ML19207C214

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LER 79-025/03X-0:on 790806,during Steady State Operation at 45% Thermal Power,Emergency Diesel Generator a Found in Degraded Mode, & B Engine Also Declutched.Caused by Relay Failure Due to Normal End of Life.Relay Replaced
ML19207C214
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 08/31/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19207C215 List:
References
LER-79-025-03X, LER-79-25-3X, NUDOCS 7909100481
Download: ML19207C214 (1)


Text

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DATE 80 7 8 60 61 DOCK ET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEOUENCES h o 2 l On Augus t 6,1979 durine stendv state operations at 45% thermal power and 145 MW o 3 1 electrical power, "A" emergency diesel generator was found in a degraded mode per Fort Vrain Technical Specification LCO 4.6.1. This is reportable per Fort St. Vrain l o 4 I S t.

0g. l Technical Specification AC 7.5.2(b)2. When "A" diesel engine declutched "B" diesel l 0 is l engine also declutched. Redundant equipment was operable and available. There was l 0 7 lno af fect on public health or safety. l 0 8 7 8 9 COMP.

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34 05 3 40 42 43 64 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS ii o lA relav f ailed due to normal end o f life. The unit had been tested satisfactorily I i i Ithe orevious month. The relav was replaced and tested and the surveillance succern- 1 1 2 i fully completed. I I

i a l 1 4 l 8 3 30 STA S  % POWER OTHE R STA TUS SO RY DISCOVERY 0ESCRIPTION

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NAME OS PREPARER

[g(( - J. W. Gahm PHCNE:

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