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Category:Letter
MONTHYEAR05000316/LER-2024-004, AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications2024-11-11011 November 2024 AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications IR 05000315/20240032024-10-31031 October 2024 Integrated Inspection Report 05000315/2024003 05000316/2024003 07200072/2024001 and Exercise of Enforcement Discretion AEP-NRC-2024-77, U2C28 Steam Generator Tube Inspection Report2024-10-21021 October 2024 U2C28 Steam Generator Tube Inspection Report AEP-NRC-2024-80, Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Cask2024-10-15015 October 2024 Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Cask AEP-NRC-2024-79, Unit 2, Independent Spent Fuel Storage Installation - Registration of Dry Spent Storage Cask2024-09-26026 September 2024 Unit 2, Independent Spent Fuel Storage Installation - Registration of Dry Spent Storage Cask AEP-NRC-2024-78, Reply to a Notice of Violation: EA-24-0472024-09-23023 September 2024 Reply to a Notice of Violation: EA-24-047 05000316/LER-2024-002-01, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-09-12012 September 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak IR 05000315/20244022024-09-10010 September 2024 Security Baseline Inspection Report 05000315/2024402 and 05000316/2024402, Independent Spent Fuel Storage Installation Security Inspection Report 07200072/2024401 AEP-NRC-2024-69, Core Operating Limits Report2024-09-0909 September 2024 Core Operating Limits Report IR 05000315/20243012024-09-0505 September 2024 NRC Initial License Examination Report 05000315/2024301 and 05000316/2024301 ML24225A0022024-09-0303 September 2024 Issuance of Amendment Nos. 363 and 344 Revising Technical Specifications Section 3.8.1, AC Sources-Operating, for a One-Time Extension of a Completion Time IR 05000315/20240112024-08-30030 August 2024 NRC Inspection Report 05000315/2024011 and 05000316/2024011 and Notice of Violation AEP-NRC-2024-76, Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating2024-08-28028 August 2024 Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating AEP-NRC-2024-51, Annual Report of Loss-Of-Coolant Accident Evaluation Model Changes2024-08-28028 August 2024 Annual Report of Loss-Of-Coolant Accident Evaluation Model Changes 05000316/LER-2024-003, Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage2024-08-22022 August 2024 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage IR 05000315/20240052024-08-21021 August 2024 Updated Inspection Plan for Donald C. Cook Nuclear Plant, Units 1 and 2 (Report 05000315/2024005 and 05000316/2024005) AEP-NRC-2024-61, Unit 2 - Response to Request for Additional Information for Neutron Flux Instrumentation License Amendment Request2024-08-15015 August 2024 Unit 2 - Response to Request for Additional Information for Neutron Flux Instrumentation License Amendment Request ML24221A2702024-08-0808 August 2024 Unit 2 Independent Spent Fuel Storage Installation - Registration of Dry Spent Fuel Storage Cask AEP-NRC-2024-62, Unit 2, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Cask2024-08-0707 August 2024 Unit 2, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Cask ML24256A1482024-08-0202 August 2024 2024 Post Examination Submittal Letter AEP-NRC-2024-47, Form OAR-1, Owners Activity Report2024-07-30030 July 2024 Form OAR-1, Owners Activity Report ML24183A0162024-07-25025 July 2024 Review of Reactor Vessel Material Surveillance Program Capsule W Technical Report ML24169A2142024-07-25025 July 2024 Issuance of Amendment No. 362 Regarding Change to Technical Specification 3.4.12, Low Temperature Overpressure Protection System IR 05000315/20240022024-07-24024 July 2024 Integrated Inspection Report 05000315/2024002 and 05000316/2024002 ML24197A1262024-07-15015 July 2024 Unit 2 - Request for Additional Information (RAI) for License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating 05000316/LER-2024-002, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-07-15015 July 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak ML24191A0692024-07-0909 July 2024 Operator Licensing Examination Approval - Donald C. Cook Nuclear Power Plant, July 2024 AEP-NRC-2024-56, Unit 2, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Cask2024-07-0808 July 2024 Unit 2, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Cask AEP-NRC-2024-48, Response to Request for Additional Information (RAI) for License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating2024-07-0202 July 2024 Response to Request for Additional Information (RAI) for License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating ML24176A1012024-06-21021 June 2024 57143-EN 57143 - Paragon Energy Solutions - Update 1 (Final) - 10CFR Part 21 Final Notification: P21-05242024-FN, Rev. 0 AEP-NRC-2024-45, Report Per Technical Specification 5.6.6 for Inoperability of Post Accident Monitoring Neutron Flux Monitoring2024-06-13013 June 2024 Report Per Technical Specification 5.6.6 for Inoperability of Post Accident Monitoring Neutron Flux Monitoring ML24163A0132024-06-12012 June 2024 Request for Information for the NRC Age-Related Degradation Inspection: Inspection Report 05000315/2024012 and 05000316/2024012 ML24159A2522024-05-30030 May 2024 10 CFR 50.71(e) Update and Related Site Change Reports AEP-NRC-2024-23, Core Operating Limits Report2024-05-23023 May 2024 Core Operating Limits Report ML24141A2162024-05-20020 May 2024 —Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes Inspection 05000316/LER-2024-001, Reactor Trip Due to Main Turbine Trip from a High-High Thrust Bearing Position Trip2024-05-20020 May 2024 Reactor Trip Due to Main Turbine Trip from a High-High Thrust Bearing Position Trip AEP-NRC-2024-40, Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating2024-05-16016 May 2024 Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating AEP-NRC-2024-41, Annual Radiological Environmental Operating Report2024-05-15015 May 2024 Annual Radiological Environmental Operating Report IR 05000315/20240012024-05-14014 May 2024 Integrated Inspection Report 05000315/2024001 and 05000316/2024001 IR 05000315/20244012024-05-14014 May 2024 – Security Baseline Inspection Report 05000315/2024401 and 05000316/2024401 AEP-NRC-2024-26, Transmittal of Donald C. Cook Nuclear Plant, Emergency Plan Revision 492024-05-14014 May 2024 Transmittal of Donald C. Cook Nuclear Plant, Emergency Plan Revision 49 AEP-NRC-2024-07, Unit 2 - Transmittal of Report of Changes to the Emergency Plan2024-05-14014 May 2024 Unit 2 - Transmittal of Report of Changes to the Emergency Plan AEP-NRC-2024-24, Form OAR-1, Owners Activity Report2024-05-0707 May 2024 Form OAR-1, Owners Activity Report ML24115A2152024-05-0707 May 2024 LTR: CNP Non-Acceptance with Opportunity TS 3-8-1 ML24256A1472024-05-0606 May 2024 DC Cook 2024 NRC Examination Submittal Letter: Submittal ML24116A0002024-05-0202 May 2024 – Regulatory Audit in Support of Review of the Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors AEP-NRC-2024-35, Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations2024-04-30030 April 2024 Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations AEP-NRC-2024-28, 2023 Annual Radioactive Effluent Release Report2024-04-29029 April 2024 2023 Annual Radioactive Effluent Release Report AEP-NRC-2024-31, Annual Report of Individual Monitoring2024-04-24024 April 2024 Annual Report of Individual Monitoring AEP-NRC-2024-02, Unit 2 License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating2024-04-0303 April 2024 Unit 2 License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating 2024-09-09
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000316/LER-2024-004, AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications2024-11-11011 November 2024 AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications 05000316/LER-2024-002-01, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-09-12012 September 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak 05000316/LER-2024-003, Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage2024-08-22022 August 2024 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage 05000316/LER-2024-002, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-07-15015 July 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak 05000316/LER-2024-001, Reactor Trip Due to Main Turbine Trip from a High-High Thrust Bearing Position Trip2024-05-20020 May 2024 Reactor Trip Due to Main Turbine Trip from a High-High Thrust Bearing Position Trip 05000315/LER-2023-002, Failure of Unit 1 West Auxiliary Feedwater Pump to Restart During Load Sequencer Testing2023-12-12012 December 2023 Failure of Unit 1 West Auxiliary Feedwater Pump to Restart During Load Sequencer Testing 05000315/LER-2023-001, Two Trains of Fuel Handling Area Exhaust Ventilation Inoperable2023-09-28028 September 2023 Two Trains of Fuel Handling Area Exhaust Ventilation Inoperable 05000315/LER-2022-003-01, Automatic Trip on Losss of Flow Due to Reactor Coolant Pump Trip2023-02-22022 February 2023 Automatic Trip on Losss of Flow Due to Reactor Coolant Pump Trip 05000316/LER-2022-001, Automatic Reactor Trip Due to Steam Generator High-High Level2023-01-0404 January 2023 Automatic Reactor Trip Due to Steam Generator High-High Level 05000315/LER-2022-003, Automatic Reactor Trip on Loss of Flow Due to Reactor Coolant Pump Trip2022-10-19019 October 2022 Automatic Reactor Trip on Loss of Flow Due to Reactor Coolant Pump Trip 05000315/LER-2022-002, Ice Condenser Door Inoperable Resulting in a Condition Prohibited by Technical Specifications2022-09-20020 September 2022 Ice Condenser Door Inoperable Resulting in a Condition Prohibited by Technical Specifications 05000315/LER-2022-001, Manual Reactor Trio Following Manual Turbine Trio Due to High Vibrations on Main Turbine2022-07-21021 July 2022 Manual Reactor Trio Following Manual Turbine Trio Due to High Vibrations on Main Turbine 05000316/LER-2021-002, Re Manual Reactor Trip Due to an Unisolable Steam Leak2021-08-18018 August 2021 Re Manual Reactor Trip Due to an Unisolable Steam Leak 05000315/LER-2021-001, Main Steam Safety Valve Setpoints Found Outside Technical Specifications Limits2021-06-10010 June 2021 Main Steam Safety Valve Setpoints Found Outside Technical Specifications Limits 05000316/LER-2020-004-01, Regarding Unit 2 Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level2021-02-25025 February 2021 Regarding Unit 2 Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level 05000316/LER-2020-004, Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level2020-12-0909 December 2020 Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level 05000315/LER-2020-001, Containment Closure Requirements Not Met During Refueling Operations2020-12-0909 December 2020 Containment Closure Requirements Not Met During Refueling Operations 05000316/LER-2020-003, Manual Reactor Trip and Automatic Safety Injection Due to Failed Open Pressurizer Spray Valve2020-11-0202 November 2020 Manual Reactor Trip and Automatic Safety Injection Due to Failed Open Pressurizer Spray Valve 05000316/LER-2020-002, Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Leakage2020-06-25025 June 2020 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Leakage 05000316/LER-2020-001, Failure of Source Range Nuclear Instrumentation Resulting in a Condition Prohibited by Technical Specifications2020-01-0909 January 2020 Failure of Source Range Nuclear Instrumentation Resulting in a Condition Prohibited by Technical Specifications 05000315/LER-2019-002, Condition Prohibited by Technical Specification Due to an Inoperable Steam Generator Stop Valve Dump Valve2019-11-26026 November 2019 Condition Prohibited by Technical Specification Due to an Inoperable Steam Generator Stop Valve Dump Valve 05000316/LER-2017-0012017-05-19019 May 2017 1 OF 5, LER 17-001-00 for Cook, Unit 2 re Containment Hydrogen Skimmer Ventilation Fan #1 Inoperable Longer than Allowed by Technical Specifications 05000316/LER-2016-0022017-02-0909 February 2017 Emergency Diesel Generators Declared Inoperable Due to a Manufacturing Design Issue, LER 16-002-00 for Donald C. Cook Nuclear Plant Unit 2 Regarding Emergency Diesel Generators Declared Inoperable Due to a Manufacturing Design Issue 05000316/LER-2016-0012016-08-31031 August 2016 Manual Reactor Trip Due To Moisture Separator Heater Expansion Joint Failure, LER 16-001-00 for Donald C. Cook Nuclear Plant, Unit 2 Regarding Manual Reactor Trip Due To Moisture Separator Heater Expansion Joint Failure ML16193A3902016-07-15015 July 2016 Donald C. Cook Nuclear Plant Unit 2 - A Loss of Main Condenser Event Occurred Due to a Storm-Induced Debris Damage of the Circulating Water System Pumps in the Forebay (LER-316-2014-003-00) 05000315/LER-2015-0022016-01-18018 January 2016 -Technical Specification Violation due to Inoperable Residual. Heat Removal Pump, LER 15-002-01 for D.C. Cook, Unit 1, Regarding Technical Specification Violation Due to Inoperable Residual Heat Removal Pump 05000316/LER-2015-0012016-01-15015 January 2016 Manual Reactor Trip Due To A Secondary Plant Transient, LER 15-001-01 for D.C. Cook, Unit 2, Regarding Manual Reactor Trip Due to a Secondary Plant Transient ML0528703602005-10-0505 October 2005 Special Report for D. C. Cook Unit 2 Re Unit 2 Reactor Coolant Inventory Tracking System ML0508903452005-03-22022 March 2005 LER 99-001-01 Donald C. Cook Nuclear Plant Unit 2, Regarding Supplemental LER for Degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations ML0210601432002-04-12012 April 2002 LER 02-02-00, Donald C. Cook Nuclear Plant Unit 2, Technical Specification 3.9.4.c Was Violated During Core Alteration ML0209205342002-03-15015 March 2002 LER 99-012-01 for Cook Nuclear Plant, Unit 1 Re Auxiliary Building ESF Ventilation System May Not Be Capable of Maintaining ESF Room Temperature Post-Accident ML9936300511999-12-20020 December 1999 LER 99-S004-00, Intentionally Falsifying Documentation Results in Unauthorized Unescorted Access, on 11/18/99. with Letter Dated 12/20/99 05000315/LER-1999-027, LER 315/99-027-00, Underrated Fuses Used in 250 Vdc System Could Result in Lack of Protective Coordination1999-11-29029 November 1999 LER 315/99-027-00, Underrated Fuses Used in 250 Vdc System Could Result in Lack of Protective Coordination ML18219E1521978-09-27027 September 1978 Submit Licensee Event Report Nos. RO 78-051/03L-0 & RO 78-052/03L-0 ML18219B5201978-09-27027 September 1978 09/27/1978 Letter Enclosure of Licensee Event Report ML18219B5211978-09-19019 September 1978 09/19/1978 Letter Enclosure of Licensee Event Report ML18219E1531978-09-18018 September 1978 Submit Licensee Event Report No. RO 78-050/03L-0 ML18219B5541978-09-18018 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Report (RO 78-062/03L-0) ML18219E1541978-09-12012 September 1978 Submit Licensee Event Report No. RO 78-049/03L-0 ML18219B5551978-09-12012 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-56/03L-1 and RO 78-061/03L-0) ML18219B5561978-09-0808 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-059/03L-1 and RO 78-060/03L-0) ML18219E1551978-09-0808 September 1978 Submit Licensee Event Report No. RO 78-048/03L-0 ML18219B5571978-09-0505 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting License Event Report RO 78-059/03L-0 ML18219B5581978-08-30030 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Report RO 78-058/03L-0 ML18219B5621978-08-22022 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-056/03L-0 and RO 78-057/03L-0) ML18219B5611978-08-18018 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-052/03L-0, RO 78-053/03L-0, RO 78-054-03L-0 and RO 78-055/03L-0) ML18219E1561978-08-15015 August 1978 Submit Licensee Event Report No. RO 78-047/03L-0 ML18219E1571978-08-14014 August 1978 Submit Licensee Event Report Nos. RO 78-045/03L-0 & RO 78-046/03L-0 ML18219E1581978-08-14014 August 1978 Submit Licensee Event Report Nos. RO 78-043/03L-1 & RO 78-044/03L-1 ML18219E1601978-08-11011 August 1978 Submit Licensee Event Report Nos. 1978-043-03L & 1978-044-03L 2024-09-12
[Table view] |
Text
NUCLEAR REGULATORY COMMISSION DOCKET NUMBER NRC FORM ~195 I2 7g)
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SO- 3(A FILE NUMBER
'NRC DISTRIBUTION FoR ART 50 DOCKET MATERIAL INCIDENT REPORT Tp. J G Keppler FROM: Indiana & Michigan P1m Co DATE OF DOCUMENT l"24-77 Brid'gman, .Mich R W Jurgensen DATE RECEIVED gLETTE goRIGINAI R>> 0 NOTOR IZE 0' PROP INPUT FORM NUMBER OF COPIES RECEIVED
"~ kfUNCLASSIFIED ~ one signed COP Y DESCRIPTION ENCLOSURE
.Ltr ts'ans the follo17ing: RO 76- 9)-on 12-24-76'alent og Reactor coolant malysis tw iodine scapi e~ollowing transient,;...',
du'e'ower lp'LANT NAME Cook g ]
NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J COLLINS
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NRC FORM 196 (2 7B)
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'%rneramn G,*i:M~ED 8 MCO~llX DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 January 24, 1977 Freed~ >~7>
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Mr. J. G. Keppler., Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevel t Road Glen El lyn, IL 60137 Operating Li cense DPR-58 Docket No. 50-315
Dear Mr. Keppler:
Pursuant to the requirements of Appendix A Technical Specifications and the United States Nuclear Regulatory Commission Regulatory Guide 1.16, Revision 4, Section 2.b, the following report is submi tted:
RO-50-315/76-59 Sin ce rely,
. W. Ju ens Plant M nager 'RegutBto>'u ":Ip RW J/mj
>> g'ac cc: R. S. Hunter J. E. Dolan G. E. Lien R. Ki ~ lb urn R. J.'Vollen BPI R. C. Callen MPSC K. R. Baker RO: III R. Walsh, Esq.
P. W. Steketee, Esq.
G. Charnoff, Esq.
G. Olson J. M. Hennigan PNSRC R. S. Kei th Dir., IE (30 copies)
Dir., MIPC (3 copies)
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Llt"ENSEE EVENT REPORT CONTROL BLOCK: SE PRINT ALL REQUIRED INFORIVIATIOM3 6""
1'ICENSEE LICENSE EVENT NAME LICENSE NUMBER TYPE TYPE
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- 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT OATE Ion~Icon'~ L ~L 0 5 0 0 3 1 5 68 69 1 2 2 4 7 5 74 0
75 1 2 4 7, 7 80 7 8 57 58 59 60 61 I
EVENT DESCRIPTION Qpg ON DECEMBER 23'976 AT 2100 HOURS POWER REDUCTION WAS STARTED WITH THE UNIT TRIPPED 7 8 9 80 FROM APPROXIMATELY 7X AT 0008 HOURS ON DECEMBER 24, 1976. REACTOR COOLANT ANALYSIS 7 89 ~ .. 80
[oOP4 SHOWED DOSE E UIVALENT I-131 ACTIVITY TO BE 3.1 uCi m. THIS IS IN EXCESS OF LIMIT 7 8 9 7 8 9 80
[oaf R0-50-315/76-52,0N NOVEMBER 20, 1976. (RO-50-315/76- 59 )
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-80 SYSTEM CAUSE COMPON84T COMPONENT CODE CODE COMPONENT CODE SUPPLER MANUFACTURER Ioc7I ~zz ~F z z z z z Z
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48 7 8 9 10 .11 12 CAUSE DESCRIPTION
[oOs] SEE SUPPLEMENT 7 8 9 80
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7 8 9 80 QO]
89 80 FACIUTY STATUS POWER 'THER STATUS METHOD OF DISCOVERY DISCOVERY DESCRIPTION
@171 ~G ~00 0 NA 44 45 46 ROUTINE SAMPLING 80 7 8 9 10 .12 13 FORM OF ACTIVITY COATENT REI.EASED OF RELEASE, AMOUNT OF ACTIVITY LOCATiON OF RELEASE 2J Z Z NA
~ 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q~aj ~00 0 Z NA 80 7 89 11 12 13 PERSONNEL INJURIES 7 8 9" 11 12 80 PROBAHLTE CONSEQUENCES Qqg NA 7 8 9 80 LOSS OR DAMAGE TO FACIUTY PE OESCIIIATION 7 89 ~ 10 PUBLICITY NA 7 89 80 ADBITIONAL FACTORS Q~e] NA 7 89 80
~18 NA 7 89 80 J L RI SCHL I NG PHGNE(616)465-5901(368)
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~ i SUPPLEME 0 REPORTABLE OCCURRENCE RO 50 5 76 59 ff INDIANA & MICHIGAN'OWER COMPANY DONALD C. COOK NUCLEAR PLANT Iodine S'ike Followin PowerTransient As this shutdown was planned and, due to the iodine spiking noted following reactor trip on November 20, 1976, a revised sampling program had been set up to increase the data collection frequency. This program consisted of collecting samples each two hours prior to unit shutdown, each half hour for the first four hours following reactor trip and each two hours after that period until data stabilized.
Reactor power had been slowly decreasing during the week prior to shutdown due to core stretch out, with power in the 90%%d range 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first out-of-specification sample.* On December 23, 1976, at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, reactor power reduction was started with the unit tripped from approximately 7S power at 0008 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> on December 24, 1976. In pre-paration for shutdown, CVCS purification flow had been increased to maximum (120-125 gpm) on December 13, 1976, and maintained at this level through shutdown.", Volume control tank hydrogen pressure was reduced at 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> on December 23, 1976, in preparation for degassing of the system with remain-ing degassing operations (VCT level increase and venting to the gas header) starting at 1820 hours0.0211 days <br />0.506 hours <br />0.00301 weeks <br />6.9251e-4 months <br /> on December 24, 1976, with three tank purges completed by 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> on December 25, 1976.
Primary coolant I-131 activity following return to equilibrium after the November 30, 1976 reactor trip had stabilized at 1.5-- 2.0xlO-z wCi/cc.~
I-131 activity remained at this level until 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> on December 24, 1976 when the activity increased to 2.5 yCi/cc, approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> following initiation of power reduction. Iodine release at this time period is consis-tent with data reported in Westinghouse Electric Corporation WCAP-8637, "Iodine Behavior Under Transient Conditions in the Pressurized Water Reactor." The increased data collection sampling frequency after the spike indicates that the I-131 activity began decreasing immediately following the initial spike with values remaining constant at approximately 1.6 pCi/cc for an 8 - 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> period before further decrease (See Figure 2). I-133, 135 values showed trends similar to the I-131 activity (Figure 3). DOSE E(UIVALENT I-131 values peaked at 3. 1 pCi/gm at 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> on December 24, 1976, with values exceeding the 1.0 pCi/gm specification for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after the spike. DOSE EQUIVALENT I-131 values were in the "Acceptable Operation" portion of Technical Specifications Figure 3.4-1 at all times during the transient.*
Fuel burnup by core region is indicated in Table 1.
As iodine values began decreasing immediately following the spike and have remained at low values during fuel movement operations (1.5x10 " pCi/cc) and with all data similar to that following the November 20, 1976, incident, the December 24, 1976 spike is also attributed to the normal spiking phenomena during power transients rather than fuel clad failure. No iodine spiking was noted during depressurization of the reactor coolant system.
- See Figure 1 Coolant samples are brought to ambient conditions before counting; therefore, units of pCi/cc and pCi/gm are interchangeable.
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INDIANA 8 MICHIGAN POKIER COMPANY DONALD C. COOK NUCLEAR PLANT TABLE 1 FUEL BURNUP BY CORE REGION REGION NO. BURNUP FOR CUMULATIVE ENERGY FOR CUMULATI>/E PERIOD BURNUP PERIOD ENERGY (MMD/MTU (MHD/MTU) (BTU), (BTU) 0.3023E+04 0.1894+05 0.7285+13 0.6565+14 0 '272+04 0. 1915+05 0. 7803+13 0. 4566+14
- 3. 0.2375+04 0.1350+05 0.5632-:13 0.3201+14 Core Total 0.2891+04 0.1721+05 0.2072+14 0.1233+15 Period: October 1, 1976 - December 30, 1976
INDIANA 5 MICHIGAN POWER COMPANY DONALD C. COOK t'IUCLEAR PLANT TABLE 1 FUEL BURNUP BY CORE REGION REGION NO. BURNUP FOR CUMULATIVE Ei'lERGY FOR CUMULATIVE PERIOD BURNUP PERIOD ENERGY (MWD/MTU) 'MWD/MTU (BTU) (BTU) 0.3023E+04 0.1894+05 0.7285+13 0.6565+14
- 2. 0.3272+04 0 '915+05 0.7803+13 0.4566+14
- 3. 0.2375+04 0.1350+05 0.5632+13 0.3201+14 Core Total 0.2891+04 0.1721+05 0.2072+14 0.1233+15 Period: October 1, 1976 - December 30, 1976
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