ML18101A358

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Insp Repts 50-272/94-24 & 50-311/94-24 on 940918-1105. Violations Noted.Major Areas Inspected:Public Health & Safety During Day & Backshift Hours of Station Activities, Including Emergency Preparedness,Security & Engineering
ML18101A358
Person / Time
Site: Salem  
Issue date: 11/28/1994
From: Jason White
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18101A356 List:
References
50-272-94-24, 50-311-94-24, NUDOCS 9412060124
Download: ML18101A358 (21)


See also: IR 05000272/1994024

Text

,*

Report Nos.

License Nos.

Licensee:

Facility:

Dates:

Inspectors:

Approved:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/94-24

50-311 /94-24

DPR-70

DPR-75

Public Service Electric and Gas Company

P.O. Box 236

Hancocks Bridge, New Jersey 08038

Salem Nuclear Generating Station

September 18, 1994 - November 5, 1994

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Resident rn*sp,,ector

T. H.

F~~h, ~esident Inspector


~~:zf'..f_!_~~~~Z':::~~------------------

J.

ll~ White, Chief, Reactor Projects

/

Section 2A

Inspection Summary:

_!..'.L-_~i..LL __

Date

This inspection report documents inspections to assure public health and

safety during day and backshift hours of station activities, including:

operations, radiological controls, maintenance and surveillance testing,

emergency preparedness, security, engineering/technical support, and safety

assessment/quality verification. The Executive Summary delineates the

inspection findings and conclusions .

9412060124 941128

PDR

ADOCK 05000272

Q

PDR

SALEM EXECUTIVE SUMMARY

Salem Inspection Reports 50-272/94-24; 50-311/94-24

September 18, 1994 - November 5, 1994

OPERATIONS

(Modules 40500, 60705, 60710, 71707, 92701, 92901)

Salem management took appropriate action in response to an operator

_

inadvertently closing two Main Steam Isolation Valves.

The inspector observed

good housekeeping in containment, excellent radiation protection pre-job

briefings and coverage, and thorough inspection and detailed deficiency

documentation by the Containment Walkdown Team.

The licensee took appropriate

corrective actions for peeling paint in containment and lube oil leakage from

reactor.coolant pump oil collection systems.

Plant staff conducted fuel

handl.ing activities safely. Inspectors noted management oversight of

refueling activities. For an hour and 32 minutes during irradiated fuel

movements, the licensee failed to assure containment integrity as required by

Technical Specification 3.9.4. This is an apparent violation .. In response to

identification of missed check valve surveillances, operations performed an

operability determination of significantly improved quality over previous

efforts.

MAINTENANCE AND SURVEILLANCE

(Modules 61726, 62703, 92902, TI 2515/125)

PSE&G did not take adequate corrective action to preclude recurrence of work

control inadequacies that occurred during the Salem Unit 1 fall 1993 refueling

outage.

As a result, on three occasions during the reporting period, workers

improperly performed outage work activities which contributed to the potential

for serious personnel injury.

The plant staff did not adequately address vacuum pump inlet valye

deficiencies.

As a result, valve mis-operation caused a reduction of

condenser vacuum.

Quick response by operators precluded a reactor trip.

The inspectors con~uded that Salem had adequate controls to prevent foreign

materials from entering and remaining in safety systems.

Plant staff properly

planned, controlled and conducted complex main steam safety relief valve

testing.

Operators failed to perform a nuclear instrumentation calorimetric within the

time required by Technical Specifications. This is an apparent violation.

Maintenance staff and supervisors performed outage maintenance on the 2C

diesel generator carefully and appropriately.

Poor communication between

system engineers and operations concerning centrifugal charging pump

vibrations resulted in a requirement for operators to conduct an accelerated

Salem Unit 2 shut down to comply with Technical Specifications .

ii

ENGINEERING AND TECHNICAL SUPPORT (Modules 37551, 71707, 92700,)

The licensee initially failed to critically evaluate a condition that had the

potential to involve corrosion on the auxiliary feedwater (AFW) piping.

Once

they initiated an investigation, the licensee thoroughly and adequately

addressed the piping concerns.

Marginal control air system performance continued to challenge normal plant

operation.

The inspectors concluded that the licensee responded appropriately

to the inadequately tapped fuel header bolt holes and inadequately torqued

fuel oil header bolts.

The licensee developed a reasonable basis to conclude that sustained Salem

Unit 2 operation at levels up to 102.6% did not compromise plant safety.

However, failure to consider the worst case implications of increased electric

generation indicated weaknesses in problem identification, resolution, and

safety perspective. Failure to promptly identify and correct the overpower

condition is a apparent violation.

PLANT SUPPORT (Modules 71707, 71750, 92700)

Radiation Protection demonstrated consistently strong performance throughout

the inspection period.

Inspectors noted a large number of corrective

maintenance activities for the plant radiation monitors, though the trend has

been decreasing for the last three years.

The inspectors concluded that the

frequent degraded condition of the radiation monitors tended to be a constant

distraction to operators and required frequent compensatory action.

The

inspectors also noted that plant management recently increased efforts to

improve radiation monitoring equipment reliability through improved

maintenance and greater emphasis on developing a long term solution.

A security guard failed to control, access to a vital area. This- is an

apparent violation of security plan requirements.

On September 7, PSE&G

announced that they had named Mr. Leon Eliason President and Chief Nuclear

Officer of the newly formed PSE&G Nuclear Business Unit.

In addition, on

September 8, PSE&G announced that they had named Mr. John Summers to the

position of Salem Mechanical Maintenance Manager for a one year period.

The inspectors noted that Salem and Engineering and Plant Betterment (E&PB)

managers had performed various levels of analysis to identify areas for

performance improvement.

The E&PB and Operations analyses and improvement

plans, in particular, demonstrated thorough analysis and carefully mapped out

action plans. Other departments had less formal plans with fewer means to

track improvement.

Senior management stated that measures had been initiated

to establish a more uniform approach to improving performance .

iii

TABLE OF CONTENTS

TABLE OF CONTENTS . * * .

1.0

SUMMARY OF OPERATIONS ..

I.I

Salem Units I and 2 .

. . .

'

iv

I .

I

. 2. 0

OPERATIONS

  • * . * * * . .

. . * . . . . . . . . . .

I

3.0

4.0

5.0

6.0

7.0

2.1

Inspection Activities ..*..**..... ~ . . . . * . .

I

2.2

Inspection Findings and Significant Plant Events

. . . .

I

MAINTENANCE AND SURVEILLANCE TESTING

. * . *

3.1

Maintenance Observations ...*.

3.2

Surveillance Observations

3.3

Inspection Findings .

ENGINEERING . . . . . . . . . .

PLANT SUPPORT . . . . . * . . . . . . . . .

5.1

Radiological Controls and Chemistry .

5. 2 * Emergency Preparedness . . . . . .

. . . . . . . .

5.3

Security .......

-............. .

5.4

Safety Assessment and Quality Verification ... .

LICENSEE EVENT REPORTS (LER), PERIODIC AND SPECIAL REPORTS, AND

OPEN ITEM FOLLOWUP

. . .

6.1

LERs and Reports ... .

6.2

Open Items .... .

EXIT INTERVIEWS/MEETINGS

.

. . . . . .

  • 7.1

Resident Exit Meeting .......... .

7.2

Salem Specialist Entrance and Exit Meetings

7.3

Management Meetings ......... .

iv

4

4

5

5

10

13

13

14

14

14

15

15

16

16

16

17

17

1.0

1.1

SUMMARY OF OPERATIONS

Salem Units 1 and 2

DETAILS

Unit 1 operated at power throughout the report period.

Unit 2 began the period at 100% power.

On September 22, 1994, as a result of

high centrifugal charging pump vibration, operators shut the unit down to

comply with a Technical Specification action statement.

On September 27,

operators commenced a reactor startup.

On September 29, operators manually

tripped the reactor when an operator inadvertently closed two main steam

isolation valves at 30% power.

On September 30, operators again commenced a

reactor startup and returned the unit to 100% on October 3.

On October 13,

operators commenced a shutdown for the eighth refueling outage.

The unit

remained in the outage through the end of the report period.

2.0

OPERATIONS

2.1

Inspection Activities

The inspectors verified that Public Service Electric and Gas (PSE&G) operated

the facilities safely and in conformance with regulatory requirements.

The

inspectors evaluated PSE&G management control by direct observation of

activities, tours of the facilities, interviews and discussions with

personnel, independent verification of safety system status and Technical

Specification compliance, and review of facility records.

The inspectors

performed normal and back shift inspections, including 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> of deep back

shift inspections.

2.2

Inspection Findings and Significant Plant Events

A.

Inadvertent Main Steam Isolation Valve (MSIV) Closure

On September 29, with Salem Unit 2 at 30% power during a startup, a control

room operator inadvertently closed two of the four MSIVs.

The operators

recognized the error as the valves began to close, and manually tripped the

reactor in anticipation of a reactor trip on high reactor coolant system

pressure in the pressurizer.

The plant responded as designed. Operations

management reviewed the event and the performance of the operators. They

concluded that the operator had been instructed to close the MSIV warming

valves.

He had correctly repeated back the instructions to close the warming

valves, then removed a protective cover intended to prevent inadvertent MSIV

closure, and closed the valves.

Management concluded that operator

recognition of the error and action to trip the reactor had been prompt and

appropriate.

Based on past performance of the operator making the error,

including an evaluation of previous performance, and at the request of the

operator, operations management removed the operator from duties involving

direct control of plant equipment.

The inspectors considered operations

management actions appropriate.

..

2

B.

Conta;nment Walkdown

On October 14, 1994, the licensee conducted 52.0P-PT.CAN-0001, Containment

Walkdown, at the onset of their refueling outage.

The inspector observed good

housekeeping in containment., excellent radiation protection pre-job briefings

and*coverage, and thorough inspection and detailed deficiency documentation by

the Containment Walkdown Team.

The inspector noted that peeling paint on

walls and floors posed a potential for containment sump clogging. The

inspector determined that the licensee identified the peeling paint, and

planned to address it during the outage.

The inspector observed good

management oversight and attention in this area.

In addition, the inspector noted a significant amount of lube oil coating the

reactor coolant pump {RCP) platforms in containment.

The oily platforms

presented a personnel safety concern, and a thin coating of oil on the stator

windings presented a potential reliability concern.

The inspector noted that

NRG Information Notice 94-58, .Reactor Coolant Pump lube Oil Fire, identified

that some RCP oil collection systems present fire hazards.

Oil leaking from

  • the lube oil system may come in contact with either {l) surfaces that are hot

enough to ignite the oil, or {2) an electrical source of ignition. The

licensee removed the oil to address the personnel safety hazard, and planned

to take action to address the oil leaking from the collection system.

The

inspector noted good communication between maintenance, engineering, and

vendor representatives and considered that the licensee had tak~n appropriate

action.

c.

Refuel;ng Act;v;t;es

At 11:38 p.m. on October 24, 1994, operators began to move fuel from the

reactor core to the spent fuel pool.

At 2:35 p.m. on October 27, operations

completed core offload.

On October 31, reactor engineering, with Westinghouse

support, commenced fuel rod ultrasonic and visual inspection for the offloaded

core.

At the end of the inspection period they had inspected 153 of 193

assemblies. Westinghouse preliminary findings indicated eight leaking

peripheral fuel rods.

The inspector noted that the position of the failed

rods correlated to Westinghouse findings from the Unit 2 seventh refueling

outage.

{Refer to NRC Inspection Report 50-272&311/93-15)

The inspector observed good control of preparations for refueling, new fuel

inspection, core off-load, and failed fuel inspection.

The inspector noted

that, contrary to an internal commitment, the training program for refueling

operators did not review previous fuel handling problems experienced at during

the Hope Creek outage. Operations identified a weakness in the tracking and

implementation of this training, took short-term actions to provide additional

focused training, and initiated a review of refueling training practices for

long-term improvement.

The inspector noted Operations management and Quality

Assurance direct involvement in refueling activities. _However, on two

occasions inspectors identified minor fuel handling equipment deficiencies

known by equipment operators, but not conveyed to management.

3

With the unit defueled, operations relied upon the spent fuel cooling system,

and the ability to connect the Unit 1 spent fuel pool (SFP) cooling to Unit 2.

The licensee failed to implement a procedure change dated October 24, 1993,

following an overflow of the Unit 2 SFP while operating with SFP cooling

systems cross connected (See NRC Inspection Report 50-272&311/93-23).

Upon

recognition, the licensee immediately implemented the procedure change.

The

inspector noted that workers expertly conducted the fuel handling activities.

The inspector observed good communication and coordination between the control

room, containment, and the fuel handling building. The licensee, with

-Westinghouse support, safely off loaded the Unit 2 core.

D.

Containment Isolat;on Dur;ng Core Alterat;ons

At 11:38 p.m. on October 24, 1994, operators began core alterations for the

Unit 2 eighth refueling outage.

At 1:10 a.m. on October 25, operations

suspended core alterations upon discovery of open service water.valves that

provided access from containment directly to the auxiliary building. -A

Bechtel supervisor, working in containment, identified a release pathway from

open service water vent valves in containment to open service water drain

valves outside of containment. - Previously, operators tagged the service water

valves open for planned outage work on containment fan cooling units.

The licensee immediately suspended fuel handling operations upon

identification of the potential release pathway affecting containment

integrity. Operations isolated the service water drain valves outside

containment and verified service water piping intact between isolation valves

and containment. Operations reviewed all maintenance activities and conducted

two independent reviews of tagged valve reports to insure containment

integrity. Operations made an on-the-spot change to S2.0P-ST.CAN-0007,

Refueling Operations - Containment Isolation, to require these independent

reviews.

At 6:05 a.m. on October 25, operations resumed fuel handling

operations.

The irispector noted that the Bechtel supervisor demonstrated good oversight .

The inspector determined that the licensee took prompt and appropriate

corrective action to restore containment integrity. However, the inspector

noted that the licensee took action to preclude recurrence that duplicated

requirements exi~ting at the time of the occurrence.

The SRO failed to

conduct an adequate review prior to the commencement of fuel alterations. The

inspector determined that management did not clearly convey their expectations

concerning the depth of review required to fully satisfy containment integrity

under these conditions. The inspector concluded that failure to assure

containment integrity during the performance of core alterations was a

violation of Technical Specification 3.9.4.

(VIO 50-311/94-24-01)

E.

1PR25 Operab;1;ty

As documented in NRC Inspection Report 50-272&311/94-21 on October 17, the

licensee determined that they had not performed surveillances to verify the

ability of check valves 1PR25 and 2PR25 to permit flow under design

conditions.

The referenced report provides details of the surveillance

requirements and the licensee failure to include the flow verification in the

4

In Service Testing {IST) program.

As a result of the missed surveillance, the

resident inspectors questioned whether the licensee concluded that valve

1PR25 for Salem Unit 1 could perform its design function, and how its

potential inability to perform its intended function affected the associated

ECCS systems (Containment Spray, Safety Injection, Residual Heat Removal).

At

the time, Salem Unit 2 was in a refueling outage.

-The licensee completed an operability determination, and inspectors reviewed

the analysis. The inspectors noted that the licensee, in performing the

determination, had not identified the design flow and pressure conditions for

valve operability. The licensee did not identify a basis to establish that

the valve could permit required flow.

In addition, the licensee did not

establish the effect of insufficient flow through the valve on the associated

ECCS systems.

In response to the inspector questions, the licensee

demonstrated that during quarterly ECCS testing the valve had permitted flow

greater than the expected flow under worst case conditions.

The licensee

concluded that the missed surveillance did not result in plant operation with

undetected degradation of ECCS systems.

The inspectors concluded the licensee appropriately determined that ECCS

remained operable. The inspectors noted that the operability determinations

utilized the recently established operations department guidance.

The

inspectors found that the operations department had significantly increased

the quality of operability determinations.

The inspectors also noted,

however, that lack of consideration of the design conditions (such as

pressur~, flow, etc) required for operability of a compon~nt reduced the

quality of the operability determination process.

3.0

MAINTENANCE AND SURVEILLANCE TESTING

3.1

Maintenance Observations

The inspectors observed selected maintenance activities on safety-related

equipment to ascertain that the licensee conducted these activities in

accordance with approved procedures, Technical Specifications, and appropriate

industrial codes and standards.

The inspector observed portions of the following activities:

Work Order(WO) or Design

Unit

Change Package CDCPl

Description

Salem 2

DCP 2EC-3220

Replacement of Pressurizer

Spray Valve Internals

Salem 2

DCP 2E0-2334

Change out of Trim Set for

Pressurizer Relief Valves

Salem 2

WO 940123023

Inspection of Reactor Vessel

Head Bolting

Salem 2

WO 941020030

CCHX Tube Inspection

Salem 2

Salem 2

Salem 2

Salem 2

WO 941009005

WO 940927031

DCP 2EC-2269

DCP 2EC-3286

5

Service Water Pipe Inspection

21 Auxiliary Feedwater Pump

Suction Check Valve Inspection

Modifications to 21 Station

Power Transformer

Modify Diesel Generator

Intake/Exhaust Piping~

The maintenance activities inspected were effective with respect to meeting

the safety objectives of the maintenance program.

3.2

Surveillance Observations

The inspectors performed detailed technical procedure reviews, witnessed in

progress surveillance testing, and reviewed completed surveillance packages.

The inspectors verified that the surveillance tests were performed in

accordance with Technical Specifications, approved procedures, and NRC

regulations.

The inspector reviewed the following surveillance tests with portions

witnessed by the inspector:

Unit

Procedure No.

Test

Salem 1

Sl.OP-ST.CBV-0003

Containment Systems - Cooling

Systems

Salem 1

Sl.OP-ST.SW-001

Inservice Testing Service

Water Valves

Salem 1

Sl.OP-ST.CBV-0003

Containment Systems - Cooling

Systems

Salem I

SI.OP-ST. SW-001

Inservice Testing Service

Water Valves (CFCUs)

The surveillance testing activities inspected were effective with respect to

meeting the safety objectives of the surveillance testing program.

3.3

Inspection Findings

A.

Maintenance Performance Deficiencies

During the inspection period, the licensee reported several instances of

deficient maintenance performance.

No event had nuclear safety significance.

However, the potential existed for serious industrial safety consequences .

..

6

On October 29, electricians cut through the wrong 4KV electrical cable. The

work procedure directed the electricians to cut existing circulating water

(CW} pump feeder cables into 4 foot sections. The modification package

directed the electricians to remove the section from the cable tray prior to

making the cut.

As a result of interference of other cables and cable trays,

the electrician decided to make a cut without removing the entire length of

cable from the cable tray. Although he believed he had identified the correct

cable, he incorrectly cut a 4KV feeder to the Chemical Treatment building.

Fortunately, operators previously tagged out the feeder to support another

work activity. Fortuitously, the electrician did not sustain any injury.

On November 4, the site services personnel loaded Salem CW trash racks onto a

flatbed truck, using a 55 ton crane.

When the crane swung the load over the

truck, it tipped over slightly injuring the crane operator. The licensee

determined that the crane tipped due to inadequate implementation of controls

designed to insure the outriggers were properly extended.

Also on November 4, a contractor working in the containment on a reactor

coolant pump seal attempted to lower his tool box using improper rigging.

The

box slipped out of the sling and dropped 20 feet to the floor.

The incident

did not result in injury or damage to plant equipment.

The contractor told

the maintenance manager that he knew the rigging method was inadequate because

he had dropped the tool box on two other occasions.

The maintenance manager

immediately removed the contractor from the job and stopped all work on the

reactor coolant pump seal activity.

In response, the licensee stopped all work to review the events with workers,

and reinforce the need to understand and adhere to work controls.

In

addition, the licensee took disciplinary action against responsible

individuals, and emphasized the requirement for effective pre-job briefs. The

inspectors noted that the above mishaps represent additional examples of poor

work control similar to problems previously identified in NRC Inspection

Report 50-272 and 311/93-23 and the subject of NRC Notice of Violation dated

March 9, 1994.

The inspectors noted that the examples described above and the

~xamples. described in NRC Inspection Report 93-23 demonstrate that lice'nsee

  • corrective action efforts have not been totally eff~ctive in precluding

recurrences.

B.

Loss of Condenser Vacuum

At 5:43 a.m. on October 4, 1994, equipment operators removed the no. 24

condenser vacuum pump from service for preventative maintenance.

Control room

operators noted decreasing condenser vacuum and reduced power.

At 5:46 a.m.

equipment operators returned the no. 24 vacuum pump to service. Control room

operators initiated S2.0P-AB.Cond-0001, Loss of Condenser Vacuum.

At 5:50

a.m. operators restored vacuum to normal and stopped the power reduction.

The

licensee determined that the no. 24 vacuum pump inlet valve (24AR25} failed to

close when the vacuum pump was removed from service and subsequently caused

the loss of vacuum.

7

The inspector observed that the west-side vacuum indication did not accurately

reflect condenser pressure, complicating the response to the valve failure.

The inspectors noted that operators identified the instrument problem on

November 16, 1993, and further determined that on August 14, 1993, a work

order was generated to investigate 24AR25, as the valve did not close when the

pump was removed from service. The valve was presumed fixed, and the work

order closed out, when yet another work order was generated for 24AR25 on July

3, 1994.

The work order generated on July 3, 1994 remained open on October 4,

1994.

The inspector concluded that plant staff had not adequately resolved

.this recurrent balance of plant equipment failure.

As a result, it continued

to unnecessarily challenge plant operation.

C.

Foreign Material Exclusion (FME) Controls Temporary Inspection (TI

2515/125)

The inspectors reviewed licensee FME controls to determine if the licensee had

adequate measures to prevent foreign material from inadvertently entering

safety systems during maintenance activities, outages, and routine operations.

The inspectors found that Nuclear Administration Procedure (NAP) 21, System

Cleanliness Program, provided instructions on proper cleaning methods and

provided instructions to prevent the intrusion of debris into the reactor

vessel and into the primary system.

Salem Maintenance Procedure GP.ZZ-6, Tool

and Miscellaneous Items Accountability and Closure Control, provided

instructions that prevent introduction of foreign material (debris, tools)

into open systems.

The procedure-also provided instructions to account for

tools, parts, and material during maintenance, testing, and inspection

activities. Reactor Engineering (RE) procedures for refueling, fuel handling,

and fuel repair referenced NAP-21 and ZZ-6 for controlling debris.

The RE

procedures include additional guidance for controlling activities involving

the spent fuel pool and transfer pool.

Based on a licensee search of the Incident Report data base, the inspectors

concluded that no documented instances of foreign material intrusion occurred

within the previous year, nor did the inspectors recall the occurrence of

foreign material intrusion problems.

The inspectors observed maintenance

activities to determine if foreign material exclusion control procedures were

available and being followed.

The inspector noted acceptable intrusion

control during maintenance activities on the 2C emergency diesel generator,

during fuel handling in the containment, and various other outage related

activities. At the end of the report period, the licensee had completed less

than half of the Salem Unit 2 refueling outage.

Based on the amount of

outage related equipment and material in containment, the inspectors concluded

that effective containment closeout played a central role in preventing loose

material from affecting safety. The inspectors could not assess the

effectiveness of containment closeout prior to the end of the inspection

report due to the duration of the outage.

Based on these observations, the inspector concluded that the licensee

adequately prevented foreign material from entering safety systems during

maintenance outage and routine activities .

8

D.

Auxiliary Feed Pump Trip

surveillance test 52.0P-SP.AF-003, Inservice Testing - No. 23 Auxiliary

Feedwater Pump.

Operators determined that the trip latch was not fully

engaged and vibration on pump startup caused the trip valve to actuate.

Prior to running the pump, the procedure required the operator to ~ress the

emergency trip lever to manually trip the valve through the overspeed trip

mechanism, insuring overspeed protection.

On resetting the trip, the

operator failed to properly engage the trip mechanism.

The licensee

determined that the procedure did not provide sufficient operator guidance to

ensure that the operator fully seated the overspeed trip mechanism (OTM).

The

procedure provided additional verification only if the operator had not

properly seated the OTM.

The procedure had previously required the operator

to properly seat the OTM, and the operator had no reason to suspect that he

had not properly seated the OTM.

The licensee changed the procedure to

require the mechanical check to positively verify trip linkage engagement.

The inspector noted that the No. 23 AFW pump tripped in exactly the same

manner on September 9, 1993.

(See Inspection Report 50-311/93-21)

Following

that occurrence, the licensee made an "on-the-spot" change to the surveillance

to ensure proper trip mechanism engagement.

However, as noted above, the

modified procedure did not require adequate engagement verification.

The inspector determined that the October 7, pump trip had no safety

consequence since the pump was inoperable for the surveillance test. However,

the inspector noted that similar misalignment upon resetting the trip valve at

the conclusion of the surveillance could result in an AFW pump trip for a pump

start under accident conditions. The inspector observed that improper OTM

engagement following completion of a surveillance would be masked by the

requirement to manually trip the pump at the beginning of the next

surveillan,ce. The inspector planned to continue to review the adequacy of the

licensee's evaluation of the AFW pump surveillance activity. (IFI 50-311/94-

24-02)

E.

Missed Surveillance for Nuclear Instrumentation System (NIS)

At 7:45 a.m. on October 13, during a Unit 2 shut down in preparation for the

outage, a technician asked the operating crew for permission to perform a heat

balance calibration of the NIS.

Technical Specifi~ation (TS) 4.3.1.1.1, Table

4.3-1 requires plant staff to perform the calibration once each 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when

  • power is above 15%.

Plant staff performed the previous calibration at 9:51

a.m. on October 12. Believing, incorrectly, that the calibration was a daily

requirement, the shift supervisor stated that he expected power to be below

15% by the end of the day, therefore, the calorimetric would not be required.

The operators continued the plant shutdown, reducing plant power below 15%

after 9:51 p.m., and did not perform a calorimetric during a period of more

than 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Failure to perform the NIS heat balance calibration is a

violation of TS 4.3.1.1.1.

(VIO 50-311/94-24-03)

9

F *.

. Main _Steam Safety Relief Valve Testing

On October*14, 1994, the inspector observed main steam safety valve testing in

place. The inspector noted that plant staff properly planned, carefully

controlled, and safely conducted the complex evolution.

In addition, the

inspector noted good coordination and involvement by maintenance, system

engineering, quality assurance, operations, and maintenance management.

G.

2C Emergency Diesel Generator Maintenance Activities

On October 16, 1994, Salem maintenance staff began a 2C emergency diesel

generator (EOG} outage to perform preventative maintenance, slip ring

machining, air start system piping and valve replacement, and cylinder liner

replacement. Maintenance technicians successfully completed all scheduled

maintenance.

On October 30, operations declared the 2C EOG operable following

satisfactory post-maintenance and operability testing.

Maintenance personnel replaced both 2C diesel air start receiver check valves

and drain valves.

In addition, maintenance replaced the carbon steel piping

between the air compressor and air start receiver in kind. Maintenance

replaced 8 cylinder liners, which were previously replaced in January 1994,

following discovery of a cracked liner in the 2C EOG (see NRC Inspection

Report 50-272&311/93-27).

The replacement liners used in January arrived

without qualification documentation.

In January, maintenance bored several

small holes in a low stress area to qualify the liners for safety-related use.

The licensee planned to evaluate the removed liners for stress iriduced

cracking.

The results of this evaluation has the potential of affecting 18

EOG which also contains cylinder liners with bored metallurgic sample holes.

The inspector determined that the licensee properly planned and conducted the

maintenance.

The inspector observed good work practices, excellent foreign

material exclusion (FME) practices, good procedure use, and effective PSE&G

supervision in the field.

H.

Maintenance of No. 21 Centrifugal Charging Pump

On September 19, plant staff identified inadequate coupler spacing in the No.

21 charging pump speed increaser. After adjustirig the spacing, engineering

staff noted elevated vibration readings during the post maintenance test

  • (PMT}.

The readings had not reached the required action range specified in

t.he IST program.

As a result system engineers concluded that the pump met the

post maintenance acceptance criteria for operability, since the PMT did not

include acceptance criteria for vibration associated with the speed increaser.

The system engineers did not inform operations staff of the increased

vibration. The system engineers did, however, request that operations run the

pump again on night shift to permit gathering more extensive vibration data.

During a two hour run, the system engineering staff found that the vibration

had significantly increased. After approximately two hours of data review,

they informed the operations staff that the pump should be considered

inoperable.

As a result of the system engineering staff input, operations

declared the pump inoperable. They concluded that the pump had been

inoperable since they entered the Technical Specification LCO action statement

10

to begin maintenance, three days earlier. As a result, operations staff

performed an accelerated shut down of Salem Unit 2 to meet the requirements of

Technical Specification 3.0.3.

The inspectors concluded that operations staff, when informed of the vibration

concerns, properly interpreted Technical Specification requirements and

appropriately shut down Salem Unit 2.

The inspectors also concluded that

system engineering unnecessarily imposed the requirement for an accelerated

shut down on the operations staff. The system engineers failed to promptly

and appropriately assess the impact of high vibration on the operability of

the centrifugal charging pump.

The surveillance procedure did not consider

vibration of the speed increaser as part of the acceptance criteria. The

inspectors concluded, however, that system engineering and planning staff

inappropriately failed to consider vibration as part of the required

acceptance criteria, since maintenance with the potential for adversely

affecting the speed increaser had been performed.

4.0

ENGINEERING

A.

Suspected Auxil;ary Feedwater Piping Degradation

On September 6, 1994, the inspector informed the system engineer of watermarks

running down the wall beneath the no. 22 auxiliary feedwater. (AFW) piping

penetration in the main steam isolation valve (MSIV) room on Salem Unit 2.

The engineer considered the leakage normal and attributed it to ground water

leakage past the Williamson penetration seal.

On September 9, the inspector

observed standing water in the MSIV room beneath the AFW penetration.

The

inspector obtained rust from between the AFW piping and the penetration walls.

Based on the presence of rust, the system engineer examined the piping and

penetration more closely and determined that ground water leakage might be

eroding the AFW pipe coating. The system engineer initiated ultrasonic

testing (UT) to evaluate AFW piping wall thickness.

On September 19, the inspector requested an operability evaluation. The

licensee appropriately evaluated AFW operability.

On September 21, the Plant

Manager ordered a detailed evaluation of the AFW piping.

On September 22, UT

examination found the wall thickness greater than the minimum required wall

thickness and within manufacturing tolerances. Chemical analysis of water and

dirt samples from the pipe penetration were inconclusive. During excavation

of the outside area around the penetration the licensee observed evidence of

water infiltration into the penetration, and determined that the seals were

inadequately installed. Engineering did not find any indication of pressure

boundary leakage or degradation.

The licensee replaced the penetration seals

and declared the AFW piping operable.

The inspector concluded that the licensee demonstrated weak safety focus in

their initial lack of timely response to a potential safety issue.

Subsequently, the licensee conducted a very thorough AFW piping evaluation.

The inspector noted that the penetration still leaked after completion of the

seal repairs, but determined that no immediate AFW piping concern existed .

11

B.

Control Air Abnormalities

The inspectors documented control air system problems in NRC Inspection Report

50-272 and 311/94-19.

The inspectors noted the three additional examples of

control air degraded performance during this inspection period.

On October 5, 1994, during the performance of a control air surveillance test,

the no. 2 emergency air compressor tripped immediately on low oil pressure due

to an initial oil pres.sure fluctuation. Subsequent maintenance testing

demonstrated acceptable oil pressure, within the required time, to prevent

tripping of the compressor on startup.

On October 28, while preparing to

remove the no. 2 station air compressor (SAC) from service, for corrective

maintenance, the no. 3 SAC failed to properly load. Maintenance completed

prolonged maintenance (16 days) on no. 3 SAC on October 19.

The station air

and control air header pressures dropped, the no. 1 emergency control air

compressor auto started, and the operators began to restore no. 2 SAC.

Within

25 minutes, operators restored the no. 2 SAC and returned no. 3 SAC to standby

status.

On October 31, maintenance took the no. 11 control air dryer out of

service for preventive maintenance and "B" control air header pressure dropped

to 86 psig.

Normal control air pressure is 90-I20 psig.

The inspectors determined that plant staff took immediate corrective actions

in response to control air problems as required by procedure and Technical

Specification requirements.

However, marginal control air system performance

continues to provide challenges to plant operation.

C.

Diesel Generator Fuel Oil Supply Header Bolt Problems

During the 2C emergency diesel generator (EDG) maintenance outage, maintenance

personnel discovered that the diesel vendor had not tapped some fuel supply

header bolt holes sufficiently to permit full bolt insertion.

(Each cylinder

has two such bolts.) The licensee experienced previous problems with the fuel

header bolts.

On three occasions (April 30, 1993; November I3, 1993; and

September 25, I994) workers found bolts broken in two pieces following diesel

runs. A PSE&G Research and Testing laboratory evaluation, dated March IO,

I994, determined that fatigue caused the first two failures.

As a result of

the discovery, engineering suspected that inadequately tapped bolt holes

caused the fatigue failures. Maintenance tapped the holes deeper in the 28

and 2C EDGs and planned to take the same action for 2A EOG during its outage

window.

The maintenance staff verified the full insertion of all fuel supply

header bolts in the Salem Unit I EDGs by visual and physical inspection.

The

licensee is evaluating the condition for reportability under IO CFR Part 2I.

On October 30, I994, while running the IA EOG to demonstrate operability after

corrective maintenance, an equipment operator emergency tripped the IA EDG due

to fuel oil spraying out from under the fuel injection pump covers. Operators

were running the IA EOG to satisfy Technical Specification requirements due to

corrective maintenance on the IC EDG.

Maintenance found two fuel header bolts

backed completely out on one cylinder. Although the fuel oil supply line was

still aligned for that cylinder fuel injection, fuel oil leaked out, and

overflowed eight adjacent fuel injector pump cover plates. The licensee noted

no affect on engine performance, however, the fuel spraying on the running

12

engine presented a threat of fire.

The licensee concluded that the bolts were

not adequately tightened previously and vibrated loose.

In response, the

licensee verified that all the fuel supply header bolts had been torqued to

14-16 ft-lbs.

The inspectors concluded that the licensee responded appropriately to the

inadequately tapped fuel header bolt holes and inadequately torqued fuel oil

header bolts.

D.

Susta;ned Operation of Salem un;t 2 above 3411 Megawatts (thermal)

As documented in NRC Inspection Report 50-272&311/94-01, the licensee found

that they had operated Salem Unit 2 at thermal power levels up to 101.4% (3459

MWth) power for sustained periods during operating cycle 7, and at sustained

thermal power levels up to 102.58% (3499 MWth) + or - 7% during operating

cycle 8.

The licensee attributed the immediate cause of the overpower

operation to inaccurate feedwater flow indication.

The licensee concluded

that they did not immediately recognize the overpower condition because they

attributed the increased electric output to plant improvements and calculation

uncertainties.

The licensee, with assistance from Westinghouse, performed extensive

evaluation of the effects of sustained operation at 104.5% power (3565 MWth).

The licensee concluded that sustained operation at 104.5% power did not

compromise plant safety since it did not affect some analyzed accidents, and

detailed analyses for the remaining analyzed accidents concluded that

sufficient margin existed to offset the adverse consequences resulting from

overpower operation.

The licensee also concluded that they did not recognize

the possible connection between increased generator output and decreased

calculated reactor coolant system (RCS) flow rate. The licensee identified a

number of corrective actions, including inspection and root cause analysis of

the inaccurate feedwater flow indication, replacement of the feedwater flow

nozzles, establishing a trending program for statepoint and calorimetric data,

and improved use of operating experience feedback.

The inspectors concluded that the PSE&G assessment of the safety significance

of operating at greater than 100% power reasonably concluded that the safe

operation of the plant had not been compromised.

However, since the licensee

did not assess the operation at 102.58% power until after the fact, the

licensee operated the plant in an unanalyzed condition for sustained periods

during operating cycle 8.

In addition, the licensee did not promptly identify

that the increased electric output resulted from increased reactor power, a

potential safety problem.

The licensee had sufficient empirical data

available (RCS flow and core temperature change) to allow them to challenge

the accuracy of the feedwater flow indication during operating cycle 7 and 8.

The analysis, however, failed to question the accuracy of feedwater flow

indication.

The lack of questioning was due, in part, to the expectation that

the increased electric generation resulted from recent improvements in balance

of plant equipment.

In summary, the licensee failure to consider the worst

case implications of the increased electric generation indicated weaknesses in

13

problem identification, resolution, and safety perspective.

Failure to

promptly identify and correct a significant condition adverse to quality is a

violation of 10 CFR 50, Appendix B, Criterion XVI.

(VIO 50-272&311/94-24-04)

(CLOSED: URI 50-272&311/94-01-02)

5.0

PLANT SUPPORT

5.1

Radiological Controls and Chemistry

5.1.1 Inspections Findings

A.

Radiation Protection Outage Activities

The inspector observed consistently strong Radiation Protection performance

throughout the inspection period. Radiation protection staff conducted good

radiation worker briefings, properly posted radiation and contaminated areas,

and generally assured excellence in radiological worker practices. Radiation

protection technicians actively monitored the radiologically controlled area,

were very knowledgeable of plant conditions and- radiological practices, and

strictly controlled access point entries and exits. The inspector noted good

radiation protection management supervision involvement at the control points

and in the plant, especially in containment .

B.

Radiation Monitoring System Reliability

During the past year, inspectors have noted a large number of corrective

maintenance activities for the plant radiation monitors.

Based on a review of

documented work activities, the inspectors noted the following numbers of

corrective maintenance activities for the Salem radiation monitors:

RMS Corrective Maintenance

Salem 1

Salem 2

1/1/91 - 12/31/91

383

379

1/1/92 - 12/31/92

280

365

10/1/93 - 9/30/94

216

305

The inspectors concluded that the frequent degraded condition of the radiation

monitors posed unnecessary distraction to operations and maintenance staff,

even though the frequency of repair trended down over the past three years.

The inspectors also noted that plant management recently increased efforts to

improve radiation monitoring equipment reliability through improved

maintenance and increased emphasis on developing a long term solution.

5.2

Emergency Preparedness

5.2.1 Open Item Followup

14

(Closed) Unresolved Item (50-272 and 311/92-17-01)

Following an unplanned loss of shutdown cooling at Hope Creek in October 1992,

the inspectors reviewed the event and PSE&G's evaluation of reportability

under 10 CFR 50.72 requirements.

The inspector also reviewed Salem's relevant

reporting requirements.

The inspector reviewed PSE&G's current procedures and expectations concerning

reportability under 10 CFR 50.72 for loss of shutdown cooling and decay heat

removal.

The criteria for making a non-emergency four hour report were, a}

the event was an engineered safety feature (ESF} actuation and b} the event

was one which alone could have prevented the fulfillment of a safety function

needed to remove residual heat.

The inspector determined that these criteria

met the applicable reporting requirements of 10 CFR 50.72, paragraph (b}(2}.

The inspector concluded that the licensee was in compliance with NRC

req~irements and adequate means existed to properly document loss of shutdown

cooling events. This item is closed.

5.3

Security

5.3.1 Inspection Findings

On October 24, 1994, a guard providing control of a temporary access to the

no. 2C emergency diesel generator room, failed to properly verify that the

inspectors had been authorized access to the EOG.

Post orders, issued to

provide instructions for access control, instructed the guard to verify that

each person needing access to the EOG room, had been granted authorization

prior to permitting entry.

In response to the inadequate performance, a

security supervisor took immediate action to insure compliance with the

requirement for verification of authorization to the vital area.

In addition,

the security contractor took appropriate disciplinary action and conducted

remedial training for the guard.

In addition, the contractor reviewed the

incident with the guard force.

Failure to insure proper authorization to a

vital area prior to granting access is a violation.

(VIO 50-272&311/94-24-05)

5.4

Safety Assessment and Quality Verification

5.4.1 Inspection Findings

A.

PSE&G Management Changes

On September 8, PSE&G management announced that they had acquired the services

of John Summers to fill the position of Manager, Salem Mechanical Maintenance

on a temporary basis (1 year).

In addition, on September 7, PSE&G announced

that the nuclear division had been re-established as a separate PSE&G business

unit headed by President and Chief Nuclear Officer, Leon Eliason .

15

B.

Management Assessment of Salem Performance

The inspectors interviewed the Vice President of Operations and Salem general

manager, the Salem department managers, and the Vice President and managers of

the corporate engineering organization. The inspectors conducted the

interviews to determine and assess the process for effecting change in the

performance of *the Salem staff and supporting organizations. The inspectors

requested that the managers relate the areas identified as most in need of

change, the basis for determining the areas needing change, and the action

planned to generate the required change.

The inspectors learned that corporate engineering managers had performed

extensive research specific to their organization to identify areas for

improvement.

The results identified weaknesses in leadership ability, the

need for process improvements, and the need for organizational changes.

Corporate engineering developed a comprehensive plan to address the identified

areas for improvement.

Some Salem managers also performed independent analysis of their organizations

to identify the areas in need of change.

The operations department, for

example, identified processes and personnel performance issues among the areas

for improvement.

The operations staff demonstrated significant ownership and

pride in the documented plan for improving operations performance.

Other Salem managers had also identified areas for improvement.

The sources

of the identification process included reports issued by the NRC and other

outside organizations, and Comprehensive Performance Assessment Team results.

The inspectors observed_ that the managers identified many fruitful areas for

improvement.

The inspectors also noted that some of the managers did not have

direct ownership for the source of the areas identified for improvement, and

had not established a plan for achieving the identified improvements.

Senior

management stated that they had initiated efforts to establish a more uniform

approach to improving performance.

6.0

LICENSEE EVENT REPORTS (LER), PERIODIC AND SPECIAL REPORTS, AND OPEN

ITEM FOLLOWUP

6.1

LERs and Reports

The Salem Monthly Operating Reports for August and September were reviewed for

accuracy and content, and were determined to be acceptable.

The inspectors

also reviewed the following LERs to determine whether the licensee took the

corrective actions stated in the report, and to determine if licensee

responses to the events were adequate, met regulatory requirements conditions,

and commitments:

Salem.LERs

Unit 1

Number

LER 94-14

LER 94-08

Unit 2

LER 94-10

LER 94-11

16

Event Date

August 25, 1994

August 28, 1994

September 22, 1994

September 29, 1994

Description

Licensee entered Technical

Specification 3.0.3 to permit

maintenance on the Analog Rod

Position Indication System.

Late performance of quarterly

channel functional test.

Controlled reactor shutdown due to

no. 21 centrifugal charging pump

being inoperable greater than 72

hours.

Manually initiated reactor trip

following unplanned closure of two

main steam isolation valves .

For the LERs listed above, the inspectors determined that there were no

violations or deviations, and considered the LERs closed.

6.2

Open Items

The inspector reviewed the following previous inspection items during this

inspection. These items are tabulated below for cross reference purposes.

Number

272& 311/92-17-01 __ ,

272&311/94-01-02

Report Section

5.2.2.A

4.D

7.0

EXIT INTERVIEWS/MEETINGS

7.1

Resident Exit Meeting

Status

Closed

Administratively closed and

re-opened as a violation

(272&311/94-24-04)

The inspectors met with Mr. J. Hagan and other PSE&G personnel periodically

and at the end of the inspection report period to summarize the scope and

findings of their inspection activities.

17

Based on NRC Region I review and discussions with PSE&G, it was determined

that this report does not contain information subject to 10 CFR 2

restrictions.

7.2

Salem Specialist Entrance and Exit Meetings

Inspection

Reporting

Date(s)

Subject

Report No.

Inspector

9/26-10/7/94

Engineering

50-272 and 311/94-27

Calvert

Inspection

10/17-28/94

MOV Inspection

50-272 and 311/94-26

Prividy

10/17-21/94

Effluents

Inspection

50-272 and 311/94-28

Peluso

10/24-26/94

Emergency

50-272 and 311/94-23

Laughlin

Preparedness

10/24 - 11/3/94

Radcon Inspection 50-272 and 311/94-30

Noggle

7.3

Management Meetings

On October 21, 1994, Charles W. Hehl, Director, Division of Radiation Safety

and Safeguards, NRC, Region I, visited Salem Units I and 2 in preparation for

the Systematic Assessment of Licensee Performance (SALP).