRIPTION AND CORRECTIVE ACTICNS h i

o 1 Upon investigation, the root valves for 1-E21-PS-N003B & 9B were found shut.

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l review of the calibration folders and trouble tickets revealed that these valves werd i

2 last ooerated on 11/30/79, while perfotnina PT 3.1.12PC, Core Sprav Pump Discharze I

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l Pressure Interlock Channel Functional Test, which chacks the setooint and cerformanc4 i

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of these switebes. The isolation valves were opened and PT'7.1.8 was completed econt'd) 80 7

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PERSeN~ Et'~A 1642 056 oESCRP1,0~e NU..ER

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NAME OF PREPARER PHONE:

LER CONTINUATION - RO # l-79-106 EACILITY: BSEP Unit No. 1 EVENT DATE:

12-7-79 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (ennt'd) successfully. The signoff for returning the isolation valves to the open position on PT 3.1.12PC was signed off; however, that signoff also includes two other items requiring act' ten. All I&C PT's will be reviewed and revised as required to provide a signoff specifically for returning operated valves to their normal position.

This event will be reviewed by all I&C and Electrical personnel. ADS permissive for "LPCI pump running" would have been available from five other sources -

RHR pumps A, B, C, D and Core Spray Pump A.

1642 057