:on 911127,RMS 1R12A Containment Noble Gas Radiation Monitor Channel Alarmed,Resulting in Containment Purge Isolation Signal.Caused by Failure of Detector Connector.Connector Replaced & Housing Cleaned| ML18100A363 |
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| Site: |
Salem  |
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| Issue date: |
05/04/1993 |
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| From: |
Pollack M Public Service Enterprise Group |
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| Shared Package |
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| ML18100A362 |
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| References |
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| LER-91-035, LER-91-35, NUDOCS 9305120061 |
| Download: ML18100A363 (5) |
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NRC FORM 366 (6-891 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LERI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P*530I, U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-01041. OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1 I I
DOCKET NUMBER (21 PAGE 131 Salem Generating Station - Unit i o I 5 I o I o l o I 2 I 7 12, OF 015 TITLE (41 F.no-ineered Safetv Feature signal initiated from the Radiation Monitoring System.
EVENT DATE (51 LER NUMBER (61 REPORT DATE (71 OTHER FACILITIES INVOLVED (81 MONTH DAY YEAR YEAR [:} SEQUENTIAL E>
REVISION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI NUMBER NUMBER o1s1010101 I I i Ii 21 7 91 i -
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I OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE Rl<;lUIREMENTS OF 10 CFR §: (Chock one or more of th* following) (111 MODE (Bl 1
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20.406(1111)(vl 60.7311112)(iii) 60.73(111211*1 LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE M. J. Pollack -
LER Coordinator 61 01 9 3 13 I 9 1-12 I 0 12 I 2 COMPLETE ONE.LINE FOR EACH COMPONENT FAILURE DESCRIBED JN THIS REPORT 1131 MANUFAC*
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SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR k-i NO EXPECTED SUBMISSION n YES (If y6S, comp/et* EXPECTED SUBMISSION DATE)
DATE 1151 I
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ABSTRACT (Limit to 1400 spaces. i.~.. approximately fifteen single-space typewrirten lines) 116)
This LER is a supplement to LER 272/91-035-00.
The Apparent Cause of occurrence section has been revised to address the results of subsequent investigation.
On November 27, 1991, at 0042 hours4.861111e-4 days <br />0.0117 hours <br />6.944444e-5 weeks <br />1.5981e-5 months <br />, the Radiation Monitoring System (RMS) 1R12A Containment Noble Gas Radiation Monitor channel alarmed resulting in a Containment Purge/Pressure-Vacuum Relief (CP/P-VR) system isolation signal.
Investigation of the event was initiated which included taking a portable Containment air sample.
The sample did not indicate any increased activity.
The 1R12A RMS channel was declared inoperable and Technical Specification 3.3.3.l Table 3.3-6 Action 20 was entered on November 27, 1991, at 0334 hours0.00387 days <br />0.0928 hours <br />5.522487e-4 weeks <br />1.27087e-4 months <br />.
The root cause of the ESF signal actuation is equipment failure.
Investigation identified that the detector connector had failed.
The signal ground wire, in the connector, had broken.
Also, the cable shield wire was found unconnected and pushed back into the connector.
The connector was subsequently replaced.
The channel was then tested successfully and returned to service.
A program to replace older RMS channel connectors has been initiated.
93051200~~ i~ggg~72 PDR ADO NRC Form 366 (6-891 s
PDR
- - I
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER.
5000272
PLANT AND SYSTEM IDENTIFICATION
Westinghouse
- - Pressurized Water Reactor LER NUMBER 91-035-01 PAGE 2 of 5 Energy Industry Identification system (EIIS) codes are identified in the text as {xx}
IDENTIFICATION OF OCCURRENCE:
Engineered Safety Feature signal initiated from the Rad'iation Monitoring System
11/27/91 Report Date:. 5/4/93 This report is a supplement to LER 272/91-035-00 which was initiated by Incident Report No.
91~864.
The Apparent Cause of Occurrence section has been revised -to address the results of subsequent investigation (committed to in the original LER). *
- CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 100% - Unit Load 1.160 MWe DESCRIPTION OF OCCURRENCE:
On November 27, 1991, at 0042 hours4.861111e-4 days <br />0.0117 hours <br />6.944444e-5 weeks <br />1.5981e-5 months <br />, the Radiation Monitoring System
{RMS) {IL} 1Rl2A Containment Noble Gas Radiation Monitor channel alarmed resulting in a Containment Purge/Pressure-Vacuum Relief (CP/P-VR) System {BF} isolation signal.
Investigation of the event was initiated which included taking a Containment air sample.
The sample did not indicate any iricreased activity.
The 1R12A RMS channel was declared inoperable and Technical Specification 3.3.3.1 Table 3.3-6 Action 20 was entered on November 27, 1991, at 0334 hours0.00387 days <br />0.0928 hours <br />5.522487e-4 weeks <br />1.27087e-4 months <br />.
The CP/P-VR System isolation signal is an Engineered Safety Feature
{ESF) {JC}.
Therefore, the Nuclear Regulatory Commission was notified of the automatic actuation signal in accordance with Cod~ of Federal Regulations 10CFR 50.72(b) (2) (ii) on November 27, 1991, at 0119 hours0.00138 days <br />0.0331 hours <br />1.967593e-4 weeks <br />4.52795e-5 months <br />.
Technical Specification Table 3.3-6 Action 2o states:
"With the number of channels OPERABLE less than required by the Minimum Channels.OPERABLE requirement, comply with the ACTION requirements of Specification 3.4.6.1 11
"The following Reactor Coolant System leakage detection systems I
~ICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DESCRIPTION OF OCCURRENCE:
shall be OPERABLE:
DOCKET NUMBER 5000272 (cont'd)
LER NUMBER 91-035-01 a. -The containment atmosphere particulate radioactivity monitoring system, b.
The containment sump level monitoring system, and PAGE 3 of 5 c.
Either the containment fan cooler condensate flow rate or the containment atmosphere gaseous radioactivity monitoring system."
Technical Specification 3.4.6.1 Action Statement states:
"With only two of the above required leakage detection systems OPERABLE, operation may continue for up to 30 days provided grab samples of the containment atmosphere are obtained and analyzed at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when the required gaseous and/or particulate radioactivity monitoring system is inoperable; otherwise, be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
APPARENT CAUSE OF OCCURRENCE:
The root cause of the ESF signal actuation is equipment 'failure.
Investigation identified that the de.tector connector had_ failed.
The signal ground wire, in the connector, had broken.
Also, the cable shield wire was found unconnected and pushed back into the connector.
The connector was subsequently replaced.
The channel was then tested successfully and returned to service.
Detector connector failures have been experienced with other RMS channels in both Salem Units (e.g., LER 311/90-021-00, 2Rl2A ESF signal actuation).
A program to replace older RMS channel connectors has been initiated.
ANALYSIS OF OCCURRENCE:
This event did not affect the health-or safety of the public.
l However, due to the automatic actuation signal of an ~SF system, it
Isolation of the *CP/P-VR System is an ESF.
It mitigates the release of radioactive material to the environment after a design basis accident.
Air samples are pulled from the Containment atmosphere through filter paper which continuously moves past the lRllA (Containment Particulate Radiation Monitor) detector.
The air sample then passes
- ::=1
LICENSEE EVENT REPORT_ (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 ANALYSIS OF OCCURRENCE:
(cont'd)
LER NUMBER 91-035-()1 PAGE 4 of 5 through a charcoal cartridge (monitored by the 1R12B detector) and is then mixed into a fixed shielded volume where it is viewed by the 1R12A (Containment Noble Gas Radiation Monitor) detector.
The air sample is then returned to the Containment.
The 1R12A, Containment Noble Gas Monitor, (a geiger-mueller detector) monitors the radioactive noble gas activity in the Containment atmosphere.
It is used to identify RCS leakage in conjunction with the containment sump level monitoring system, and either the.
containment fan cooler condensate flow rate monitoring system, or the containment radioactive particulate (lRllA) radioactivity monitoring system.
~
Both the lRllA and 1R12A RMS channels provide an alarm signal which will cause automatic isolation of the CP/P-VR System.
At the time of the 1R12A ESF signal actuation, Containment Purge and Pressure-Vacuum Relief activities were not in progress.
The.
Containment Ventilation valves were closed.
They did not change position as a result of the isolation signal.
During the 1R12A event, RCS leakage within the containment did not increase nor were there any significant indications of increasing Containment activity based on subsequent air samples.
The* initial investigation (as discussed in the original issue of this LER) identified that the 1R12A monitor may have responded to actual radioactivity, the source of which was not presently known.
Prior to the event, on November 26, 1991, the 1R12A count rate was observed to be trending up.
During this increase, the 1R11A Containment Particulate Monitor RMS channel spiked high resulting in a CP/P-vR System isolation signal (see LER 272/91-034-00).
Investigation of the lRllA event identified 1800 cpm above background on the lRllA _
filter paper.
The lRllA and 1Rl2A monitor the same sample of Containment air.
The lRllA RMS channel activity was determined to be Pb-214 and Bi-214 (naturally occurring Radon daughter products).
This activity was thought to_ also be the reason for the observed increase in 1Rl2A background counts.
The 1R12A detector housing and detector were subsequently cleaned, on November 26, 1991, resulting in the lowering of the 1R12A background count rate to a nominally expected value.
The investigation of the November 27, 1991 1R12A event included*
cleaning the detector housing and detector, again resulting in the lowering of the 1R12A background count rate to a nominally expected value.
Also, a channel calibration check was successfully performed..
A search for leaks, within the Containment, was conducted.
An extremely small leak was identified on the Pressurizer Relief Tank (PRT) rupture disc.
This leak was determined to be inconsequential I
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 ANALYSIS OF OCCURRENCE:
DOCKET NUMBER 5000272 (cont'd}
LER NUMBER 91-035-01 PAGE 5 of 5 to an increase in Containment airborne activity.
An air sample by the PRT did not show an increase in airborne activity.
The 1R12A RMS channel was subsequently returned to service on November 29, 1991, at.1125 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.280625e-4 months <br />, 'at which time Technical Specific::ation Table 3.3-6 Action 20 was exited.
On December 5,* 1991, at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />, 1R12A RMS channel was taken out of service due to observed readings approaching the channel's warning setpoint.
The appL:icable Action Statement was entered.
Containment air samples, as before, did not show any increase in background activity.
Analys,is of detector and detector housing smears showed Pb-214, Bi-214 and Rb-88.
The channel was returned.to service and the Action Statement exited on December 6,. 1991, at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />.
Subsequent analysis has shown that Pb-214/BI-214 acitivty was not sufficient to drive the 1Rl2A RMS channel into warning or alarm.
CORRECTIVE ACTION
The 1Rl2A failed connector was replaced.
The channel was then tested successfully and returned to service.
A program to replace older RMS channel connectors has been initiated.
The 1Rl2A channel detector and detector housing were cleaned and a channel calibration check was performed satisfactorily.
The channel was returned to service on November 29, 1991, at 1125 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.280625e-4 months <br />, at which time Technical Specification Table ~.3-6 Action 20 was exited.
The PRT rupture disc leak was repaired.
MJP:pc SORC Mtg.93-040 t
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| | | Reporting criterion |
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| 05000311/LER-1991-001, :on 910104,discovered That Hourly Roving Fire Watch Patrol for Several Areas Not Completed.Caused by Personnel Error.Responsible Individual Terminated & Event Discussed W/Appropriate Personnel |
- on 910104,discovered That Hourly Roving Fire Watch Patrol for Several Areas Not Completed.Caused by Personnel Error.Responsible Individual Terminated & Event Discussed W/Appropriate Personnel
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1991-001-02, :on 910111,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated.Caused by Equipment Failure.Channel Detector Connectors Checked & Returned to Svc |
- on 910111,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated.Caused by Equipment Failure.Channel Detector Connectors Checked & Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1991-002, :on 910116,radiation Monitoring Sys Channel Failed.Caused by Equipment Design Concerns.Sys Design Mods Under Investigation.Channel Inspected & Repaired |
- on 910116,radiation Monitoring Sys Channel Failed.Caused by Equipment Design Concerns.Sys Design Mods Under Investigation.Channel Inspected & Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-002-02, :on 910117,RHR Pump 11 Room Cooler Leakage Noted on Metal Weld of Inlet Control Valve.On 910124,leakage Noted on SI Pump Room Cooler & Auxiliary Feedwater Pump Cooler.Caused by Equipment Failure |
- on 910117,RHR Pump 11 Room Cooler Leakage Noted on Metal Weld of Inlet Control Valve.On 910124,leakage Noted on SI Pump Room Cooler & Auxiliary Feedwater Pump Cooler.Caused by Equipment Failure
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1991-003-01, :on 910110,leakage Noted in Svc Water Sys Charging Pump 21 Cooler Piping.On 910130,leakage Noted in Svc Water Sys Charging Pump Cooler 22 Piping.Caused by Equipment Failure.Piping Repaired |
- on 910110,leakage Noted in Svc Water Sys Charging Pump 21 Cooler Piping.On 910130,leakage Noted in Svc Water Sys Charging Pump Cooler 22 Piping.Caused by Equipment Failure.Piping Repaired
| | | 05000272/LER-1991-003-01, :on 910209,steam Generator 14 Steamline Flow Channel I Transmitter Sensing Line Isolated During Investigation of Erroneous Reading.Caused by Personnel Error.Disciplinary Action Taken |
- on 910209,steam Generator 14 Steamline Flow Channel I Transmitter Sensing Line Isolated During Investigation of Erroneous Reading.Caused by Personnel Error.Disciplinary Action Taken
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000311/LER-1991-003, :on 910225,ASME Code 3 Piping Leakage Occurred. Caused by Equipment Failure.Repair of Affected Components Completed in Accordance W/Asme Code & Addl Insp Being Reviewed & Modified |
- on 910225,ASME Code 3 Piping Leakage Occurred. Caused by Equipment Failure.Repair of Affected Components Completed in Accordance W/Asme Code & Addl Insp Being Reviewed & Modified
| 10 CFR 50.73(o)(2) | | 05000272/LER-1991-003-02, :on 910209,steam Generator 14 Steamline Flow Channel I Transmitter Sensing Line Isolated During Investigation of Erroneous Readings.Caused by Personnel Error.Event Reviewed W/Personnel |
- on 910209,steam Generator 14 Steamline Flow Channel I Transmitter Sensing Line Isolated During Investigation of Erroneous Readings.Caused by Personnel Error.Event Reviewed W/Personnel
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1991-004-01, :on 910206,turbine Runback from 100% to 90% Power Occurred Due to Overtemp/Delta Temp Signal.Caused by Equipment Failure.Recorders Attached to RPS Comparator Circuits & Failed Capacitors Replaced |
- on 910206,turbine Runback from 100% to 90% Power Occurred Due to Overtemp/Delta Temp Signal.Caused by Equipment Failure.Recorders Attached to RPS Comparator Circuits & Failed Capacitors Replaced
| | | 05000311/LER-1991-004-02, :on 910218,radiation Monitoring Sys intermediate-range Vent Monitor 2R45B Spiked High,Causing Channel 2R41 to Deenergize.Caused by Damaged Cable Shield Connection.Detector Cable Replaced |
- on 910218,radiation Monitoring Sys intermediate-range Vent Monitor 2R45B Spiked High,Causing Channel 2R41 to Deenergize.Caused by Damaged Cable Shield Connection.Detector Cable Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-005, :on 910209,containment Fan Coil Units Did Not Meet Design Accident Requirements Identified by Updated Fsar.Caused by Inadequate Administrative Control.Cleaning of Inlet Side of Water Box Performed |
- on 910209,containment Fan Coil Units Did Not Meet Design Accident Requirements Identified by Updated Fsar.Caused by Inadequate Administrative Control.Cleaning of Inlet Side of Water Box Performed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000311/LER-1991-005-02, :on 910226,sustained Undervoltage Relay Min Drop Out Trip Setpoints Set Below Tech Spec Value.Caused by Personnel Error & Procedural Inadequacy.New Relay Procedures Implemented |
- on 910226,sustained Undervoltage Relay Min Drop Out Trip Setpoints Set Below Tech Spec Value.Caused by Personnel Error & Procedural Inadequacy.New Relay Procedures Implemented
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1991-006, :on 910321,control Room Radiation Monitoring Sys Monitor Spiked High,Resulting in ESF Actuation.On 910305 Channel Low Failure Signal Generated.Caused by Broken Wire in Detector Cable.Wires Rebuilt |
- on 910321,control Room Radiation Monitoring Sys Monitor Spiked High,Resulting in ESF Actuation.On 910305 Channel Low Failure Signal Generated.Caused by Broken Wire in Detector Cable.Wires Rebuilt
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1991-006-01, :on 910302,ESF Actuation,Automatic Switching of Control Room Ventilation to Emergency Mode of Operation Occurred.Caused by Equipment Failure.Channel Detector Cable Connection Rebuilt |
- on 910302,ESF Actuation,Automatic Switching of Control Room Ventilation to Emergency Mode of Operation Occurred.Caused by Equipment Failure.Channel Detector Cable Connection Rebuilt
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-006, :on 910216,20 & 27,containment Purge/Pressure Vacuum Relief Sys Isolation Occurred & Actuation Signals Initiated by Radiation Monitor Channel.Caused by Inadequate Administrative Controls.Channel Reset |
- on 910216,20 & 27,containment Purge/Pressure Vacuum Relief Sys Isolation Occurred & Actuation Signals Initiated by Radiation Monitor Channel.Caused by Inadequate Administrative Controls.Channel Reset
| | | 05000311/LER-1991-007-02, :on 910522,channel Failure Occurred.Caused by Equipment Design Concerns.Failed Channel Control Module Replaced & Channel Functional Test Successfully Completed |
- on 910522,channel Failure Occurred.Caused by Equipment Design Concerns.Failed Channel Control Module Replaced & Channel Functional Test Successfully Completed
| 10 CFR 50.73(o)(2) 10 CFR 50.73(o)(2)(x) 10 CFR 50.73(o)(2)(viii)(A) 10 CFR 50.73(o)(2)(v) 10 CFR 50.73(o)(2)(vii) 10 CFR 50.73(o)(2)(i) | | 05000272/LER-1991-007-01, :on 910217,motor-driven Auxiliary Feedwater Pumps Started After 125-volt Dc Distribution Cabinet Power Supply Transferred to Emergency Power.Caused by Inadequate Administrative Controls.Schematics Reviewed |
- on 910217,motor-driven Auxiliary Feedwater Pumps Started After 125-volt Dc Distribution Cabinet Power Supply Transferred to Emergency Power.Caused by Inadequate Administrative Controls.Schematics Reviewed
| 10 CFR 50.73(o)(2)(vii) 10 CFR 50.73(o)(2)(iii) | | 05000272/LER-1991-007, :on 910217,motor Driven Auxiliary Feedwater Automatically Started After Distribution Cabinet 1CCDC Power Supply Transferred to Emergency Power Supply.Caused by Inadequate Administrative Controls |
- on 910217,motor Driven Auxiliary Feedwater Automatically Started After Distribution Cabinet 1CCDC Power Supply Transferred to Emergency Power Supply.Caused by Inadequate Administrative Controls
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1991-008-01, :on 910603,sustained Undervoltage Relay Min Dropout Trip Setpoint Voltage for Three 4 Kv Vital Bus 2A Undervoltage Relays Found Below TS Min Allowable Value. Caused by Setpoint Drift.Procedure Revised |
- on 910603,sustained Undervoltage Relay Min Dropout Trip Setpoint Voltage for Three 4 Kv Vital Bus 2A Undervoltage Relays Found Below TS Min Allowable Value. Caused by Setpoint Drift.Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1991-008-02, :on 910603,sustained Undervoltage Relay Min drop-out Setpoint Voltage for 4-kV Vital Bus Found Below TS Allowable Value of 91%.Cause Not Determined.Design Change to Replace Relays Initiated |
- on 910603,sustained Undervoltage Relay Min drop-out Setpoint Voltage for 4-kV Vital Bus Found Below TS Allowable Value of 91%.Cause Not Determined.Design Change to Replace Relays Initiated
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000272/LER-1991-008, :on 910217,reactor Protection Signal from Nuclear Instrumentation Sys Received.Caused by Personnel Error Due to Inattention to Detail.Individual Counseled & Event Reviewed W/Personnel |
- on 910217,reactor Protection Signal from Nuclear Instrumentation Sys Received.Caused by Personnel Error Due to Inattention to Detail.Individual Counseled & Event Reviewed W/Personnel
| | | 05000311/LER-1991-009-02, :on 910630,ESF Actuation Occurred as 21 Motor Driven Auxiliary Feedwater Pump Started.Caused by Equipment Failure.Failed Ssps Output Card Replaced & Results of Study Assessed to Determine Preventive Measures |
- on 910630,ESF Actuation Occurred as 21 Motor Driven Auxiliary Feedwater Pump Started.Caused by Equipment Failure.Failed Ssps Output Card Replaced & Results of Study Assessed to Determine Preventive Measures
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-009, :on 901220,discovered Unsealed Portion of Heba Barrier Between Inboard Mechanical Penetration Area & Chiller Room.On 901101 Concern Raised Re Adequacy of Evaluations.Missing Portion Installed |
- on 901220,discovered Unsealed Portion of Heba Barrier Between Inboard Mechanical Penetration Area & Chiller Room.On 901101 Concern Raised Re Adequacy of Evaluations.Missing Portion Installed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1991-010-02, :on 910723,ESF Actuation Signals Initiated. Caused by High Channel Spike on Channel 2R1B & Noble Gas Monitor 2R45C Due to Faulty Equipment Design.Detector Assembly Replaced & Design Mods Underway |
- on 910723,ESF Actuation Signals Initiated. Caused by High Channel Spike on Channel 2R1B & Noble Gas Monitor 2R45C Due to Faulty Equipment Design.Detector Assembly Replaced & Design Mods Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-010, :on 910220 & 0304,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Actuated & Channel 1R12A Alarmed.Caused by Procedure Inadequacy.Alarm Point Procedure Revised |
- on 910220 & 0304,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Actuated & Channel 1R12A Alarmed.Caused by Procedure Inadequacy.Alarm Point Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-011, :on 910220,high Rad Area Found Unlocked & Unguarded.Caused by Personnel Error.Event Reviewed by Radiation Protection Dept & Corrective Action Taken Against Technician Responsible |
- on 910220,high Rad Area Found Unlocked & Unguarded.Caused by Personnel Error.Event Reviewed by Radiation Protection Dept & Corrective Action Taken Against Technician Responsible
| | | 05000272/LER-1991-011-02, :on 910730,discovered That Nonradioactive Liquid Waste Discharge Radiation Monitoring Sys Channel Setpoint Not Correct.Caused by Inadequate Design Review. Design Change Process Procedure Revised |
- on 910730,discovered That Nonradioactive Liquid Waste Discharge Radiation Monitoring Sys Channel Setpoint Not Correct.Caused by Inadequate Design Review. Design Change Process Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(o)(2)(vii) | | 05000311/LER-1991-012-02, :on on 910826,4 Kv Vital Bus 2A Tripped While Starting & Loading Diesel Generator 2A.Caused by Technician Connecting Jumper to Wrong relay.Color-coded Banana Jackets Installed on Relay Terminal Lugs |
- on on 910826,4 Kv Vital Bus 2A Tripped While Starting & Loading Diesel Generator 2A.Caused by Technician Connecting Jumper to Wrong relay.Color-coded Banana Jackets Installed on Relay Terminal Lugs
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(o)(2)(vii) | | 05000272/LER-1991-012, :on 910306,control Ventilation Automatically Switched from Normal to Accident Mode of Operation.Cause Undetermined.Investigation Continuing & Design Mods Include Proposal for Channel Equivalent Replacement |
- on 910306,control Ventilation Automatically Switched from Normal to Accident Mode of Operation.Cause Undetermined.Investigation Continuing & Design Mods Include Proposal for Channel Equivalent Replacement
| | | 05000272/LER-1991-013, :on 910318,discovered That Cold Leg Side of Tube in Row 18,column 12 Unplugged.Caused by Personnel Error.Mods to Independent Review Process Implemented & Correct Tube Plugged |
- on 910318,discovered That Cold Leg Side of Tube in Row 18,column 12 Unplugged.Caused by Personnel Error.Mods to Independent Review Process Implemented & Correct Tube Plugged
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1991-013-02, :on 910828,0901 & 10,CP/pressure-vacuum Relief Sys Isolation Signal Received.Caused by Problems W/Equipment Design.Scalar Module Replaced,Channel Backplane Cleaned & Inspected.Channel Drawer & Circuits Vacuumed |
- on 910828,0901 & 10,CP/pressure-vacuum Relief Sys Isolation Signal Received.Caused by Problems W/Equipment Design.Scalar Module Replaced,Channel Backplane Cleaned & Inspected.Channel Drawer & Circuits Vacuumed
| 10 CFR 50.73(a)(2) 10 CFR 50.73(o)(2)(v) | | 05000311/LER-1991-014, :on 911010,containment purge/pressure-vacuum Relief Sys Isolated Due to Failure of 2R12B Channel.Channel Removed from Svc & Being Replaced W/More Reliable Equipment During Current Sixth Refueling Outage |
- on 911010,containment purge/pressure-vacuum Relief Sys Isolated Due to Failure of 2R12B Channel.Channel Removed from Svc & Being Replaced W/More Reliable Equipment During Current Sixth Refueling Outage
| | | 05000272/LER-1991-014, :on 910322,two Channels Made Inoperable in Single Sys.Caused by Equipment Design Concerns.Sample Pump Replaced & Pump Will Be Replaced Every Three Months |
- on 910322,two Channels Made Inoperable in Single Sys.Caused by Equipment Design Concerns.Sample Pump Replaced & Pump Will Be Replaced Every Three Months
| | | 05000311/LER-1991-014-02, :on 911010,monitor 2R12B RMS Channel Failed Low Resulting in ESF Signal for CP/pressure-vacuum Relief Sys Isolation.Caused by Component Failure.Channel Returned to Svc.Mods Planned to Eliminate Spurious RMS |
- on 911010,monitor 2R12B RMS Channel Failed Low Resulting in ESF Signal for CP/pressure-vacuum Relief Sys Isolation.Caused by Component Failure.Channel Returned to Svc.Mods Planned to Eliminate Spurious RMS
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | | 05000311/LER-1991-015-02, :on 911021,nuclear Instrumentation Sys Power Range Channels Indicated Less than 29.8% Rated Thermal Power & Declared Inoperable.Caused by Application of Current Methodology.Potentiometers Adjusted |
- on 911021,nuclear Instrumentation Sys Power Range Channels Indicated Less than 29.8% Rated Thermal Power & Declared Inoperable.Caused by Application of Current Methodology.Potentiometers Adjusted
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1991-015, :on 910329,plant Vent Radioactive Noble Gas Monitor 1R41C Channel Failed Low,Resulting in Containment Purge Isolation Signal.Caused by Failure of Scalar Test Jacket.Test Jacket Replaced |
- on 910329,plant Vent Radioactive Noble Gas Monitor 1R41C Channel Failed Low,Resulting in Containment Purge Isolation Signal.Caused by Failure of Scalar Test Jacket.Test Jacket Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1991-016-02, :on 911025,two Hose Stations Inadvertently Deleted from Procedure Re Detailed Insp of TS-related Hose Stations.Caused by Inappropriate Procedural Rev.Procedure Writer & Reviewer Counseled |
- on 911025,two Hose Stations Inadvertently Deleted from Procedure Re Detailed Insp of TS-related Hose Stations.Caused by Inappropriate Procedural Rev.Procedure Writer & Reviewer Counseled
| | | 05000272/LER-1991-016, :on 910331,Tech Spec Action Statement 3.11.2.5 Entered Due to Oxygen Concentration of 2.3% by Vol in Waste Gas Decay Tank 13.Caused by Failure of 1R41C Channel.Channel Repaired & Procedures Mods to Be Assessed |
- on 910331,Tech Spec Action Statement 3.11.2.5 Entered Due to Oxygen Concentration of 2.3% by Vol in Waste Gas Decay Tank 13.Caused by Failure of 1R41C Channel.Channel Repaired & Procedures Mods to Be Assessed
| | | 05000311/LER-1991-017-03, :on 911109,reactor/turbine Trip Occured on Low Auto Stop Oil Pressure Followed by Turbine/Generator Failure.Caused by Failure of 63-3 Auto Stop Oil Protection Pressure Switch.Matrix Review Performed |
- on 911109,reactor/turbine Trip Occured on Low Auto Stop Oil Pressure Followed by Turbine/Generator Failure.Caused by Failure of 63-3 Auto Stop Oil Protection Pressure Switch.Matrix Review Performed
| | | 05000272/LER-1991-017, :on 910413,sustained Undervoltage Relay Min Drop Voltage Found Below TS Min Allowable Value & Monthly Surveillance Test of Undervoltage Relay Setpoints Not Performed Since 910109.Procedures Enhanced |
- on 910413,sustained Undervoltage Relay Min Drop Voltage Found Below TS Min Allowable Value & Monthly Surveillance Test of Undervoltage Relay Setpoints Not Performed Since 910109.Procedures Enhanced
| 10 CFR 50.73(a)(2) | | 05000311/LER-1991-018-02, :on 911129,radiation Monitor 2R1A Spiked High & on 911205,monitor Spiked Low.Caused by Susceptibility of Monitor to Voltage Transients.Design Mods Implemented to Eliminate Spurious ESF Actuations |
- on 911129,radiation Monitor 2R1A Spiked High & on 911205,monitor Spiked Low.Caused by Susceptibility of Monitor to Voltage Transients.Design Mods Implemented to Eliminate Spurious ESF Actuations
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-018, :on 910410,buffer Relay BC-621 Failed to Energize,Resulting in Failure of Trip Functions to Valve 13BF13.On 910413,uncrimped Connector Found on Electrical Connection.Wiring Crimped |
- on 910410,buffer Relay BC-621 Failed to Energize,Resulting in Failure of Trip Functions to Valve 13BF13.On 910413,uncrimped Connector Found on Electrical Connection.Wiring Crimped
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-019, :on 910428,three Cases of Tech Spec Noncompliance Occurred.Caused by Inadequate Procedures & Personnel Errors.Operations Dept Procedures Revised & Event Reviewed |
- on 910428,three Cases of Tech Spec Noncompliance Occurred.Caused by Inadequate Procedures & Personnel Errors.Operations Dept Procedures Revised & Event Reviewed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000311/LER-1991-019-02, :on 911207,containment Radioactive Noble Gas Monitor Channel Alarmed,Resulting in ESF Actuation Signal. Caused by Inadequate Administrative Controls.Procedure Re SG Work During Refueling Activities Revised |
- on 911207,containment Radioactive Noble Gas Monitor Channel Alarmed,Resulting in ESF Actuation Signal. Caused by Inadequate Administrative Controls.Procedure Re SG Work During Refueling Activities Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1991-020-02, :on 911122,containment purge/pressure-vacuum Relief Sys Isolated Due to 2R12A RMS Channel Response.Caused by Personnel Error.Disciplinary Action Taken W/Personnel Involved in Event |
- on 911122,containment purge/pressure-vacuum Relief Sys Isolated Due to 2R12A RMS Channel Response.Caused by Personnel Error.Disciplinary Action Taken W/Personnel Involved in Event
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-020, :on 910510,control Room General Area Radiation Monitoring Sys Monitor Spiked High.Caused by Equipment Failure.Failed Channel Light Socket Replaced |
- on 910510,control Room General Area Radiation Monitoring Sys Monitor Spiked High.Caused by Equipment Failure.Failed Channel Light Socket Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-021, :on 910522 & 0603,Tech Spec 3/4.8.3.1 Noncompliance Discovered.Caused by Personnel Error.Amend Implementation Event Reviewed W/Prior Tech Spec Administrator |
- on 910522 & 0603,Tech Spec 3/4.8.3.1 Noncompliance Discovered.Caused by Personnel Error.Amend Implementation Event Reviewed W/Prior Tech Spec Administrator
| 10 CFR 50.73(o)(2) 10 CFR 50.73(o)(2)(iv) 10 CFR 50.73(o)(2)(v) | | 05000311/LER-1991-021-01, :on 911219,monthly Surveillance of Wg Analyzer for Reliable Operation Overdue.Caused by Personnel Error. Event Reviewed W/Applicable Personnel & Discplinary Action Taken |
- on 911219,monthly Surveillance of Wg Analyzer for Reliable Operation Overdue.Caused by Personnel Error. Event Reviewed W/Applicable Personnel & Discplinary Action Taken
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1991-022, :on 910606,two ESF Actuations Occurred.Caused by Personnel Error & Inadequate Human Factors Design.Bus Cubicle Design Reviewed to Determine Feasibility for Installation of More Accessible Connections |
- on 910606,two ESF Actuations Occurred.Caused by Personnel Error & Inadequate Human Factors Design.Bus Cubicle Design Reviewed to Determine Feasibility for Installation of More Accessible Connections
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1991-023, :on 910612,two Channels in Single Sys Inoperable.Caused by Equipment Failure.Pump Belts Replaced & & Pump Restored to Svc.Tech Spec Action Statements Exited |
- on 910612,two Channels in Single Sys Inoperable.Caused by Equipment Failure.Pump Belts Replaced & & Pump Restored to Svc.Tech Spec Action Statements Exited
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
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