05000325/LER-1979-052-03, /03L-0 on 790728:during Startup,Rods 26-15 & 18-23 Had No Position Indication at Notchs 38 & 30,respectively. Caused by Faulty Prototypic Inlet Piping Probe in Drywell. Problems Will Be Corrected During Next Outage

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/03L-0 on 790728:during Startup,Rods 26-15 & 18-23 Had No Position Indication at Notchs 38 & 30,respectively. Caused by Faulty Prototypic Inlet Piping Probe in Drywell. Problems Will Be Corrected During Next Outage
ML19207B469
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/24/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19207B464 List:
References
LER-79-052-03L, LER-79-52-3L, NUDOCS 7908290514
Download: ML19207B469 (1)


LER-1979-052, /03L-0 on 790728:during Startup,Rods 26-15 & 18-23 Had No Position Indication at Notchs 38 & 30,respectively. Caused by Faulty Prototypic Inlet Piping Probe in Drywell. Problems Will Be Corrected During Next Outage
Event date:
Report date:
3251979052R03 - NRC Website

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