05000293/LER-1979-023-03, /03L-0 on 790616:during Routine Testing,Noted That Closing Times for A0-203-1A & E Greater than Allowable Limits.Caused by Changes in Characteristics of Hydraulic Operators.Operators Adjusted

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/03L-0 on 790616:during Routine Testing,Noted That Closing Times for A0-203-1A & E Greater than Allowable Limits.Caused by Changes in Characteristics of Hydraulic Operators.Operators Adjusted
ML19225A538
Person / Time
Site: Pilgrim
Issue date: 07/16/1979
From: Mathis C
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19225A537 List:
References
LER-79-023-03L, LER-79-23-3L, NUDOCS 7907190525
Download: ML19225A538 (1)


LER-1979-023, /03L-0 on 790616:during Routine Testing,Noted That Closing Times for A0-203-1A & E Greater than Allowable Limits.Caused by Changes in Characteristics of Hydraulic Operators.Operators Adjusted
Event date:
Report date:
2931979023R03 - NRC Website

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