IR 05000440/2019002
| ML19210D576 | |
| Person / Time | |
|---|---|
| Site: | Perry |
| Issue date: | 07/26/2019 |
| From: | Chuck Norton NRC/RGN-III/DRP/B2 |
| To: | Payne F FirstEnergy Nuclear Operating Co |
| References | |
| IR 2019002 | |
| Download: ML19210D576 (12) | |
Text
July 26, 2019
SUBJECT:
PERRY NUCLEAR POWER PLANTINTEGRATED INSPECTION REPORT 05000440/2019002
Dear Mr. Payne:
On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Perry Nuclear Power Plant. On July 17, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC inspectors did not identify any finding or violation of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Charles H. Norton, Acting Chief Branch 2 Division of Reactor Projects
Docket No. 05000440 License No. NPF-58
Enclosure:
As stated
Inspection Report
Docket Number:
05000440
License Number:
Report Number:
Enterprise Identifier: I-2019-002-0056
Licensee:
FirstEnergy Nuclear Operating Company
Facility:
Perry Nuclear Power Plant
Location:
Perry, OH
Inspection Dates:
April 01, 2019 to June 30, 2019
Inspectors:
T. Briley, Senior Resident Inspector
J. Nance, Resident Inspector
J. Rutkowski, Project Engineer
J. Steffes, Senior Resident Inspector
Approved By:
Charles H. Norton, Acting Chief
Branch 2
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Perry Nuclear Power Plant in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
The plant began the inspection period shutdown for refueling outage (RFO) 1R17. On April 5, 2019, at 5:16 a.m., the plant was placed in startup mode and achieved criticality at 7:25 a.m. that same day. On April 6, 2019, at 11:59 p.m., the main generator was synchronized to the grid. On April 7, 2019, at 2:44 a.m., the main generator was removed from the grid due to hydraulic oil intrusion into the generator casing. On April 7, 2019, at 5:44 p.m., after correcting the cause of the oil intrusion to the generator casing, the main generator was synchronized to the grid. The plant reached 100 percent power on April 11, 2019. On April 27, 2019, the licensee reduced reactor power to 60 percent in order to correct balance of plant steam leaks.
The licensee resumed 100 percent power operations that same day. On May 31, 2019, the licensee commenced power reduction to 13 percent reactor power and removed the main generator from the grid on June 1, 2019. On June 2, 2019, following repairs to the number four turbine stop valve, the licensee synchronized the main generator to the grid at 1:43 a.m. and commenced power ascension. The licensee returned the plant to 100 percent power on June 4, 2019. The reactor remained at approximately 100 percent power for the remainder of the inspection period except for rod sequence exchanges and required testing.
On April 25, 2018, FirstEnergy Solutions (FES) / FirstEnergy Nuclear Operating Company (FENOC) notified the U.S. Nuclear Regulatory Commission (NRC) that they intend to shut down all four of their operating nuclear power plants (ADAMS Accession Number ML18115A007).
Perry Nuclear Power Plant, Unit 1, is scheduled to be shut down May 31, 2021. On March 21, 2018, FES, FirstEnergy Nuclear Generation (FENGEN), and FENOC filed for bankruptcy. The NRC continues to maintain focus on public health and safety and the protection of the environment. This will include a continuous evaluation by inspectors to determine whether the licensee's financial condition is impacting safe operation of the plant.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Summer Readiness Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated summer readiness of offsite and alternate alternating current power systems on June 5 and 24, 2019
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 1 division 1 direct current system while the high pressure core spray system was unavailable on May 9, 2019
- (2) Reactor core isolation cooling system May 25-30, 2019
- (3) Unit 2 start-up transformer electrical lineup on June 24-25, 2019
71111.04S - Equipment Alignment
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
Low pressure core spray complete system walkdown
- (1) The inspectors evaluated system configurations during a complete walkdown of the low pressure core spray system on April 3-4, 2019
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Auxiliary building 574 foot elevation fire zone (FZ) 1AB-1g, on May 28-30, 2019
- (2) Control complex division 1 switchgear FZ 3c on May 28-30, 2019
- (3) Control complex 638 foot elevation FZ 4a, e, l, g, h, c and d on May 28-30 2019
- (4) Intermediate building 599 foot elevation OIB-2, FHB 0FH-1,2 on May 28-30, 2019
- (5) Diesel generator division 2, FZ 1DG-1a on May 28-30, 2019
71111.06 - Flood Protection Measures
Inspection Activities - Underground Cables (IP Section 02.02c.) (1 Sample)
The inspectors evaluated cable submergence protection in:
- (1) Underground cable inspection and condition review for safety-related manholes 1 and 2 on May 8 and 22, 2019
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the Control Room during plant startup from 1R17 refueling outage on April 5-9, 2019
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated an operations crew-evaluation scenario in the plant training simulator on May 13, 2019
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Reactor recirculation system flow control valves on June 2-5, 2019
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Plant risk assessment while the low pressure core spray system was unavailable for maintenance on April 18, 2019
- (2) Plant risk assessment while the "A" train of control room heating, ventilation and air conditioning and emergency recirculation system was unavailable due to maintenance on May 22-23, 2019
- (3) Plant risk assessment associated with the main turbine electro-hydraulic control system emergent leak repair, May 28-June 1, 2019
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (3 Samples)
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Emergency service water "A" control power fuses operability determination on May 29-31, 2019
- (2) Low pressure core spray operability determination on May 29-June 3, 2019
- (3) Average power range monitors A, C, and E failed channel check acceptance criteria operability determination on June 1-4, 2019
71111.19 - Post-Maintenance Testing
Post Maintenance Test Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the following post maintenance tests:
- (1) Division 3 diesel generator following maintenance on May 24, 2019
- (2) Reactor recirculation pump A slow speed breaker 2A 52LCS mechanical switch contacts following repair on June 1, 2019
- (3) Positive assist non-return check valves relay following repair on June 1, 2019
- (4) Main turbine electro-hydraulic control leak following repair on June 3, 2019
- (5) Remote shutdown panel following power supply replacement on June 26, 2019
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors continued evaluation of refueling outage 1R17 activities from April 1-6, 2019. Activities evaluated by the inspectors included, but were not limited to, refueling operations, containment closure, plant heatup, startup and fatigue management
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Inservice Testing (IP Section 03.01)
- (1) SVI-E12-T2001, RHR 'A' Pump and Valve Operability Test, on June 25-26, 2019
Surveillance Tests (other) (IP Section 03.01) (3 Samples)
- (1) SVI-B13-T0001, Shutdown Margin Calculation, on April 5-8, 2019
- (2) SVI-B21-T0373-A, Safety Relief Valve and Low-Low Set Pressure Actuation Channel Calibration, for 1B21-N668A on April 25-26, 2019
- (3) SVI-R43-T1317, Diesel Generator Start and Load Division 1, on June 27, 2019
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated an emergency response organization drill on May 15,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04)===
- (1) Unit 1 (April 1, 2018 - March 31, 2019)
MS06: Emergency AC Power Systems (IP Section 02.05) (1 Sample)
- (1) Unit 1 (April 1, 2018 - March 31, 2019)
MS07: High Pressure Injection Systems (IP Section 02.06) (1 Sample)
- (1) Unit 1 (April 1, 2018 - March 31, 2019)
71152 - Problem Identification and Resolution
Semiannual Trend Review (IP Section 02.02) (1 Sample)
- (1) The inspectors reviewed the licensees corrective action program for potential adverse trends in the flow-accelerated corrosion impacts and programmatic requirements that might be indicative of a more significant safety issue on June 28-29, 2019
71153 - Follow-Up of Events and Notices of Enforcement Discretion Personnel Performance (IP Section 03.03)
- (1) On April 7, 2019, at 1:23 a.m., following main generator synchronization to the grid after completion of the 1R17 refueling outage, operators tripped the main turbine in response to hydrogen seal oil detraining section level high and generator casing liquid level high alarms. The inspectors evaluated this unplanned event and licensees performance.
INSPECTION RESULTS
Observation: Flow-Accelerated Corrosion Program 71152 The inspectors reviewed condition reports associated with leaks in system piping induced by flow-accelerated corrosion. The inspectors considered the inputs, evaluations, planned and completed actions for each flow-accelerated corrosion induced leak. The inspectors further reviewed the licensee's programmatic and trend analysis and additionally performed their own search of the corrective action program to validate appropriate inputs were considered during the self-assessment. The inspectors compared the licensee's evaluations, actions, and trend analysis to the programmatic requirements and controls.
The inspectors did not identify any concerns with the licensee's characterization or corrective actions and determined that the scope of each evaluation was appropriate for the circumstances.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On July 17, 2019, the inspectors presented the integrated inspection results to Mr. F Payne and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Miscellaneous
Certification of Summer Readiness
06/28/2019
Procedures
Drawing 302-
0632-00000
Reactor Core Isolation Cooling System
ELI-R11
Station Interbus Transformers
ELI-R22
15KV and 5KV Metal Clad Switchgear
ELI-R42
DC Systems: Batteries Chargers Switchboards
05/09/19
ELI-S11
Power Transformer
SOI-E51
Reactor Core Isolation Cooling System
VLI-E51
Reactor Core Isolation Cooling System
VLI-E21
Low Pressure Core Spray System
FPI-01B
Intermediate Building
FPI-0CC
Control Complex
FPI-0FH
Fuel Handling Building
FPI-1AB
Auxiliary Building Unit 1
FPI-1DG
Diesel Generator Building
PTI-P54-P0041
Semiannual Fire Door Inspection
Work Orders
200701882
Manhole 1 and 2/ Division 3 Inspections
05/20/2019
200712140
Inspect and Dewater Manholes
06/17/2019
71111.11Q Miscellaneous
Evolution Specific
Reactivity Plan
Beginning of Cycle 18 Startup 129
OTLC-
3058201902_PY-
SGC1-Evaluated
Simulator
Scenario
OTLC-3058201902_PY-SGC1-Evaluated Simulator
Scenario
Perry Nuclear
Power Plant Plant
Health Report
2018-2
Perry Nuclear Power Plant Plant Health Report 2018-2
01/28/2019
eSOMS Plant
Narrative Logs
Plant Narrative Logs
05/28/2019
Procedures
NOP-OP-1007
Risk Management
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Work Orders
200595679
Replace Guide Vane Actuator OE
05/21/2019
200785158
Low Pressure Core Spray Water Leg Pump Water Leak 15
Drop Per Minute
04/18/2019
Miscellaneous
eSOMS Plant
Narrative Logs
Plant Narrative Logs
05/24/2019
eSOMS Plant
Narrative Logs
Plant Narrative Logs
05/24/2019
Operability
Evaluations
ATL-2019-0251-
ATA-26
APRM Channel Checks
06/02/2019
Procedures
PTI-E22-P0011
HPCS Diesel Generator Slow Speed Start for Post-
Maintenance Inspections
05/24/2019
Work Orders
200753986
Accident Monitoring and Remote Shutdown Channel Checks 06/26/2019
200759929
Perform Engine Maintenance
05/17/2019
20078821
'B' PAC (Positive Assist Check) Valves are not Opening/CR
06/02/2019
200788564
N32 - Turbine EHC (Electro Hydraulic Control) Fluid
Leak/CR
06/02/2019
200788818
Recirculation Pump 'A' Failed to Downshift. Single Loop
Operation on Reactor Recirculation Pump 'B' at this Time.
Simple Troubleshooting Order.
06/01/2019
Corrective Action
Documents
2019-03242
Flow Control Valve A Movement During Hydraulic Power
Unit Startup
04/06/2019
2019-03270
Hotwell Pump Motor "A" and Surrounding Area Oil Spilled
04/07/2019
2019-03273
High Main Generator Casing Liquid Level Requires Manual Trip of Main Turbine
04/07/2019
Corrective Action
Documents
Resulting from
Inspection
2019-03184
NRC ID: Resident Inspector Identified an HRA Posting
Improvement
04/04/2019
Procedures
ARI-H51-P176-
0002-C2
Seal Drain Enlargement Liquid Detector Full
IOI-3
NOP-OP-1002
Conduct of Operations
SOI-N42
Hydrogen Seal Oil System
SVI-B13_T0001
Shutdown Margin Calculation
04/05/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Work Orders
200714859
SVI-B21-T0373A
04/22/2019
200729176
SVI-E12-T2001, RHR A Pump and Valve Operability Test
06/25/2019
200754234
SVI-R43-T1317 Diesel Generator Start and Load Division 1
06/27/2019
Miscellaneous
Perry ERO Integrated Drill Scenario Guide 5/15/2019 Rev 0
05/15/2019
71151
NOBP-LP-4012-
Mitigating Systems Performance Index (MSPI) Unavailability
Index (UAI) & Unreliability Index (URI) for Emergency AC
Power Systems
04/01/2018 -
03/31/2019
NOBP-LP-4012-
Mitigating Systems Performance Index (MSPI) Unavailability
Index (UAI) & Unreliability Index (URI) for High Pressure
Injection System (HPCS) & High Pressure Emergency
Diesel Generator (EDG)
04/01/2018 -
03/31/2019
NOBP-LP-4012-
Safety System Functional Failures
04/01/2018 -
03/31/2019
Corrective Action
Documents
2019-00392
Two Through-Wall Leaks Identified in Low Pressure Drain
Piping
01/15/2019
2019-00935
Potential Negative Trend of Through-Wall Steam Leaks and
Piping Flange Steam Leaks
01/30/2019
2019-02268
1R17 FAC Location 49 on Heater Drain Inlet Nozzle to
1N21B0001C (Low Pressure Feedwater Heater 1C)
03/13/2019
2019-02332
1R17 FAC Examination Results on RWCU Spool Piece
Between 1C and 2A Heat Exchangers
03/14/2019
2019-02427
A Through Wall Hole Found on N36 Feed Water Heating 24
inch Extraction Steam Pipe
03/17/2019
2019-04170
Additional Pitting Discovered in Piping Downstream of
Emergency Service Water
05/07/2019
Procedures
NOP-ER-2005
Flow-Accelerated Corrosion Program
Corrective Action
Documents
CR 2019-03273
High Main Generator Casing Liquid Level Requires Manual Trip of the Main Turbine
04/07/2019