ML19207C225

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LER 79-026/03L-0:on 790807,bearing Water Makeup Pump P-2105 Removed from Svc to Perform Line Repair W/Reactor at 65% Power.Caused by Hole in Recirculation Line of Pump,Requiring Removal from Svc.Line Repaired.Pump Returned to Svc
ML19207C225
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 08/31/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19207C226 List:
References
LER-79-026-03L, LER-79-26-3L, NUDOCS 7909100504
Download: ML19207C225 (1)


Text

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- LICENSEE EVENT REPORT CONTROL BLOCK: l 1

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(PLEASE PRINT OR TYPE ALL REQUIRED INFOHMATION) o 1 lC 10LICENSEEl F lS IV l1 @l15 0 0 -l 0l 0 0 0 l 0 l - l 0 l 250 l@{4 26 l1 l1 l2 l0 @l5 7 CAl T 68l@

LICENSE TYPE JC 7 8 9 CODE 14 LICENSE NUMBER CON'T

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EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES o 2 With the reactor operating at approximatelv 65% power, bearing water makeuo pu=o P-12105 was removed from service to perform a line repair. Reportable per Technical Spe- l 0 3 No o 4 l cification AC 7.5.2(b)2 operation under degraded mode permitted by LCO 4.2.2.

No af fect on public health or l o 5 l accompanying occurrence or probable consequences.

I o s I safe ty .

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o18 l so SYSTEM CA USE CAUSE COMP. VALVE CODE CODE SUSCODE COMPONENT CODE SUSCOOE SU8 CODE o 9 l C i s l@ ly_]@ 18 l@ lP 1l PI El xl x @ l Alh lZ lh 12 13 18 19 20 7 8 9 10 11 CCCUR RENCE REPORT R EVISION SE OUENTI AL EVENT YE AR REPORT NO. CODE TYPE NO.

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, 21 22 23 24 26 27 28 29 30 31 ME HOURS S8 i FOR 8. SU Li MANUFA RER TAKEN AC CN ON PLANT l33A l@l34 Zl@ l'35 Zl@ lM Zl@ 31 0l 0l 0l 0l 40 W Q lNjg lN 41 42 4

@ lu Xl 9l 9 l 9lg 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l A hole in the recirculation line to the ou=o recuired that the pu=o be taken out of l i i l service for repair. The line was repaired, inspected. and the ouma returned to [

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% POWER OTHER STATUS D1 O RY DISCOVERY DESCRidTION ST S lAl@l Review of Plant Records l i s W@ l 0l 6l 5l@l N/A l ACT1vlTY CO TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE i e ]Zl RELEASE @D OF RELE ASElZ lgl N/Al l N/A 80 8 9 10 11 44 45 7

PERSCNNEL ExPCSURES NUMBER TYPE DESCRIPTION l

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  • ERSONNE t iNau' RIES .9;p;f. A,.

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i 3 8 9 0[0l0l@l N/A11 12 go LOSS OF OR DAVAGE TO 5ActLtTV

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(SS E DE CA)PTION ll ll lll l ll ltjj 2l0 l l Ni A l I

NAME OF DREPARER /[ _

J . W. Gahm PHONE.

(303) 785-2253

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