ML18096A595

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Initial SALP Repts 50-272/90-99,50-311/90-99 for 900801-911228
ML18096A595
Person / Time
Site: Salem  PSEG icon.png
Issue date: 02/26/1992
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18096A593 List:
References
50-272-90-99, 50-311-90-99, NUDOCS 9203310107
Download: ML18096A595 (32)


See also: IR 05000272/1990099

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ENCLOSURE 1

INITIAL SALP REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT NOS.

50-272/90-99

50-311/90-99

PUBLIC SERVICE ELECTRIC AND GAS COMPANY

SALEM GENERATING STATION

UNITS 1AND2

ASSESSMENT PERIOD: AUGUST 1, 1990 - DECEMBER 28, 1991

BOARD MEETING DATE: FEBRUARY 26, 1992

9203310107 920325

.PDR

ADOCK 05000272

G

PDR

,

2

TABLE OF CONTENTS

I.

INTRODUCTION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

II.

SUMMARY OF RESULTS

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

II.A

Overview . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

II.B

Facility Performance Analysis Summary . . . . . . . . . . . . . . . . . . . . . 4

II.C

Unplanned Shutdowns, Unit Trips and Forced Outages . . . . . . . . . . . . 5

III.

PERFORMANCE ANALYSIS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

III.A Plant Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

III.B Radiological Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

III. C Maintenance/Surveillance . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

13

III.D Emergency Preparedness (EP)

. . . . . . . . . . . . . . . . . . . . . . . . . .

17

III.E Security . . . . . . . . . . . . . . . . . . . . . . . . . . .. . . . . . . . . . . . . .

18

III.F Engineering/Technical Support . . . . . . . . . . . . . . . . . . . . . . . . . .

20

III.G Safety Assessment/Quality Verification . . . . . . . . . . . . . . . . . . . . .

24

IV.

SITE ACTIVITIES AND EVALUATION CRITERIA . . . . . . . . . . . . . . . .

28

IV .A Licensee Activities

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

28

IV .B NRC Inspection and Review Activities . . . . . . . . . . . . . . . . . . . . .

29

IV. C SALP Evaluation Criteria. . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

29

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) is an integrated Nuclear.

Regulatory Commission (NRC) staff effort to collect observations and data to periodically

evaluate licensee performance on the basis of this information. The SALP process is

supplemental to normal regulatory processes used to ensure compliance with NRC rules and

regulations. SALP is to be sufficiently diagnostic to provide a rational basis for allocating

NRC resources and to provide meaningful feedback to the licensee's management to improve

the quality and safety of plant operations.

An NRC SALP Board, composed of the staff members listed below, met on February 26,

1992, to review the collection of performance observations and data and to assess the

licensee's performance at the Salem Generating Station. This assessment was conducted in

accordance with the guidance in NRC Manual Chapter 0516, "Systematic Assessment of

Licensee Performance. " A summary of the guidance and evaluation criteria is provided in

Section IV. C of this report.

This report is the NRC's assessment of the licensee's safety performance at the Salem

Generating Station, Units 1 and 2 for the period August 1, 1990 to December 28, 1991.

The SALP Board was composed of:

Chairman:

C. W. Hehl, Director, Division of Reactor Projects (DRP), Region I (RI)

Members:

T. P. Johnson, Senior Resident Inspector, Salem/Hope Creek, RI

J. C. Stone, Project Manager (Salem), Office of Nuclear Reactor Regulation (NRR)

C. L. Miller, Director, Project Directorate I-2, NRR

A. R. Blough, Chief, Projects Branch No. 2, DRP, RI

W. D. Lanning, Deputy Director, Division of Reactor Safety (DRS), RI

R. W. Cooper, Deputy Director, Division of Radiation Safety and Safeguards (DRSS), RI

Others in Attendance:

J. R. White, Chief, Reactor Projects Section 2A, DRP, RI

S. M. Pindale, Resident Inspector, Salem/Hope Creek, RI

S. T. Barr, Resident Inspector, Salem/Hope Creek, RI

H. K. Lathrop, Resident Inspector, Salem/Hope Creek, RI

J. G. Partlow, Associate Director for Projects, NRR

B. C. Westreich, Reactor Engineer, DRP, RI

I. B. Moghissi, Reactor Engineer Intern (Salem), NRR

M. J. Davis, Performance Evaluator, Performance & Quality Evaluation Branch, NRR

D. L. Caphton, Senior Technical Reviewer, DRS, RI

2

Others in Attendance (continued)

W. J. Pasciak, Chief, Facilities Radiation Protection Section, (FRPS), DRSS, RI

R. L. Nimitz, Senior Radiation Specialist, FRPS, DRSS, RI

J. C. Jang, Senior Radiation Specialist, Effluents Radiation Protection Section, DRSS, RI

L. S. Cheung, Senior Reactor Engineer, Electrical Section, DRS, RI

C. Z. Gordon, Senior Emergency Preparedness (BP) Specialist, BP Section, DRSS, RI

D. F. Limroth, Senior Reactor Engineer, Safeguards Section, DRSS, RI

S. Dembek, Project Manager (Hope Creek), NRR

3

II.

SUMMARY OF RESULTS

II.A

Overview

PSE&G operated both reactors of the Salem facility in a generally safe and conservative

manner. A strong level of management involvement in facility activities promoted a safety

conscious approach. Improvements were noted relative to unit operations, though instances

of personnel errors affecting plant performance occurred occasionally. An improving

performance trend was noted in the area of radiological controls. Facility material condition,

the quality of procedures, and system engineer performance also improved. The security and

emergency preparedness areas maintained a superior level of performance. Independent

review groups and station review committees provided safety conscious assessments of

related activities.

The Unit 2 turbine generator failure was a significant event that occurred during the period.

Several contributing causes were identified which indicated deficiencies in several functional

areas. The most prominent causes involved personnel error, insufficient preventive

maintenance, and inadequate surveillance. The licensee conducted a thorough review *of the

event, adequately determined root causes and related causal factors, and implemented or

planned effective corrective actions. Aggressive resolution of several performance related

issues were in process at the end of this SALP period.

Several initiatives indicated continued management support and consequent improvement in

the radiological controls program. However, occasional instances of insufficient corrective

actions, lapses in control and oversight of some activities, and deficiencies in the

maintenance of quality relative to the on-site dosimetry processing laboratory detracted from

an otherwise strong and effective program.

The licensee's programs and efforts relative to maintenance and surveillance activities have

been effective in assuring plant system reliability and sufficiency. Problems with material

condition of certain plant systems, while improving, still persist and challenge plant

performance, and continue to require intensive maintenance and surveillance efforts.

Instances of personnel errors, insufficient adherence to procedures, and inattention to detail

still persisted earlier in the period. The licensee's efforts to correct these types of

deficiencies resulted in a reduced frequency of discrepant performance later in the period.

The licensee's corrective action programs functioned well at times as evidenced by the

improvements previously mentioned. Occasional weakness was noted relative to the

effectiveness of some specific corrective actions, and some personnel errors due to a lack of

attention to detail indicated inconsistent performance. Notwithstanding these performance

deficiencies, there was an overall slight improvement noted during the SALP period.

4

11.B

Facility Performance Analysis Summary

1.

2.

3.

4.

5.

6.

7.

Functional

Area

Plant Operations

Radiological Controls

Maintenance/

Surveillance

Emergency

Preparedness

Security

Engineering/

Technical Support

Safety Assessment/

Quality Verification

Previous Assessment Period:

Present Assessment Period:

Rating, Trend

Last Period

2

2

2, Declining

1

1

2

2

May 1, 1989 through July 31, 1990

Rating, Trend

This Period

2

2, Improving

2

1

1

2

2

August 1, 1990 through December 28, 1991

5

II.C

Unplanned Shutdowns, Unit Trips and Forced Outages

1.

Power Level

8/17/90

25%

UNIT 1

Root Cause

Inadequate

Preventive

Maintenance

Functional Area

Maintenance/

Surveillance

An automatic reactor trip occurred due to low-low water level in the No. 14 steam generator

(SG). A loss of power to one non-vital bus occurred during supply breaker switching,

resulting in a loss of power to the No. 14 reactor coolant pump (RCP) motor. The breaker

failure was due to lack of cubicle preventive maintenance. The resultant decreased loop flow

caused a level shrink in the No. 14 SG. The unit subsequently proceeded to Mode 5 to

replace the No. 14 RCP motor when a phase-to-ground fault occurred during restart

preparations.

2.

9/10/90

78%

Personnel Error

Operations

The reactor tripped automatically due to low-low water level in the No. 13 steam generator

(SG). While preparing to isolate a high pressure turbine drain line steam leak, operators

inadvertently caused all turbine governor valves to close. This unexpected closure caused

SG level shrink to the trip setpoint. Licensee post-trip review determined that operations

personnel failed to initiate an adequate plan and procedure for the troubleshooting and repair

activities.

3.

6/16/91

100%

External Cause

NIA

An automatic reactor trip occurred due to a lightning strike on the phase "B" main power

transformer. The main generator output breakers opened to protect the main generator,

resulting in an automatic main turbine and reactor trip.

4.

9/16/91

100%

6

Inadequate

Installation/

Deficient Design

Maintenance/*

Surveillance &

Engineering/

Technical Support

An unplanned shutdown was made to repair an unisolable leak on the turbine electro-

hydraulic control system (EHC). The EHC leak was due to poor EHC piping installation

(insufficient thread engagement), and a deficient design that used dissimilar metals at the

EHC block connection. The condition was worsened by a missing EHC pipe hanger, which

resulted in increased vibration of the susceptible components.

UNIT2

Power Level

Root Cause

Functional Area

1.

914190

60%

Multiple

NIA

Component Failures

An automatic main turbine and reactor trip occurred on high-high water level in the No. 24

steam generator (SG). While at 100% power, the No. 21 steam generator feed pump

(SGFP) tripped on low suction pressure. Unit operators immediately initiated a rapid load

reduction to 60% power; however, the No. 24 SG water level reached the high-high setpoint

before the operator could effectively control an associated feedwater flow transient caused by

a failed Feedwater regulator valve. Two additional equipment problems resulted in the 1'To.

21 SGFP trip: a failed suction pressure switch; and a heater drain pump discharge control

valve which failed closed, causing a reduction in suction pressure.

2.

11/9/91

100%

Multiple Component

Failures/Personnel

Error

Maintenance/

Surveillance

and Operations

An automatic main turbine and reactor trip occurred during main turbine trip testing. The

main turbine and generator sustained severe damage when the turbine failed to trip and

proceeded to overspeed. Causal factors included lack of preventive maintenance and

surveillance testing on the turbine trip solenoid valves and operator procedure non-

compliances regarding failure to resolve a test deficiency during unit turbine generator

startup.

7

ID.

PERFORMANCE ANALYSIS

ID.A Plant Operations

III.A.1

Analysis

The previous SALP rated the Salem Operations functional area as Category 2. The quality of

the emergency operating procedures was noted as being an operations strength. The operator

requalification program was successful in that all licensed operators tested, passed the NRC

administered exam. Improvements were noted in management involvement, supervisory

oversight, and root cause analysis initiatives. A reduced reactor trip and personnel error rate

was observed. A weakness was noted relative to the quality of the abnormal operating

procedures.

During this assessment period, both reactor units were generally operated in a safe and

conservative manner. Examples include effective and conservative midloop operations, a

well planned 10-day maintenance and testing outage at Unit 2 and a prompt Unit 1 shutdown

due to increased electrohydraulic control system leakage. However, examples of deficient

performance were also observed. For example, a Unit 1 safety injection charging pump was

operated with its suction valve closed due to multiple personnel errors, communication

deficiencies, and breaches of several programmatic barriers in the safety tagging program.

Late in the period, a boric acid transfer pump was similarly operated with its suction valve

closed due to miscommunication and procedural non-compliance. Similarly, several licensed

personnel, including supervision, permitted a Unit 2 startup to proceed without resolving a

test discrepancy that indicated that the turbine overspeed protection system was not

functioning properly. That deficiency contributed to the Unit 2 turbine-generator failure

event.

Licensee efforts continued to be effective in reducing the frequency of reactor trips caused by

operations personnel. During the current period, there were a total of five reactor trips for

both units. This compares to six reactor trips in the last assessment period. During the

period, Unit 1 did not experience a reactor trip for over nine months and Unit 2 for over 14

months, during which Unit 2 operated continuously for 245 days. One of the five reactor

trips during this assessment period was attributed to personnel error by a licensed operator

while troubleshooting a sheared turbine drain instrument line. Operator error contributed to

the Unit 2 turbine-generator failure event. Operator response to reactor trips and plant

transients was excellent. In several instances, prompt operator actions averted the necessity

for reactor trips. One example included a Unit 2 steam generator feedwater pump trip,

where operator response was sufficiently effective and timely to prevent a unit trip.

The five operating shifts are effectively staffed, as each has three senior reactor operator

(SRO) and four reactor operator (RO) licensed individuals. Additionally, one separate SRO

licensed individual supervises the work control group for each shift. There are a total of 47

8

licensed operators, including 40 on-shift, and 7 in staff and training positions. Aggressive

management attention has been effective in resolving previously identified licensed operator

staffing weaknesses by training and qualifying several additional SROs and ROs.

The licensed reactor operator training programs continued to be effectively implemented.

Licensed operator initial and requalification examination performance demonstrated that the

candidates were generally well prepared for examinations. However, because of operator

performance and written test issues, one licensed operator initial examination administered

during this period did not demonstrate good performance. Additionally, the licensee was

ineffective in correcting self-identified training deficiencies identified during a facility audit

examination. This demonstrated a weakness in the corrective action process.

Licensed operators' safety perspective and awareness of plant conditions were consistently

evident. The procedure upgrade project has made a positive contribution toward improved

operations. Procedural adherence was generally good. Shift turnovers were formal and

included thorough briefings of the oncoming crew. Control room access was effectively

controlled, and activities were limited to those directly related to plant operations.

Aggressive management attention has resulted in reductions in the number of lit annunciators.

The use of overtime was properly controlled. Good performance of non-licensed equipment

operators was observed during unit tours and equipment testing and operation.

The licensee's emergency operating procedure (EOP) program and implementation have

generally functioned well. EOP quality and implementation were good. The licensee was

responsive in correcting specific EOP deficiencies; however, the licensee did not broadly

review other EOPs for similar deficiencies. Consequently, similar deficiencies existing in

other EOPs were not addressed. This indicated a narrowly focused review of identified

deficiencies. Abnormal operating procedures were being revised during the assessment

period to correct weaknesses identified in the previous SALP period.

Operations supervision and management oversight and attention to operations on a daily basis

were evident during this assessment period. An operational perspective of plant problems

and work prioritization was well communicated and understood in daily meetings. The daily

meetings provided the operations shift personnel a direct and effective interface with

operations and station management.

Plant housekeeping has continued to improve during this period. General area and

component painting and cleaning, enhanced housekeeping area responsibility controls, and

continued management emphasis have been effective in improving overall plant

housekeeping.

The licensee generally made timely and appropriate 10CFR50.72 NRC notification reports.

However, initial corrective actions for reporting and event classification deficiencies that

were identified in the last SALP period were ineffective and resulted in examples of untimely

and inconsistent reporting. One example included a late NRC notification of an auxiliary

9

feedwater system actuation, due to licensee reportability guidance that was inconsistent with

reportability requirements. Effective programmatic improvements were made later in the

period. The overall quality of written licensee event reports submitted during this period was

very good.

The overall fire protection program was effective. Dedicated fire protection personnel

performed well and were knowledgeable, which demonstrated an effective training program.

Of particular noteworthiness was the fire brigade's excellent response to the Unit 2 main

generator explosion and fire. Appropriate operator involvement and interface in fire

emergencies were evident. Plant and site management strongly supported the fire protection

program.

Summary

The Salem reactor units were operated safely and conservatively. Operator response to plant

transients and reactor trips was good; however, multiple errors and/or programmatic barrier

breakdowns contributed to several operational events. EOP quality and implementation were

good. Corrective actions for identified weaknesses were at times incomplete. Increased

management involvement was effective in resolving licensed operators staffing weaknesses;

however, the licensed reactor training programs demonstrated some weaknesses. Daily

supervision and management oversight of plant operations was good.

III.A.2

Performance Rating: Category 2

ill.B Radiological Controls

III.B. l

Analysis

The previous SALP rated radiological controls at Units 1 and 2 as Category 2. The program

was characterized as good with a sufficient level of management involvement. Overall

ALARA efforts were very good, but there were weaknesses in the corrective action process

for self-identified radiological concerns and the radioactive material and contamination

control programs. The radwaste handling, transportation, and environmental monitoring

programs were effective, and performance in the area of liquid and gaseous effluent controls

was adequate.

During the current period, NRC identified that the licensee took a number of actions to

improve overall radiological controls and address previously identified weaknesses. The

actions included sending personnel to visit similar stations, establishing incentive programs

for good personnel performance, and developing a Unit 1 Outage Handbook that included

organizational descriptions and responsibilities of key personnel. Very good efforts were

made to respond to a strike by contractor radiological controls personnel. For example,

during the Unit 1 outage, work packages were prioritized to ensure that proper radiological

10

controls were implemented for on-going work. NRC observations at Unit 2 noted no

negative impact on the effectiveness of radiation protection coverage of non-outage activities.

There was a good level of expertise available within the staff, and no excessive use of

overtime was noted.

There were no external or internal personnel exposures in excess of NRC or administrative

limits during the period.

The NRC's performance-based review of significant Unit 1 outage

radiological work activities (e.g., steam generator sludge lancing) identified performance

deficiencies including improper monitoring of personnel exposure relative to large radiation

dose rate gradients, insufficient monitoring of airborne radioactivity, instances of personnel

unnecessarily working in elevated radiation fields, and poor contamination control practices.

These lapses in the quality of radiological controls were attributed to weaknesses in

procedures and the oversight of work activities by radiation protection personnel.

These deficiencies were promptly corrected by procedure revisions and appropriate training

of applicable personnel. Subsequent NRC review during the Unit 2 outage later in the period

identified significantly improved oversight of work activities. There was a high degree of

management and supervisor oversight of on-going radiological work activities, effective shift-

to-shift planning of work, and excellent oversight of work activities from an ALARA

perspective. In light of the significant improvement identified late in the period, the overall

external and internal exposure control programs were considered good.

Relative to ALARA efforts, the licensee exhibited effective planning and preparation for

steam generator work activities which resulted in the possible reduction of personnel

radiation exposure. For example, the licensee increased the number of steam generator tubes

to be tested in each generator, resulting in all tubes being tested within four outages (versus

the previously scheduled five outages), at a significant exposure saving. The station's

..

aggregate personnel exposure continues to be well below industry averages and among the

lowest in the industry for comparable facilities. Exposure goals were challenging and were

met.

The training and qualification program for radiological controls technicians contributed to a

good understanding of program requirements. Although there was no specific training and

qualification program for radiation protection supervisors, this did not result in any observed

operational performance problems. A specific training program was established late in the

period. In addition, as a result of the weaknesses in radiation protection oversight of Unit 1

outage activities identified by the NRC, PSE&G management discussed their expectations

regarding the level of oversight of work activities with radiation protection personnel.

Radiation workers were provided appropriate training.

Late in the period, an evaluation of the on-site dosimetry processing laboratory by personnel

from the National Voluntary Laboratory Accreditation Program (NVLAP) identified a

number of significant weaknesses in the management of the PSE&G processing laboratory.

The licensee immediately suspended processing of dosimeters and implemented extensive

-.

11

corrective actions to improve processing. NRC reviews at the end of the period indicated

corrective actions were on-going and dosimetry system performance met applicable

performance standards. The NRC's review of this matter found that the weaknesses

stemmed from the loss of key supervisory and management personnel and a lack of

understanding, by replacement personnel, of regulatory aspects associated with maintaining

an accredited personnel dosimetry program. Although no decrease in the quality of

dosimetry processing information was identified, this matter indicated weak understanding of

program and personnel qualification requirements by management.

The radioactive material and contamination control programs were effective. Weaknesses

identified during the previous period were addressed by a task action plan which included

revision of procedures, training of personnel, and purchase of new equipment. The licensee

has been aggressively decontaminating, cleaning and painting the radiologically controlled

areas (RCAs) of the station. As a result, total station contaminated area compared very

favorably to similar facilities. Isolated lapses in contamination control within the RCA were

noted, but quickly corrected. The efforts to minimize personnel contamination were

commendable, with very few personnel contaminations occurring during the Unit 2 outage.

The radiological occurrence report program, while continuing to be weak into the early part

of this SALP period, improved over time. NRC review late in the period found that the

program was enhanced, self-identified concerns were resolved in a timely manner,

appropriate corrective actions were taken, and root causes were clearly identified. Findings

were discussed at appropriate levels of management, including weekly station management

meetings. Monthly radiological controls performance summaries were provided to

management. A radiological controls assessor was assigned to support the Unit 2 outage.

The licensee's efforts to improve the program were commendable and indicated better

management oversight of self-identified problems.

The licensee has been proactive in improving chemistry programs and hardware. For

example, installation of an in-line secondary monitoring system, including an ion-

chromatograph, was completed during the period. A successful secondary chemistry

program has resulted in excellent steam generator performance. Likewise, excellent primary

chemistry and active management oversight has resulted in excellent fuel performance and

reliability. This has resulted in reduced exposure associated with fuel Jeaks and unplanned

steam generator work activities.

A strong radioactive waste management and transportation program was implemented.

Personnel demonstrated good understanding of program requirements as the result of an *

effective training program. Prompt corrective actions were evident when problems were

identified. Overall performance was very good. The volume of waste shipped for burial

was well below the industry average. The organization and staffing exhibited stability and

strength. The radwaste processing methods continue to operate well, and the on-site

-..

12

storage of radwaste was generally minimal. There was sufficient oversight of radioactive

waste activities. The involved personnel demonstrated adequate technical depth and scope in

the management and control of radioactive waste processing and shipping operations.

The licensee continued to conduct an effective Radiological Environmental Monitoring

Program (REMP). The meteorological monitoring program was sufficient in ensuring that

meteorological instruments were operable, maintained, and calibrated, meteorological data

were obtainable from various locations on and off site and an effective QC program was in

place to assure the quality of REMP sample analyses. Audits by the Quality Assurance

Department personnel were thorough and of appropriate technical depth to assess the REMP.

NRG reviews of the radiological effluent monitoring and control program indicated

acceptable calibration of effluent/process radiation monitoring systems (RMS), but there were

a number of Engineered Safety Feature actuations during this assessment period due to

spurious RMS signals and equipment failures. NRC review of the progress of the short and

long term RMS upgrading projects, established during the previous SALP period, indicated

the licensee was on schedule in pursuing these projects. An effective effluent control

program was conducted by the Chemistry Department.

Overall QA oversight of program areas was good. However, the observations of isolated

problems indicated a potential need for expansion of quality oversight into areas not

previously evaluated (e.g., NVLAP adherence).

Summary

Weaknesses in the radiation protection program were noted during the Unit 1 outage early in

the assessment period. The licensee took effective corrective actions to resolve the

weaknesses, including those associated with dosimetry processing, and implemented a good

radiological controls program. Overall staffing and training were good. ALARA efforts and

performance were commendable. Overall radwaste processing, storage and transportation

activities were very good. The licensee continued to implement effective confirmatory

measurements, effluent controls and a REMP.

III.B.2

Performance Rating: Category 2

Trend: Improving

13

m.C Maintenance/Surveillance

III.C.1

Analysis

The Salem Maintenance and Surveillance functional area was rated as a Category 2, with a

declining trend, in the previous SALP assessment. Maintenance program strengths were

noted in management involvement, work standards, and reliability centered maintenance

initiatives. Weaknesses were identified relative to the large maintenance backlog, procedure

quality, contractor maintenance control, and spare parts availability and control. The poor

overall material condition of the plant was also noted as a significant weakness. Surveillance

testing activities were characterized as being conducted in a well controlled fashion by

knowledgeable and experienced personnel, although weaknesses were noted in procedure

quality and in the ineffective actions which led to missed surveillances.

Maintenance:

The Salem maintenance program was effective and was satisfactorily implemented during this

assessment period. The maintenance organization performed a large volume of successful

maintenance activities and effectively supported plant operations. Management involvement

was evident, as many of the deficiencies noted in the previous assessment were addressed

and progress was achieved toward their resolution during this period. Improvements were

accomplished in the maintenance backlog, procedure quality and parts availability, but

deficiencies continued to exist in personnel error. The maintenance organization successfully

responded to plant equipment problems over the course of the assessment period and

functioned well with other Salem departments, as management initiatives began to reverse the

trends identified in the last assessment.

"

The Salem maintenance staff remained stable and experienced, and Maintenance Department

personnel were well trained and qualified. The three senior managers in the Maintenance

Department were relatively new to the Salem Station during this period, yet succeeded in

implementing a new work standards program and improving overall personnel performance

and teamwork. Despite the staffs experience level and management's direction, instances of

personnel error due to inattention to detail continued to exist. Examples included reactor

protection system actuations and plant system inoperabilities which resulted from improper

procedure adherence. Factors contributing to the number of personnel error events that

occurred during the SALP period were incomplete training and weak supervision of non-

Maintenance Department personnel, such as contractors and site services, performing work at

Salem. The majority of these instances occurred in the beginning of the period, and as a

sense of ownership developed over this period, the frequency of these events decreased.

Personnel training continued to receive strong management attention and was well supported

by the excellent training center facilities.

~ . .

14

The Salem maintenance facilities are well equipped and adequately support all maintenance

activities at the site. Management has taken steps to improve the previously identified

problems with spare parts control and availability .. The PSE&G inventory management

improvement initiative included a newly formed organization under a general manager, a new

warehouse for centralizing and storing the parts inventory onsite, and the state-of-the-art

computerized warehouse automated material management system (W AMMS). The effort

taken by PSE&G to gain control of the spare parts inventory showed indications of being

effective, as the new warehouse went into service and parts availability began to improve at

the end of the SALP period.

Good management involvement and oversight resulted in the successful completion of a

refueling outage at each unit during the assessment period. Good outage performance at

Salem was partly attributable to the institution of dedicated unit outage managers during the

last period. In addition, a mid-cycle outage was performed at Unit 2 for the accomplishment

of maintenance activities, and six forced outages occurred at the two units. The last forced

outage at Unit 2 was caused by a turbine overspeed event at the end of the period and

became the unit's sixth refueling outage. Core alterations, plant modifications, and other

refueling activities were well supported by maintenance operations. The Maintenance

Department responded especially well to the Unit 2 turbine overspeed event, as event clean-

up, plant repairs and early outage implementation were well executed on extremely short

notice.

Effective planning, the improvement in spare parts availability, and the introduction of a

reliability centered maintenance program have helped increase maintenance productivity and

reduce the maintenance backlog. The number of overdue preventive maintenance activities,

while still high, had reached its lowest point in three years by the end of this assessment

period. Despite the improvement in planning and work control, two events occurred whi~h

showed the need for continued attention in this area. A follow-up to the NRC Maintenance

Team Inspection (MTI) revealed that corrective actions taken for several MTI findings were

not thorough, predominately due to inadequate planning.

The Unit 2 turbine overspeed event in November 1991 revealed additional maintenance

planning weaknesses which directly contributed to the occurrence. Over a year prior to the

event, PSE&G committed to replace the Unit 2 solenoid valves that were directly responsible

for the overspeed event, at the first outage of sufficient duration. Due to a failure in the

planning process, the solenoids were not replaced in the May 1991 Unit 2 mid-cycle outage.

Further, though information and experience was available that indicated that the solenoid

valves could fail to function, the licensee did not establish any preventive maintenance

program for these devices.

One reactor trip was attributed to maintenance activities during this period. The trip

occurred during 4kV non-vital auxiliary power transformer feeder breaker switching. The

failure of the feeder breaker to properly close caused the loss of a reactor coolant pump, and

15

the reactor tripped on low-low water level in the respective steam generator. The root cause

of the reactor trip was mechanical failure of the breaker due to a lack of preventive

maintenance of the breaker cubicle.

An area noted in the previous assessment as a weakness was the plant material condition of

both Salem units. Recognizing a need to improve in this area, PSE&G created a special task

force with a dedicated supervisor to address material condition and equipment improvements.

While a large amount of work remains to be done, this licensee initiative has resulted in

significant improvements in the appearance and functionality of a number of Salem plant

areas. For example, the number of internal plant system leaks was reduced by over 50

percent during this assessment period.

Surveillance:

The Salem surveillance program was safely implemented during the assessment period and

positively contributed to the safe operation of the Salem station. The personnel performing

the surveillance testing were well trained and fully successful in carrying out the Technical

Specification (TS) required surveillance program.* The number of plant events related to

surveillance test performance decreased from the last period and showed a positive trend over

this period. The licensee completed an audit in the middle of this assessment period to

ensure the adequacy of the surveillance program in meeting all TS requirements. As a result

of the audit, PSE&G adequately resolved the existing administrative problems in the

program, and the number of missed surveillance tests dropped over the remainder of the

SALP period.

There were, however, five missed surveillance tests this period. Similar to last period, the

root cause of the missed tests was inadequate administrative controls. This number is do~n

from seven during the last SALP period, and the problem was successfully addressed by the

licensee's TS audit. There were no missed surveillances after May 1991. The number of

plant events related to surveillance testing also dropped this period, despite the increased

challenge posed by the problems encountered with the Salem 4kV vital bus undervoltage

relays and the Salem radiation monitoring system (RMS). Fourteen Licensee Event Reports

were submitted by PSE&G this SALP cycle documenting surveillance personnel errors and

related engineered safety feature actuations. While nine of these events were related to the

4KV bus relays and the RMS, many events remained due to personnel error and inattention

to detail. Plant events such as a chemical and volume control system valve misalignment, a

steam generator pressure channel inoperability, and circuit breaker TS non-compliance were

all attributed to personnel error and show the need for continued management attention in

this area.

No plant trips during this assessment period were directly caused by improperly performed

surveillance activities. Surveillance related improvements noted during the period included

the institution of a self-verification process designed to reduce personnel errors, and the

initiation of a system to transmit trending data from the Maintenance Department to the plant

..:._r,

-

16

Technical Department to better evaluate system and component performance. The lack of

this trending data was cited as a weakness in the previous period.

The Unit 2 turbine overspeed event exposed a weakness in the Salem surveillance test

program relative to balance of plant systems. Surveillance tests were performed to comply

with the Technical Specifications relative to turbine overspeed protection system, but the

surveillance method was not sufficient to verify the independent operability of systems and

components that actually effected turbine overspeed control. The licensee's failure to

provide sufficient suveillance testing was one of the contributing factors to the turbine

overspeed event.

The Salem Inservice Testing (IST) and Inspection (ISI) programs were effectively

implemented over the assessment period. In order to correct a deficiency noted in the last

period, all affected Salem equipment was marked with the proper locations for vibration

probes for repeatability during testing. Other activities reviewed with positive results during

the period included the Unit 1 containment integrated leakage rate test, the Unit 1 steam

generator inspection program, the Unit 1 outage radiography weld examination program, and

the installation of a service water full flow test line for the ease and repeatability of pump

testing.

Summary

The Salem maintenance and surveillance programs were successfully implemented during this

assessment period and contributed to the assurance of nuclear safety during the operation of

the Salem power plants. The majority of the problems noted over the course of this SALP

cycle, in both the maintenance and surveillance areas, were the result of personnel error and

inattention to detail. Although continued management attention is warranted in this area, _.the

programs and initiatives undertaken by Salem management following the previous SALP have

been effective in arresting the negative trend documented in that report.

III.C.2

Performance Rating: Category 2

III.C.3

SALP Board Comment

Although the SALP Board recognized the reversal of the previous negative trend in the

Maintenance/Surveillance functional area, continued PSE&G management attention is

warranted in previously identified weak areas, such as personnel errors, plant material

condition and maintenance planning, in order for the Salem maintenance program to continue

to improve.

. ' .

17

ID.D Emergency Preparedness (EP)

III.D.1

Analysis

During the previous SALP, BP was rated Category 1. That rating was based on strong

management involvement, a highly qualified BP staff, prompt resolution of technical issues,

and excellent training. PSE&G was very effective in exercise performance and in response to

actual events requiring emergency classification.

During this SALP period, the operational status of PSE&G's Emergency Preparedness

Program was found superior by NRC review. Management was directly involved in the

  • daily operation of the BP program. Three ievels of management provided oversight.

Managers at each level were qualified as members of the emergency response organization

(ERO), reviewed all changes to the Emergency Plan and Procedures, reviewed drill

scenarios, and regularly participated in drills. A thorough audit of the EP program by two

independent groups from the Quality Assurance Department identified no deficient program

areas. Management also fostered an excellent relationship with state, county, and local

governments through numerous meetings and training sessions, and in support of resolving

FEMA-identified concerns.

PSE&G was aggressive in handling technical issues. The BP Department effectively

maintained emergency response facilities and implemented a number of significant facility

improvements. These included the installation of a new callback system for ERO members,

completion of the control room simulator and Safety Parameter Display System data links to

the Technical Support Center and Emergency Operations Facility. Emergency Response

Data System installation is in progress. The new emergency news/community center, which

is under construction, also represents a significant PSE&G off-site commitment. The Puplic

Alerting System throughout the Emergency Planning Zone was maintained at 98.8% siren

availability, exceeding Federal Emergency Management Agency (FEMA) standards.

Operators at Salem and Hope Creek responded to several actual Unusual Events and one

Alert during this assessment period. Operators consistently displayed good knowledge and

familiarity with emergency action levels contained in the Event Classification Guide (ECG).

Events were correctly classified, and timely notification was made to the States and the

NRC. All response actions were consistent with Emergency Plan requirements. During the

Alert at Salem Unit 2, PSE&G activated the Salem Operations Support Center which was

instrumental in providing good in-plant support and assistance in response to the turbine-

generator failure.

Staffing of the BP program remained strong. The program was maintained by a full time,

fully qualified staff of fourteen individuals. The well-balanced mix of disciplines included

five senior reactor operators, experienced health physicists, and additional staff with

experience in radiological controls and equipment operations. The ERO was also fully

staffed, with all key managerial positions filled.

18

EP training was comprehensive, innovative, and thoroughly implemented. Operations and

EP personnel training continued to be significantly enhanced through drills on the control

room simulator. Training drills for shift operators were conducted weekly at both facilities.

The nine additional extensive training exercises conducted during the period tested major

portions of the Emergency Plan. Changes and innovations to EP training methodology were

constructive in qualifying ERO staff. ERO qualification was kept at a high level, as

demonstrated in walkthrough training sessions with ERO members. Off-site training was

also a strength, with well developed training and quality information provided to the states

and counties.

Training effectiveness was demonstrated by the excellent performance of the ERO during two

NRC-observed annual exercises. Both scenarios were very challenging, particularly the 1990

exercise, which. included full state participation, and involved both plume (10-mile) and

ingestion (50-mile) exposure pathways. Only minor areas for improvement were noted during

this exercise. Also, there were no FEMA deficiencies. During the 1991 exercise, ERO

performance was also effective. A poorly worded emergency classification guide did,

however, cause an exercise weakness involving tardy declaration of a Site Area Emergency.

This weakness had not been identified in any previous drills or exercises.

Summary

PSE&G has maintained a sound and effective EP program with clear management

commitment to maintaining a highly professional and qualified staff. The EP site staff was

proficient in ensuring readiness for implementation of emergency response activities. The

training program was thoroughly defined and effectively implemented with different

innovative performance-based techniques. The ERO was well qualified as evidenced by

exercise performance. Facilities and equipment were well maintained, and upgraded in qises

where improvements were needed. Licensee support for local governmental and support

organizations was strong.

III.D.2

Performance Rating: Category 1

111.E Security

III.E.1

Analysis

The previous SALP rated this area Category 1. That rating was based on the licensee

maintaining a performance orientated security program which reflected significant

enhancements and which exceeded regulatory requirements.

During this SALP period, station security management, which consisted of

knowledgeable and experienced security professionals, continued to provide effective

oversight of the security program, even under adverse conditions. When a security

.....

19

officer sustained a serious self-inflicted injury while on duty at the station, management

conducted an intensive investigation of the incident, and contracted a team of

psychological and security consultants to counsel members of the security force and to

conduct a study of security operations. This was indicative of management's sensitivity to

the impact of the incident on the security organization and whether the organization

contributed to the incident.

Management's attention to and involvementin the security program remained evident

throughout. this period, especially during construction of a new warehouse which required

the reconfiguration of the protected area barrier. The construction project progressed

without any negative program impact. The licensee continued to aggressively address

NRC findings and concerns. Operability.of security monitoring equipment was high as

evidenced by the minimum number of compensatory posts and a decreasing number of

security events that required logging.

The licensee also continued to conduct very aggressive, in-depth and comprehensive

audit and self-assessment programs. These programs were very effective in identifying

potential weaknesses and correcting them before they became security problems.

Staffing of the security organization was very good, with limited use of overtime and a

minimum backlog of work on security equipment. Overtime use during scheduled

refueling outages was necessary and adequately controlled. Late in the period, the

licensee increased* its security force by 30% in order to minimize the impact of overtime

on the force which was identified as a potential weakness during the security study.

Security related contingency plans that were implemented during a union job action were

excellent. The use of the auxiliary guard house was effective in separating work groups.

Security force members were thoroughly briefed on contingency actions, and good

communications among station groups were maintained.

Corporate management continued to provide appropriate financial and technical support

for the security program and organization. This was evident early in the period when

consultants were contracted to conduct a comprehensive study of the security program

and organization, and throughout the period as a systematic upgrade of the aging

assessment aids continued. Support was also apparent by the increase in security force

staffing.

As evidenced by responses to two Fitness-for-Duty (FFD) events during the period, the

licensee continued to implement a clear and strong FFD policy. The policy was

effectively promulgated to employees and contractors, and measures established to

implement the policy were properly maintained. In addition, supervisors continued to

demonstrate their knowledge of the program and its implementation.

20

In addition to a team of licensee security supervisors who provided effective day-to-day

oversight of the contractor security force, the licensee continued to maintain a well-

developed and administered security force training program. The effectiveness and

quality of the supervision and training were apparent by security officers' display of (1)

knowledge in security matters, (2) attentiveness to security responsibilities, (3)

responsiveness to security problems and ( 4) aggressiveness in following up on identified

security deficiencies. There were also a minimal number of events that were attributed

to security-personnel error.

The licensee's event reporting procedures were found to be clear and consistent with

NRC reporting requirements. Two event reports were submitted to the NRC during this

period. One report involved a security officer being inattentive to duty and the other

involved delayed arrival of a shipment of fuel. The licensee's reports were clear, concise

and indicated appropriate responses in each case.

During this period, the licensee submitted one revision to the training and qualification

plan. The revision was of high quality, technically sound and reflected well-developed

policies and procedures.

Summary

The licensee continued to maintain an effective, performance-based security program

which, in many areas, exceeded regulatory requirements. The licensee demonstrated

sensitivity in effectively managing events that challenged the performance of the security

organization. The audits and self-assessments of the security organization, program

upgrades and enhancements were indicative of excellent support from both corporate

and station management for the security program.

111.E.2

Performance Rating: Category 1

111.F Engineering/Technical Support

111.F.1

- Analysis

The previous SALP rated Engineering and Technical Support as Category 2. The

previous assessment identified weaknesses in the implementation of the temporary plant

modification program. The previous SALP also identified deficiencies involving

inconsistencies in the quality of work performed by system engineers and a problem with

the implementation of the Station Qualified Reviewers (SQR).

During this SALP period, noted improvements in the implementation of temporary

modifications were observed. Increased management control and oversight, including

periodic Station Operations Review Committee review, and increased engineering effort

21

have been successful in reducing the duration and backlog of temporary modifications.

Improvements have also been noted in the area of Station Qualified Reviewers (SQR).

The required SQR training was completed. Safety review group audits of this area also

have noted program improvements.

Engineering and Technical Support for the Salem plants was organized with a corporate

engineering group, known as Engineering and Plant Betterment (E&PB), and the onsite

system engineering group. E&PB handled those major engineering efforts such as plant

modifications, and design bases reconstitution. The onsite system engineering group also

supported operational, maintenance, testing and minor design change activities. E&PB

was appropriately staffed with experienced personnel in various engineering disciplines.

E&PB engineering problem evaluations were generally good. A good root cause analysis

was effective in identifying causes of reactor coolant system resistance temperature

detector drifting problems. Design change packages were of good quality. They were

complete and in accordance with applicable procedures. Two deficiencies were observed

in the plant modification control area. There was a lack of an independent, in depth

review of the emergency diesel generator load studies, and an inadequate control in the

use of fuses. The lack of adequate review resulted in the emergency diesel generator

load studies containing substantial technical errors. The inadequate control of fuses

resulted in the use of six undersized main fuses in safety-related 125 volt DC system.

Although no operability issues resulted, this condition was known to the licensee for a

  • considerable period of time. Prompt management attention was not implemented to

assure system reliability.

A problem involving lack of required evaluations of control room habitability for all

chemicals stored on-site was identified. The NRC was reviewing this matter at the end

of the period. During the previous SALP period, concerns were identified involving air

balance and humidity testing for air cleaning systems and high oxygen concentrations in

the Unit 1 waste gas decay tank. The licensee's progress in resolving air balance and

humidity issues has been slow.

The E&PB organization worked well with the onsite system engineering group, and

communications were noted as being improved. This was evidenced during the followup

of the main steam isolation valve design change. The onsite system engineering group

was well staffed with engineers. The establishment of a Small Design Change Project

team has been effective in reducing the system engineering workload. As a result,

improvements were noted relative to system engineer involvement in periodic field

inspections of their systems. System trending, knowledge of system outage work, and

increased management awareness have been effective in improving safety system

availability.

-.

22

System engineers' questioning attitude, and overall sense of safety perspective were good,

with noted improvements during this period. For example, system engineer

troubleshooting activities and corrective action plans for the radiation monitoring system

deficiencies, vital bus undervoltage relay setpoint drift problems, steam driven auxiliary

feedwater pump problems, Unit 2 turbine generator failure and higher than normal river

water temperatures were effective and thorough. Additionally, system engineer presence

in the field was apparent, as evidenced by their identification of several hardware issues,

such as degraded small bore service water piping and main steam isolation valve air

control valve problems. Of the five automatic reactor trips during the period, none were

attributed to the engineering activities.

Technical support for refueling and maintenance outage periods and for post-outage

recovery activities was effective. Both E&PB and onsite system engineering participated

in and interfaced with the outage organization on a daily basis. System engineering was .

noted as providing strong support during reactor startup and power ascension testing.

The licensee has established effective project management task forces led by E&PB

managers to address specific technical issues, modifications and problem areas. These

included the configuration baseline documentation (i.e., design basis reconstitution),

service water and radiation monitoring system (RMS) modifications, and the Salem

material condition revitalization project. These task forces successfully integrated offsite,

onsite and contractor engineering activities. A large number of licensee. event reports

were due to actuations caused by the poorly designed radiation monitoring systems. The

licensee has a plan in-place to correct these RMS design problems.

The Procedure Upgrade Project (PUP) showed good progress during the period. The

PUP was managed through the station Technical Department during the last SALP .

period. During this SALP period, management of PUP was moved out of the line

organization to a dedicated Salem revitalization group. This management shift appeared

to be effective as the project completed about 50% of the procedure upgrade. The

revised PUP procedures have been effective in decreasing errors and events previously

caused by inadequate or poor procedures.

Improvement was noted in the engineering procurement activities. Until 1990, the

licensee had no formal procedure for controlling the commercial grade item dedication

program. The licensee's personnel had worked closely with Electric Power Research

Institute (EPRI) personnel in the development of the EPRI commercial grade dedication

program guidelines.

Engineering's Self-Assessment Program emphasizes the key performance elements to the

engineering and management personnel. By setting goals and tracking them and by

having upper management support, significant improvements have been achieved. The

  • .

23

contribution from this effort was a positive factor in improving engineering performance,

as evidenced by a reduction in overdue engineering items, improved safety evaluatfon

quality and improved performance concerning design change project timeliness.

There was generally strong evidence of management support for improving the

engineering effort. Funding was provided by management, not only for routine

engineering activities, but also for engineering enhancement projects, such as the Salem

Revitalization Project (SRP), the Configuration Baseline Document (CBD) project, for

planned additional engineering facilities, and for additional computerized material to

increase efficiencies in engineering activities. The CBD project involves the design basis

reconstitution of 87 systems and structures for Salem. During this SALP period, 24

systems were completed. The licensee also implemented the computerized Document

Information Management System to complement the hard copy CBD for the completed

systems. However, one example where a lack of aggressive management attention

existed regarding the pressurizer power operated relief valves (PORVs). Insufficient

vendor and engineering guidance for material specifications and torquing requirements

has resulted in numerous PORV failures.

The technical content of license amendment requests and other licensee initiated

submittals was generally good and continues to improve. However, the technical content

of responses to certain NRC generic communications has required significant additional

information submittals by the licensee. Examples include submittals relative to station

blackout specifications, thermal stresses in piping systems connected to the reactor

coolant system (NRC Bulletin 88-08) and information concerning the vendor information

interface program (NRC Generic Letter 90-03). In some cases, the initial responses

provided only a schedule for submission of the requested information. However, when

the additional technical information was submitted, it was of high quality and respons~ve

to the staffs request.

Summary

The control and limitations of temporary modifications improved, and improvements

were made in the quality of work performed by the systems engineers and in the SQR

program. Corporate engineering performed well with only a few deficiencies in the

design change control area being observed. The onsite system engineering performed

well in supporting plant operations. Corporate and onsite engineering management

involvement was generally effective, although some plant issues resulted from a lack of

management attention. Progress was observed in two of the engineering enhancement

projects, the Salem Revitalization Project and the Configuration* Baseline Document

Project. At the end of the period, improvements in the engineering procurement

program were also observed. The engineering for license amendments was of good

quality; however, weaknesses were observed in the responses to NRC generic

communications.

. .

24

III.F.2

Performance Rating: Category 2

III.F.3

SALP Board Comment

There was a distinct difference in the level of quality between the licensee's responses to

generic issues and its other submittals. The licensee should pay particular attention to

improving the overall quality of its responses to generic issues.

111.G Safety Assessment/Quality Verification

IIl.G.1

Analysis

The previous SALP rated this area as Category 2. That assessment noted that

management was involved in problem resolution and the assurance of nuclear safety.

Onsite, offsite and event followup review groups had provided effective, independent

evaluation of plant activities. A weakness was noted concerning the use of the station

qualified reviewer, which prevented some issues from being reviewed by the onsite

review committee. Quality Control (QC) involvement was not sufficient to maintain an

independent review of station activities. The material condition of the plant was poor.

The implementation of the procedure upgrade project was delayed, and inadequate

procedures continued to contribute to plant events.

During this assessment period, corporate and station management continued to be

involved in the conduct of daily station operations and in effectively responding to

unplanned occurrences. Daily station manager accountability meetings were effective_ in

ensuring an appropriate level of oversight of station activities. In addition, the daily

morning meeting provided a useful operational summary for station management with

emphasis on current unit problems and identification of high priority work. That

meeting also provided the senior nuclear shift supervisor with direct access to station

management. On a semi-annual basis, the Salem General Manager conducted State-of-

the-Station meetings, which effectively communicated management's assessment of

performance. Management and supervision were observed to be present in the field,

including weekends.

Strong management attention and support were provided during this assessment period

to develop programs to improve the material condition of the Salem facility and to

improve the procedures. As a result, the procedure upgrade project (PUP) has made

noticeable progress during this assessment period. Station procedure overall quality has

likewise improved, with clear improvement noted in the procedures which have been

processed through the PUP. Plant material condition has shown some improvement.

25

Conversely, a lack of management assessment and untimely correction of known

deficiencies contributed to the existence of long-standing concerns associated with the

pressurizer power-operated relief valves.

The licensee's Station Operations Review Committee (SORC) effectiveness improved

during this assessment period. SORC reviews of reactor trips, proposed design changes,

significant technical issues, and reportable events were generally very good and displayed

an excellent safety perspective.

The independent onsite safety review groups continued to provide effective reviews of

station activities and identification of safety concerns, including the Station Quality

Assurance (SQA) Department and Safet)' Review Group (SRG). Two specific examples

are the SQA identification that Technical Specifications were inappropriately exited

during surveillance testing because of ineffective communications, and the identification

that testing of the Unit 1 containment penetration conductor overcurrent protection

devices was not properly implemented. SQA performance-based inspections continued

during this period, and Quality Control (QC) increased direct inspection activities by

providing increased department notification and hold points. SRG investigations were

comprehensive, focused on safety issues and provided meaningful recommendations to

plant management. The independent Offsite Safety Review (OSR) group was also used

effectively and provided a safety conscious review of licensee activities.

The Significant Event Review Team (SERT) process provided a multi-disciplined,

independent review of reactor trips or other safety significant events. SERTs conducted

during this assessment period were generally of excellent quality, including proper root

cause determinations and effective corrective actions. In one instance, however, the

NRC identified a minor weakness associated with a SERT evaluation in which the

..

licensee's prior recognition of existing deficiencies which contributed to the event was

not identified by the SERT. The SERT process was used effectively by station

management and was appropriately complemented by those evaluations performed by

the SRG.

The licensee had previously placed increased emphasis on attention to detail in an

attempt to reduce the number of personnel errors and procedural problems at Salem.

While PSE&G's efforts had initially been successful, station performance has been

inconsistent during this SALP period. Specifically, at about the middle of the period, a

high number of events, across all functional areas and in a relative short time period,

were attributed to personnel errors and procedural compliance/adequacy problems.

PSE&G management took action and the error rate had decreased. However, near the

end of the assessment period, several licensed operators permitted a Unit 2 startup to

proceed without resolving a test discrepancy, and this was identified as one of several

causal factors that led to the Unit 2 turbine generator failure.

-.

26

Communications and interfaces among the various station groups were generally good.

However, several ineffective intradepartmental and interdepartmental communications

were contributing causes for plant events and equipment concerns. Prompt management

action was taken and was effective in improving performance.

Outage preparations for the Salem Unit 1 refueling outage were excellent and proactive.

Aggressive outage goals were established, and thorough SQA/QC inspections and

surveillance plans were developed .. Likewise, the Salem Unit 2 10-day maintenance and

testing outage was well planned. PSE&G management displayed an excellent safety

perspective in electing to conservatively shut down the unit to perform the planned

activities.

The licensee's corrective action program generally functioned well. Improvements were

noted relative to the material condition of both units, the quality of procedures, and in

system engineer performance. However, weaknesses were noted in the LER

commitment tracking system (one causal factor of the Unit 2 turbine failure), in

correcting licensed operator training and EOP deficiencies, in addressing undersized 125

volt DC fuses, and in their investigative efforts relative to security program concerns.

Also, deficiencies were noted in personnel performance and attention to detail, which

resulted in personnel errors. At times, this resulted in degraded performance trends

during the period.

The quality of requests for routine licensing actions has shown some improvement in that

the number requests for additional information has declined. There was one notable. .

exception, however, which was the request to change the diesel generator surveillance

requirements. Significant additional information was required from the licensee. (See

Section IIl.F.) There was only one non-routine licensing action, a Waiver of Compfo~,nce

for a containment fan cooler unit, which was issued by the NRC Regional office. The

quality of the licensee's submittal was good.

The quality of the responses to NRC generic communications has not significantly

improved. On occasion, requests for additional information have been necessary for

completion of staff review (See IIl.F.)

Summary

PSE&G management continued to be effectively involved in station activities and in

problem resolution. The SERT process has been effective, and the independent review

groups ( onsite and offsite) provided safety conscious reviews of licensee activities. An

increase in QC involvement in direct inspection activities was noted. An improvement in

SORC effectiveness was also noted. The PUP made noticeable progress during this

period that resulted in an overall improvement in station procedures. Personnel errors

27

and procedure compliance continued to be a source of periodic performance problems.

Improvements were noted in routine license submittals, but .additional management

attention will be necessary to improve the responses to generic communications to the

same level.

111.G.2

Performance Rating: Category 2

111.G.3

SALP Board Comment

The SALP Board noted cyclic performance relative to attention to detail resulting in

personnel errors. The licensee should evaluate the effectiveness of their corrective

action programs to ensure that a higher level of consistent performance is achieved.

28

IV.

SITE ACTIVITIES AND EVALUATION CRITERIA

IV .A

Licensee Activities

Both Salem Units began the SALP period in Hot Standby and preparing for unit startup

following resolution of main steam isolation valve (MSIV) concerns. During Unit 1

startup activities, the reactor automatically tripped on August 17, 1990, after the No. 14

reactor coolant pump (RCP) lost electrical power. The unit was subsequently shutdown

to Cold Shutdown to replace the No. 14 RCP motor. The unit was returned to service

on September 7, 1990, and operated until September 10, 1990, when an automatic reactor trip occurred while preparing to isolate a high pressure turbine sensing line leak.

Power operation resumed on September '12, 1990.

Unit 2 was placed in service on August 20, 1990, and power operation continued until

September 4, 1990, when the unit tripped automatically due to a secondary system

transient caused by equipment failures. Power operation resumed on September 8, 1990.

Unit 1 shutdown on February 9, 1991, for its ninth refueling outage. Core offload was

completed on March 2, 1991, and core reload was completed on March 16, 1991. The

reactor was made critical on April 23, 1991, and full power operation was achieved on

April 29, 1991.

On May 10, 1991, following a 245 day record run for the unit, Unit 2 was shut down for

a scheduled maintenance outage. The unit was restarted and achieved criticality on May

21, 1991, and power ascension followed.

Unit 1 tripped on June 16, 1991, due to a lightning strike on the main transformer. T.he

unit restarted on June 24, 1991.

On September 16, 1991, the licensee initiated a shutdown of Unit 1 due to an unisolable

electro-hydraulic control (EHC) system fluid leak. The unit initially proceeded to Hot

Standby. However, a body to bonnet leak was observed on one of the two pressurizer

spray valves, requiring entry into Cold Shutdown for valve repair. The unit was restarted

on September 25, 1991, and was synchronized to the grid on September 27, 1991.

On October 18, 1991, the licensee began a Unit 2 power reduction from 100% in order

to remove chloride ions from the steam generators. The turbine generator was taken off

line, and a chemical hideout recovery evolution was performed. The licensee initiated

this hideout recovery evolution because of a vendor calculation that concluded the

chloride crevice concentration due to a September 22, 1991, condenser tube failure was

such that the steam generator tubes were subject to accelerated denting over time.

During this power reduction, the unit remained in Mode 2 at 0% power. Final chloride

29

concentration on all steam generators was within the chemistry goal. The unit was

synchronized with the grid on October 20, 1991, and was subsequently returned to full

power.

On November 9, 1991, Salem Unit 2 experienced an automatic main turbine and reactor

trip during performance of turbine mechanical trip testing. The turbine trip subsequently

reset, resulting in overspeeding the turbine and causing significant damage to the

turbine/generator set. The unit proceeded to Cold Shutdown and commenced its sixth

refueling outage, which had previously been scheduled to begin in January 1992.

The licensee continued to experience problems with service water leaks, spurious

radiation monitor alarms and actuations, *and Safeguards Equipment Cabinet failures and

actuations. The licensee continues to pursue both short and long-term solutions to these

issues.

IV.B

NRC Inspection and Review Activities

Four NRC resident inspectors were assigned to Artificial Island during the assessment

period. NRC team inspections were conducted in the following areas:

Emergency Preparedness inspections conducted on October 29 through November

2, 1990, and on December 3 through 6, 1991 to observe the Artificial Island

annual exercises.

Safety System Functional inspection conducted at Salem Units 1 and 2 on April

15 through April 26, 1991, to assess the design basis and operational readiness of

the Residual Heat Removal system.

Augmented inspection Team inspection conducted at Salem Unit 2 on November

10 through December 2, 1991, to review and evaluate the circumstances and

significance of the November 9, 1991 turbine/generator failure event.

IV.C SALP Evaluation Criteria

Licensee performance is assessed in selected functional areas, depending on whether the

facility is in a construction or operational phase. Functional areas normally represent

areas significant to nuclear safety and the environment. Some functional areas may not

be assessed because of little or no licensee activities or lack of meaningful observations

in that area. Special areas may be added to highlight significant observations.

The following evaluation criteria were used, as applicable, to assess each functional area:

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1.

Assurance of quality, including management involvement and control;

2.

Approach to the identification and resolution of technical issues from a safety

standpoint;

3.

Enforcement history;

4.

Operational events (including response to, analysis of, reporting of, and corrective

actions for);

5.

Staffing (including management);

6.

Training and qualification effectiveness;

Based upon the SALP Board assessment, each functional area evaluated is classified into

one of three performance categories. The definitions of these performance categories

are:

Category 1: Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a superior level of performance. NRC will consider

reduced levels of inspection effort.

Category 2: Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a good level of performance. NRC will consider

maintaining normal levels of inspection effort.

Category 3: Licensee management attention to and involvement in nuclear safety or ..

safeguards activities resulted in an acceptable level of performance; however, because of

the NRC's concern that a decrease in performance may approach or reach an

unacceptable level, NRC will consider increased levels of inspection effort.

The SALP report may include an appraisal of the performance trend in a functional area

for use as a predictive indicator. Licensee performance during the assessment period is

examined to determine whether a trend exists. Normally, this performance trend would

be used only if both a definite trend is discernable and continuation of the trend would

result in a change in performance rating.

The trend, is used, is defined as:

Improving: Licensee performance was determined to be improving during the

assessment period.

Declining: Licensee performance was determined to be declining during the assessment

period and the licensee had not taken meaningful steps to address this pattern.

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