ML19253B582

From kanterella
Jump to navigation Jump to search
LER 79-075/03L-0:on 790915,during Normal Operations,Drywell Equipment Drain Sump Flow Integrator Observed Not Operating While Sump Was Pumped Down Due to Blown Fuse in Integrator Current Power Supply.Fuse Replaced & Sys Tested
ML19253B582
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 10/12/1979
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19253B576 List:
References
LER-79-075-03L, LER-79-75-3L, NUDOCS 7910160438
Download: ML19253B582 (2)


Text

v. . .~m-n neoutalos y couuissioN ar.77,

, LICENSEE EVENT REPORT CONTRot stock: l l@

l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

[N gY lJ gA gF gi g 0g 0g g 0g 0g 0g 0; g0g 0 g0 4 I I I I g g g g g g 7 8 9 14 LICENSEE CODE 16 LICENSE NUVSEH 25 26 LICENSE TYPE JO $ 1 L A T 68 CON'T a

lolil ,g,]

' 8 00 Ll@l0 l 5 l0 l 0 l 0 3l3[3l@l0l9l1l5l7l9l@l1l0l1l2[7l9l@

61 DOCKET NUMBER 6d 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Ml Please See Attachment 10131 1 I 10141 l I O s t '

I O 6 l

Lo_.LJ l i O a i I 7 8 9 80 C DE CODE SUBC E COMPONENT CODE SU8C S E 7

o o 8

I M l A l@ y@ l AlQ [ l l N l S l T l R l U lg ]DEg 9 10 11 12 13 18 19 20 g

SEQUE NTI AL OCCURRENCE REPORT REVISION LER RO EVENT YEAR R EPO A T NO. CODE TYPE NO.

@Nu; as oar c

I 7I 9I [--j l 017l 5l /l 10 [3 [ Ll [__j 0l 21 22 23 24 26 21 28 29 30 31 32 TAKE A T ON ON PLAN T T HOURS 22 S8 iT D FOR b 8. SUP IE MAN

[A[gl34Zl@

3J lZlg 35

]6g 3 3/

0l 0l 0l 40 gg 41 l N [g 42 a

43 g 44 Gl0 FACI"lER0 47 CAUSE DESCRIPT!ON ANDCORRECTIVE ACTIONS h i O Please See Attachment l li lil i i

1 > l q 1 3 lt l4) l l 7 8 9 ST S  % POWER OTHER STATUS ISCO RY DISCOVERY ESCRIPTION li I s l (_E_j@ l0 l 2 l 3 l@l NA l l A lg[ Operator Observat$on

' ' " l

' !TiviTY A COArENT RELEASED OF RELE ASE i 6 gl AMOUNT NA OF "

ACTIVITYl NA @ lLOCATION OF RELEASE @

l

,eRSONsEL EoOSSES

  • NUYt$ E R TYPE DESCRIPTION i39 i NA 7

1010 l o l@LZJ@l l PERSONsE t iN;u' RIES NuYPE R oESCniPnO~@

li la l8 10101 7 9 O l@[

11 12 NA l

LOSS OF OR DAMAGE TO FACILITY TYPE DESCHIPTION t /A y l Z j@l NA li r*3,/4 i O 'f 7 8 9 10 l O70101604-3 8 8

2 o 8 9 issuEf@oESCaiPTiON

[_ N,, l to NA l

l l l l l l l l l l l l l80:7g 68 69 NAME OF PREPARER W. Verne Childs 315-342-3840 o PHONE: *

. POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT DOCKET NO. 50-333 ATTACHMENT TO LER 79-075/03L-0 Page 1 of 1 During normal operation, Operations personnel noted that the Drywell Equipment Drain Sump Flow Integrator was not operating while the sump was being pumped down.

This resulted in operation of the reactor coolant leakage detection subsystem in a degraded mode allowed by Technical Specifications Appendix A, Paragraph 3.6.D.2.

The FitzPatrick plant contains as permanent equipment dif ferentiating instruments which display and record the rate of rise of the drywell equipment drain sump icvel.

Examination of the recording charts associated with this instrument, together with the sump level indicator recorders which provide indication of the frequency of sump pump operation, revealed that the rate of identified equipment leak off was approximately 4 gpm as compared to a Technical Specification limit of 25 gpm. The re fo re , the event did not represent a significant hazard to the public health and safety.

Investigation of the problem revealed a blown fuse in the integrator current power supply. The fuse was replaced and a pump down of the sump was manually initiated to verify proper operation of the system on the same day as discovery of the event.

I1bol 165 O