ML18096A596

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Initial SALP Rept 50-354/90-99 for 900801-911228
ML18096A596
Person / Time
Site: Salem, Hope Creek  PSEG icon.png
Issue date: 02/27/1992
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18096A593 List:
References
50-354-90-99, NUDOCS 9203310110
Download: ML18096A596 (25)


See also: IR 05000354/1990099

Text

-.

ENCLOSURE 2

INITIAL. SALP REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT NO. 50-354/90-99

PUBLIC SERVICE ELECTRIC AND GAS COMPANY

HOPE CREEK GENERATING STATION

ASSESSMENT PERIOD: AUGUST 1, 1990 - DECEMBER 28, 1991

BOARD MEETING DATE: FEBRUARY 27, 1992

TABLE OF CONTENTS

I.

INTRODUCTION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

II.

SUMMARY OF RESULTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

II.A

Overview . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

II.B

Facility Performance Analysis Summary . . . . . . . . . . . . . . . . . . . . . 4

II.C

Unplanned Shutdowns, Unit Trips and Forced Outages . . . . . . . . . . . .

5

ill

PERFORMANCE ANALYSIS ............ * .... : . . . . . . . . . . . . . . . 7

ill.A Plant Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

ill.B Radiological Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

ill.C Maintenance/Surveillance . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

11

ill.D Emergency Preparedness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

14

ill.E Security . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

15

ill.F Engineering/Technical Support . . . . . . . . . . . . . . . . . . . . . . . . . .

15

ill.G Safety Assessment/Quality Verification . . . . . . . . . . . . . . . . . . . . .

17

IV.

SITE ACTIVITIES AND EVALUATION CRITERIA . . . . . . . . . . . . . . . .

21

N .A Licensee Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

21

N.B NRC Inspection and Review Activities . . . . . . . . . . . . . . . . . . . . .

21

N. C SALP Evaluation Criteria . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

22

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) is an integrated Nuclear

Regulatory Commission (NRC) staff effort to collect observations and data and to

periodically evaluate licensee performance on the basis of this information. The SALP

process is supplemental to normal regulatory processes used to ensure compliance with NRC

rules and regulations. SALP is to be sufficiently diagnostic to provide a rational basis for

allocating NRC resources and to provide meaningful feedback to the licensee's management

to improve the quality and safety of plant operations.

An NRC SALP Board, composed of the staff members listed below, met on February 27,

1992, to review the collection of performance observations and data and to assess the

licensee's performance at the Hope Creek Generating Station. This assessment was

conducted in accordance with the guidance in NRC Manual Chapter 0516, "Systematic

Assessment of Licensee Performance." A summary of the guidance and evaluation criteria is

provided in Section N. C of this report.

This report is the NRC's assessment of the licensee's safety performance at the Hope Creek

Generating Station for the period August 1, 1990 to December 28, 1991.

The SALP Board was composed of:

Chairman:

C. W. Hehl, Director, Division of Reactor Projects (DRP), Region I (RI)

Members:

T. P. Johnson, Senior Resident Inspector, Salem/Hope Creek, RI

S. Dembek, Project Manager (Hope Creek), Office of Nuclear Reactor Regulation (NRR)

C. L. Miller, Director, Project Directorate I-2, NRR

A. R. Blough, Chief, Projects Branch No. 2, DRP, RI

M. W. Hodges, Director, Division of Reactor Safety (DRS), RI

R. W. Cooper, Deputy Director, Division of Radiation Safety and Safeguards (DRSS), RI

Others in Attendance:

J. R. White, Chief, Reactor Projects Section 2A, DRP, RI

H. K. Lathrop, Resident Inspector, Salem/Hope Creek, RI

S. M. Pindale, Resident Inspector, Salem/Hope Creek, RI

B. C. Westreich, Reactor Engineer, DRP, RI

I. B. Moghissi, Reactor Engineer Intern (Salem), NRR

J. C. Stone, Project Manager (Salem), NRR

M. J. Davis, Performance Evaluator, Performance & Quality Evaluation Branch, NRR

L. S. Cheung, Senior Reactor Engineer, Electrical Section, DRS, RI

2

Others in Attendance (continued)

R. J. Paolino, Lead Reactor Engineer, Electrical Section, DRS, RI

D. L. Caphton, Senior Technical Reviewer, DRS, RI

W. J. Pasciak, Chief, Facilities Radiation Protection Section, (FRPS), DRSS, RI

R. L. Nimitz, Senior Radiation Specialist, FRPS, DRSS, RI

J. C. Jang, Senior Radiation Specialist, Effluents Radiation Protection Section, DRSS, RI

C. Z. Gordon, Senior Emergency Preparedness (EP) Specialist, EP Section, DRSS, RI

D. F. Limroth, Senior Reactor Engineer, Safeguards Section, DRSS, RI

3

II.

SUMMARY OF RESULTS

II.A

Overview

PSE&G operated the Hope Creek reactor in a manner that demonstrated a high level of

nuclear safety, and exhibited a safety conscious attitude. Strong licensee management

involvement and oversight were evident, and conservatism was displayed in most functional

areas. Strong performance was also noted during Hope Creek's third refueling outage. Self-

assessment, corrective action and root cause analysis programs were maintained at a strong

and effective level. As a result, plant operations, radiolOgical controls, emergency

preparedness, security, and safety assessment/quality verification (SA/QV) maintained a

superior level of performance. However, relative to SA/QV, the SALP Board did express

some reservation due to instances of management inattention and poor communications that

affected the quality of licensee response to certain generic issues (motor operated valves and

station blackout rule). Personnel errors continued to persist in nearly all functional areas,

but appeared to be on the decline.

Licensee attention to the maintenance/surveillance area has resulted in some improvement.

However, a Category 2 with an improving trend was once again assigned. The SALP Board

determined that performance deficiencies in the maintenance/ surveillance area and

shortcomings associated with spare parts/material procurement prevented this functional area

from fully achieving anticipated improvements.

The level of performance in the engineering/technical support area declined during this

assessment period. Significant weaknesses were noted relative to engineering's development

and response to the motor operated valve program. This was indicative of a lack of

management involvement and oversight, and miscommunication and poor attention to detail

on the part of engineering personnel. Additional weaknesses were noted relative to other ..

engineering support activities. While these deficiencies existed, some improvements have

been made in spare parts availability and material procurement. Plant operations and

maintenance were well supported by the onsite and corporate engineering staffs. Corrective

actions for engineering-related deficiencies were generally timely and effective.

Overall, individual performance and supervisory involvement in the field was very good,

though some personnel errors were apparent in most functional areas. Personnel errors also

contributed to reactor trips, but effective management attention appears to be producing an

improving trend as evidenced by performance at the end of this SALP period.

...

4

11.B

Facility Performance Analysis Summary

1.

2.

3.

4.

5.

6.

7.

Functional

Area

Plant Operations

Radiological Controls

Maintenance/

Surveillance

Emergency

Preparedness

Security

Engineering/

Technical Support

Safety Assessment/

Quality Verification

Previous Assessment Period:

Rating, Trend

Last Period

1

1

2, Improving

1

1

1

1

Rating, Trend

This Period

1

1

2, Improving

1

1

2

1

May 1, 1989 through July 31, '1990

Present Assessment Period: August 1, 1990 through December 28, 1991

~' .

5

11.C

Unplanned Shutdowns, Unit Trips and Forced Outages

1.

11/4/90

Power Level Root Cause

100%

Personnel error/

Design

Functional Area

  • Maintenance/

Surveillance

The reactor scrammed from high power due to the closure of one main steam isolation valve

(MSIV) when the MSIV' s instrument gas line sheared at the instrument block. The gas line

had been improperly connected after valve maintenance. This combined with a poor design

resulted in vibration induced fatigue cracking of the line and MSIV closure.

2.

11/17/90

100%

Component failure/

Safety Assessment/

incomplete root

Quality Verification

cause

The reactor scrammed following a main turbine trip due to high moisture separator level

during surveillance testing of the combined intermediate valves. Licensee root cause analysis

for a similar trip occurring on January 6, 1990, was incomplete. A failed check valve on the

normal drain line allowed backflow to the moisture separator during testing.

3.

2/19/91

24%

Component failure

NI A

The reactor scrammed on lbw water level during startup when the feedwater level control

valve failed closed. A relay in the control circuitry failed, closing the startup level control

valve. Level decreased to the scram setpoint before operators could respond to the

condition.

4.

2/23/91

24%

Component failure/

NI A

incomplete vendor

information

An unplanned shutdown occurred due to hydrogen leakage from the main generator. Vendor

modifications to the No. 9 hydrogen seal were not communicated to the licensee. Once

installed, the seal failed.

\\

5.

5/7/91

100%

6

Personnel error/

Design

Maintenance/

Surveillance

The reactor scrammed on low water level during surveillance testing of the f eedwater level

control (FWLC) system by a maintenance I&C technician. A personnel error due to lack of

attention to detail caused the FWLC to sense a false high level resulting in reactor feedwater

pump response to lower actual level. A contributing cause was design of cabinet such that

leads had to be lifted inside. The licensee had previously identified this issue and had

initiated a design change; however, it had not been completed prior to the scram.

l.

7

ill

PERFORMANCE ANALYSIS

ill.A Plant Operations

III.A. I

Analysis

The previous SALP rated Hope-Creek operations as Category 1. That assessment concluded

that the Hope Creek reactor was operated skillfully and in a safety conscious manner.

Reactor operator error contributed to one of four reactor scrams. Strong management and

supervisory oversight and involvement occurred at all levels from the senior reactor operator

through the station general manager. An aggressive approach by management was effective

in reducing the number of personnel errors: Senior reactor operator failure rate during

licensing and requalification exams was higher than normal.

During this assessment period, the reactor was operated in a manner that demonstrated a

nuclear safety conscious attitude. Operators competently performed their duties during unit

startups, shutdowns and transients. There were four reactor scrams during the period, but

none were the result of operator error. Operator response to reactor scrams and plant

transients was commendable. In several instances, prompt actions by operators minimized

plant transients and averted the necessity for reactor scrams due to a lightning strike event, a

runback of the recirculation pumps event, and reactor feedwater and condensate pump trips.

The five operating shifts are effectively staffed as each has three Senior Reactor Operator

(SRO) and three Reactor Operator (RO) licensed individuals (one above Technical

Specification requirements). Two separate SRO licensed individuals supervise the work

control group during regular hours. There are a total of 41 licensed operators, including 31

on shift, and 10 in staff and training positions.

The licensed reactor operator training programs for Hope Creek were well developed,

implemented, and strongly supported by management. Licensed operator initial and

requalification examinations have shown that candidates were well prepared. Increased

management attention was effective in reducing exam failures. As a result, the candidates

performed well during examinations. Facilities used for training were excellent. During

examinations, the operators exhibited good administrative knowledge, good knowledge of and

familiarity with plant systems and components, good understanding and interpretation of

annunciators and alarm signals, and the ability to quickly and accurately diagnose the events

or conditions based on signals or other instrument readings. However, results of an initial

examination near the end of the period indicated a higher than expected number of candidate

failures. Non-licensed operator training was found to be performed well.

Strong plant management oversight and attention to operations were evident on a daily basis.

An operational perspective of plant problems and work prioritization was well understood

  • .

8

and was enhanced by daily meetings. Examples included scram followup, actions associated

with a fuel pin leak, and the identification and diagnosis of increasing drywell unidentified

leak rate.

Licensed operators' plant awareness, safety perspective, and professional control room

demeanor were consistently evident. Plant operations were well supported by detailed

procedures.

Procedural adherence was very good. Shift turnovers were formal and

included thorough briefings of the relief crew. Control room access was controlled, and

activities were limited to those directly related to plant operations. Aggressive management

attention has resulted in significant reductions in the number of lit annunciators. The use of

overtime was properly controlled. Good performance of non-licensed equipment operators

was noted during observations made on plant tours, and during equipment testing and

operation. The licensee was successful in keeping operations department personnel errors

low. This was particularly evident during the refueling outage.

Overall, the licensee's implementation of the Emergency Operating Procedure (BOP)

program has functioned well. EOPs have been improved with technical adequacy issues

being satisfactorily resolved. Implementation of the current EOPs has been performed in a

thorough manner. Continued BOP administrative improvements are in process.

A higher than expected number of automatic scrams has continued for several years. The

licensee was very concerned about these scrams and embarked on an independent,

comprehensive scram review in order to identify common causal factors and establish

corrective actions. This review was thorough. Short term results appeared to be successful

as the unit operated continually for seven and one-half months at the end of the period. Two

scrams occurred in 1991.

Plant housekeeping has continued to improve during the period. Plant area painting, the ..

assignment of housekeeping area responsibilities, and management focus and attention have

been effective in achieving this level of housekeeping.

The overall fire protection program was effective. Dedicated fire protection personnel

performed well and were knowledgeable, which demonstrated an effective training program.

The fire brigade was staffed by the Site Protection group personnel, which minimized the

reliance on operators to respond to fire and first aid emergencies. Appropriate operator

involvement and interface in fire emergencies were provided. Overall, plant and site

management aggressively supported the fire protection program.

Hope Creek conducted its third refueling outage during the period. Outage preparations

were excellent. The licensee employed many lessons learned from the previous post

refueling outage critique, resulting in an effectively conducted outage, despite significant

emergent work. Refueling activities, including reactor core offload, the subsequent reload,

..

9

and fuel sipping, were effectively controlled. The unit was returned to service from its third

refueling outage in a safe and effective manner. Pre-startup activities, unit startup and power

ascension were well planned and executed.

Summary

The Hope Creek reactor was operated conservatively with nuclear safety as the top priority.

Operator errors remained low; however, unplanned automatic reactor scrams continued to be

a concern. Strong management and supervisory oversight of and involvement in operations

were evident. The licensee conducted its third refueling outage effectively. An effective

training program was noted as evidenced by exam results and operator performance during

routine and transient events. However, pobr performance was noted during an initial exam

given at the end of the period.

ill.A.2

Performance Rating: Category 1

ID.B Radiological Controls

ill.B.1

Analysis

The previous SALP report rated radiological controls as Category 1. , Program strengths

included: good management involvement, effective internal review processes such as quality

assurance audits and surveillances, good resolution of technical issues, and good staffing

levels. No weaknesses were noted.

During the current assessment period, the level of management involvement was excellent.

Managers actively observed ongoing work activities, identified problems were effectively"

corrected using the formal Radiological Occurrence Reporting system, and internal self-

assessments, audits and surveillances continued to be used effectively to assure quality in the

Hope Creek radiological control programs.

The level and quality of staffing in the area of radiation protection (RP) remained high

throughout this period. A new, appropriately qualified Radiation Protection Manager (RPM)

was .appointed during this assessment period, and the level and quality of staffing of RP

technicians continued to be excellent. Although RP technicians met appropriate qualification

requirements, there was a need to clearly define types of work experience acceptable for RP

technician qualification purposes.

The RP training program continued to be excellent. For example, RP supervisors received

annual continuing training which included systems training; nuclear codes, standards, and

regulatory concerns; and root cause analysis. The RP technician continuing training also

10

remained excellent, and included plant systems training. An area for improvement was the

system training programs, which contained little on expected radiological conditions expected

during various system operating modes.

The licensee implemented an aggressive ALARA program. Excellent exposure reduction

efforts were undertaken during the refueling outage. For example, an elaborate automated

system for removal, maintenance and re-installation of the control rod drive mechanisms was

used. In addition, audio/visual and remote reading dosimetry were effectively utilized to

control work under the vessel to reduce unnecessary personnel exposure. The licensee was

sensitive to any opportunity to reduce personnel exposure, as evidenced by removal of a

carbon steel reactor water clean-up line located in the overhead of a Reactor Building

corridor. The line exhibited contact dose rates of 800 mR/hr and required shielding to allow

personnel free access to the corridor. Licensee efforts to reduce personnel radiation

exposure during surveillance and in-service inspection (ISI) activities continued to be

effective as evidenced by excellent water chemistry control and the use of zinc injection.

Overall control of work in -radiologically controlled areas typically was excellent.

Late in the period, an evaluation of the on-site dosimetry processing laboratory by personnel

from the National Voluntary Laboratory Accreditation Program (NVLAP) identified a

number of significant weaknesses in the management of the PSE&G processing laboratory.

The licensee immediately suspended processing of dosimeters and implemented extensive

corrective actions to improve processing. NRC reviews at the end of the period indicated

corrective actions were on-going and dosimetry system performance met applicable

performance standards. The NRC's review of this matter found that the weaknesses

  • stemmed from the loss of key supervisory and management personnel and a lack of

understanding, by replacement personnel, of regulatory aspects associated with maintaining

an accredited personnel dosimetry program. Although no decrease in the quality of

dosimetry processing information was identified, this matter indicated weak understanding of

program and personnel qualification requirements by management.

The solid radwaste/transportation program continued to be strong. The organization and

staffing exhibited stability and strength. The unique asphalt solidification system continued

to operate well, and the on-site storage of radwaste was minimal. The quality oversight of

radwaste processing was of good technical depth and scope, with an appropriate level of

surveillance of the various radioactive material shipments. For example, QC surveillances .

identified calculational errors, in some radioactive shipments, that were corrected

immediately. The licensee's training program continued to provide excellent radwaste and

transportation content.

The licensee continued to conduct an effective Radiological Environmental Monitoring

Program (REMP). The meteorological monitoring program was sufficient in ensuring that

meteorological instruments were operable, maintained, and calibrated. Furthermore, the

meteorological data were obtainable from various locations on and off site. An effective QC

program was in place to assure the quality of REMP sample analyses. The audits performed

...

11

by the Quality Assurance Department were thorough and of technical depth to assess the

REMP.

The licensee continued to conduct excellent radioactive liquid and gaseous effluent control

programs. Outstanding calibration techniques for effluent/process radiation monitoring

systems were employed. The Nuclear Training Department conducted an excellent training

program for Chemistry/Radiation Protection technicians who were actually performing

effluent processes.

The licensee summarized and reported historical radioactive liquid and gaseous release data

since the start of commercial operations for trending purposes in its semiannual report. Such

reporting was a noteworthy licensee initiative.

Late in the period, the licensee identified low level contamination in the on-site sewage

system. The licensee isolated the contaminated sewage and implemented appropriate

corrective actions to preclude recurrence, reflecting an excellent understanding of this

technical issue. Air cleaning systems were well maintained and tested.

Summary

PSE&G continued to maintain and implement an effective radiological controls program.

Managers effectively controlled radiological work. Staffing levels continued to be excellent.

The ALARA program continued to demonstrate management's commitmentto reducing

personnel exposure and maintaining a low source term within the plant. The licensee

implemented an effective environmental and effluent controls program as well as an effective

radwaste processing, handling and shipping program.

III.B.2

Performance Rating: Category 1

ill.C Maintenance/Surveillance

III.C.l

Analysis

The last SALP rated the Hope Creek maintenance/surveillance functional area as a Category.

2, improving. That assessment concluded that the station had successful maintenance and

surveillance programs which were adequately scheduled, planned and implemented. Program

strengths included effective management, a well-trained and experienced work force and

good procedures. Weaknesses were noted in the procurement process and post-maintenance

system restoration. Personnel errors continued to contribute to noted plant events and

scrams.

..

12

Maintenance:

The Hope Creek maintenance program was well planned, staffed and organized, and

demonstrated strong performance in this area, including improved adherence to procedures

and appropriate oversight of maintenance activities. Management at all levels was noted to .. *.

be directly and intimately involved in the maintenance program. During the period, the

licensee implemented the use of fixed shift work coverage, leveling work activity impact and

improving scheduling efficiency and accuracy. Pre-outage system walkdowns were initiated

to improve outage efficiency. Planned maintenance outages of safety-related equipment were

screened by plant management to assure that a net safety benefit was provided. These

initiatives have been effective and were positive indicators of management's safety-conscious

and detailed control of plant maintenance. *Safety-related equipment availability was high, as

indicated by the licensee's trending data.

The most significant strength of the maintenance organization continued to be its stable and

well-trained staff. Maintenance training received strong management support, with the

training center providing extensive electrical and mechanical training facilities. Line

supervision provided good work direction. . Adherence to procedures and attention to detail

continued to improve, as evidenced by a reduced amount of rework and fewer personnel

errors. However, a small number of instances were noted where attention to detail was

poor. For example, a number of minor post maintenance material deficiencies existed on the

standby liquid control system, and required preventive maintenance was not performed on a

spare core spray pump motor after rewinding. Overall, the maintenance staff was very

knowledgeable in their respective areas of responsibility.

Management dedicated additional resources to address weaknesses noted in maintenance

support activities. The material and procurement groups were reorganized and placed under

the direction of a general manager. A new warehouse, into which central receiving and the

numerous on-site storage areas would be consolidated, was completed late in the period.

Maintenance facilities were generally well equipped, maintained and controlled. Material

control was enhanced by the implementation of the computerized warehouse automated

material management system (WAMMS). However, spare parts availability and

obsolescence continued to impact the timeliness of some maintenance activities. The number

of delayed routine maintenance requests due to parts problems decreased over the period.

During the assessment period, Hope Creek completed one refueling outage and conducted

several forced outages. Maintenance planning and outage organizations were noted strengths

during the third refueling outage from December 1990 to February 1991. Virtually all pre-

planned activities were completed with less than two percent rework, an indication that

management had effectively communicated their expectations regarding attention to detail and

work performance quality. Significant emergent work on the recirculation system piping

welds was completed with no adverse impact on the overall outage. Control rod drive

maintenance activities and forced outage repairs to a leaking hydrogen seal on the main

generator in late February 1991 were well-planned and executed. In general, station

".

13

housekeeping was very good. However, instances were noted where post-maintenance

system restoration and cleanup were poor. Management was aggressive in addressing these

issues and improvements in these areas were noted in the latter half of the period.

Maintenance contributed to one of four scrams during the period. In November 1990, the

reactor scrammed after a main steam isolation valve closed when its instrument gas line

sheared at the instrument block. This line had been incorrectly reinstalled following

maintenance during a previous assessment period. However, the design of the gas supply

lines and their susceptibility to vibration were also causal factors.

Notwithstanding the minor weaknesses identified in this area, the licensee has managed and

performed a large number of maintenance activities in an effective and safety conscious

manner.

Surveillance:

The Hope Creek surveillance program was effectively and conservatively managed and

implemented throughout the assessment period. Surveillance tests were effectively scheduled ..

and tracked through the managed maintenance information system (MMIS), which

coordinated the performance of the affected departments. The cooperative interaction of the

groups involved continued as a strength in the surveillance program.

Surveillance procedures were well written, accurate and complete. Procedural enhancements

were made in a timely manner, however, a weakness was identified in the procedure revision

process where needed changes were not always incorporated in all related procedures. The

licensee had implemented a policy whereby most surveillance activities which affected safety

system redundancy or initiation were performed on the night shift, but only between the

months of May and September when electrical load demands were high. During this

assessment period, that policy was extended to a year-round basis. As a complement to the

fixed shift work schedule, this policy contributed significantly to reducing stress levels in the

control room and to reduction in the number of late or missed surveillances.

The number of surveillance related incidents, while still high, continued to decrease from the

two previous assessment periods. Corrective actions taken to reduce personnel errors, the

predominant cause of such incidents, have been generally effective, particularly during the .

second half of this period: For example, the introduction of plastic spring clips to assist in

properly locating and identifying relay contacts, terminal strip points and cabling in mid 1991

aided in reducing the misidentification of components. No such events occurred during the

latter part of the period. Additionally, there were no missed maintenance or I&C

surveillances during 1991. While one scram occurring during this period was attributed to

personnel error during surveillance testing of the feedwater level control system, an

inadequate cabinet design contributed to the event. The licensee had addressed the issue of

cabinet scram sensitivity, but the appropriate design modification, to install external test

boxes, had not yet been implemented for this particular cabinet.

14.

The inservice inspection (ISi) program at Hope Creek continued to be well planned and

implemented. Licensee personnel involved in the program were noted to be knowledgeable

and thorough in the performance of their inspection activities including ultrasonic testing of

intragranular stress corrosion cracking (IGSCC) susceptible piping. In particular, the

licensee's investigation into indications discovered in recirculation piping welds during the -

third refueling outage, including the development of an enhanced testing technique, and the

resultant corrective actions, were commendable. The licensee had implemented an effective

program, based on industry standards, to assess erosion/corrosion in various plant

components and piping. No significant thinning was detected in over eighty areas inspected

during the third refueling outage.

Summary

The Hope Creek station has continued implementation of successful and effective

maintenance and surveillance programs. These programs have been well scheduled, planned

and managed. Program strengths included management involvement, a stable and well-

trained staff and well-written procedures.

Management efforts have been successful in

reducing the number of personnel error related events. Weaknesses included. occasional

lapses in attention to detail, material procurement, and continued, albeit reduced, personnel

error initiated plant events.

III.C.2

Performance Rating: Category 2

Trend: Improving

III.C.3

SALP Board Comment

While progress has been made on resolving a number of issues in this area, the Board noted

the continuing number of.personnel errors, especially in the surveillance area, and persistent

spare-parts related backlogs were issues requiring continued close management attention.

ID.D Emergency Preparedness

III.D.1

Analysis

The Emergency Preparedness for Artificial Island covers both Hope Creek and Salem

Generating Stations, therefore the assessment of emergency preparedness is a combined

evaluation.

III.D.2

Performance Rating: Category 1

15

ID.E Security

III.E.1

Analysis

The Security Plan for Artificial Island covers both Hope Creek and Salem Generating .

Stations, therefore the assessment of security is a combined evaluation.

III.E.2

Performance Rating: Category 1

ID.F Engineering/Technical Support

III.F.l

Analysis

The previous SALP rated Engineering and Technical Support as Category 1. The previous

assessment indicated that improvements in the performance of corporate engineering were

observed. The overall experience levels within the onsite system engineering group were

also improved. No significant weaknesses were observed during the last SALP period.

Engineering and Technical Support for Hope Creek was provided by corporate engineering,

lmown as Engineering and Plant Betterment (E&PB), and the onsite system engineering

group. E&PB handled major engineering efforts such as plant modifications, and design

bases reconstitution. The onsite system engineering group supported operations,

maintenance, testing and minor design change activities. E&PB is well staffed with

experienced personnel in various engineering disciplines.

The onsite system engineering group was well staffed with experienced and knowledgeable

personnel. The licensee continued to implement their pipeline program to train new system

engineers. Most system engineers have received formal root cause training. Evidence of

good system engineer support for station activities and a good safety perspective include:

(1) identification and followup of an ultimate heat sink related design deficiency;

(2) maintenance trending; (3) disposition for degraded equipment; (4) procedure generation;

(5) identification of and corrective actions for control rod scram time calculation errors; and

(6) disposition of reactor recirculation instrument line leakage.

The licensee has been generally aggressive in identifying and following up on engineering

related deficiencies. The corrective actions taken as a result of a recirculation system pipe

weld crack is a good example. The corrective actions involved state-of-the-art equipment

and techniques and the use of recognized industry experts for analysis. These actions, along

with a metallurgical analysis of samples obtained from the cracked welds effectively resolved

the problems and surpassed ASME Section XI Code requirements. In contrast, the licensee

was slow to properly identify the root cause and implement appropriate corrective actions

after a filtration, recirculation and ventilation system (FRVS) heater fuse failure.*

16

Technical support for refueling and maintenance outage periods, and for post outage recovery

activities was noted to be effective. Both E&PB and onsite system engineering participated

in and interfaced with the outage organization on a daily basis. The system engineering

group provided strong support during reactor startup and power ascension testing.

On schedule progress was observed in the Hope Creek Configuration Baseline Documents

(CBD) project. The CBD project involves the design basis reconstitution of 146 systems and

structures for Hope Creek. Twenty four systems were completed during this SALP period.

The CBD project has delivered quality products. The licensee also implemented the

computerized Document Information Management System (DIMS) to complement the hard

copy CBD for the completed sy~tems.

E&PB worked well with onsite system engineering. The establishment of an E&PB small

design change project group, coupled with an effective plant modification design change

process, has been effective in reducing the system engineering group workload. This has

resulted in increased system engineering presence in the field. However, significant

weaknesses were found in engineering's development of the safety related motor operated

valve (MOY) program in response to Generic Letter 89-10. Several recommended actions of

the generic letter were not properly addressed. For example, due to a lack of management

attention and poor communications, the development of a program to address safety related

MOYs was slow and well behind the committed schedule; switch setpoint values for safety

related MOYs were not properly communicated to the maintenance department from the

engineering department, and the switches were set improperly; and known industry issues,

such as diagnostics inaccuracies, differential pressure testing, trending of failures, and

periodic verification of MOY capability were not adequately addressed in the program.

Improvements were noted in the engineering procurement activities. Until 1990, the licensee

had no formal procedure for controlling the commercial grade item dedication program. The

Hope Creek program was based on the EPRI guidelines, was fully implemented, and worked

very well. However, spare parts deficiencies, involving documentation and planning,

continued, including: (1) inadequate supply of replacement parts resulting in the seismic

monitoring system being out of service during a seismic event; and (2) environmental

qualification inadequacies for nuclear instrumentation system detector connectors.

Engineering's Self-Assessment Program emphasized the key performance elements to the

engineering and management personnel. By setting goals and tracking them and by having

upper management support, significant improvements have been achieved in the areas of

overdue item reduction, safety evaluation quality and design change progress timeliness.

  • The submittals and supporting analyses for license amendment requests were generally well

written and technically sound with one exception; the incorrect classification of the

suppression pool water temperature instruments (Category 1 vs. Category 2). The need for

NRC additional information requests was infrequent. However, Hope Creek responses to

,,_

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17

generic issues were in some cases incomplete or inadequate. For example, the Hope Creek

responses to the Station Blackout Rule (SBR) were determined to be incomplete.

Conclusions that Hope Creek complies with the SBR could not be drawn from the licensee's

submittals. As discussed above, the response to GL 89-10 and its supplements was inferior.

Summary

Hope Creek has been aggressive in identifying and following up on engineering related

deficiencies. The corrective actions taken as a result of the recirculation system pipe weld

crack is a good example. Significant weaknesses in the development of the safety related

MOY program were observed. Weaknesses were also observed in Hope Creek responses to

the Station Blackout Rule, in the initial root cause evaluation associated with the FRVS

heater fuse failures, and in responses to the NRC regarding Generic Letters. Despite these

weaknesses, E&PB and onsite system engineering worked well in providing technical support

to the plant. Improvement in the engineering procurement program was observed however,

some minor problems were noted relative to documentation and planning.

III.F.2

Performance Rating: Category 2

III.F.3

SALP Board Comment

There was a distinct difference in quality between the licensee's responses to generic issues

and its other submittals. The licensee should pay particular attention to improving the

overall quality of its responses to generic issues.

ill.G Safety Assessment/Quality Verification

III.G.l

Analysis

The previous SALP rated Safety Assessment/Quality Verification (SA/QV) as Category 1.

The Hope Creek licensee was commended for having a well run, safety conscious

organization. Management was noted as being involved with the plant on a daily basis, and

for making its safety conscious attitude known throughout the plant. The licensee effectively

identified problem areas and ensured prompt and effective corrective actions. However,

isolated personnel errors continued to be an area meriting additional management attention.

Throughout this period, individual performance was very good. Direct supervision at the site

by first and second line supervisors and comprehensive management oversight of station

activities were strengths. However, personnel errors continued in all functional areas.

Additionally, four automatic scrams from power occurred during this SALP period, including

one attributed to the SA/QV area. The scram attributed to SA/QV was a repeat reactor

scram due to a moisture separator high level induced turbine trip. The licensee review of an

identical scram, in January 1990, did not completely identify all of the causal factors of the

,*

.....

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event. Otherwise, licensee actions to determine root causes of personnel errors and scram

rates were thorough and aggressive. An independent root cause analysis of the twelve*

  • scrams occurring since August 1988 was performed. Management endorsed the report's

findings and implemented a wide range of corrective measures based on the report's

recommendations. No scrams occurred during the second half of the assessment period.

Another exception to this good personnel performance was when chemistry, training and

emergency preparedness personnel failed to adequately follow procedures associated with

post accident sampling system (PASS) operations. Consequently, deficient conditions

involving the operability of the PASS were not documented or corrected promptly.

As mentioned in the Engineering/Technical Support section of this report, the licensee's

amendment and relief requests were generally of high quality, technically sound and

complete. The staff rarely required additional information to evaluate the licensee's

proposal. Although the licensee's amendment requests were generally technically well

written, there have been numerous administrative errors in their submittals during this SALP

period. Two NRC Regional Waivers of Compliance were processed during this SALP

period. One licensee submittal was well written and demonstrated good engineering

practices. However, weaknesses were identified in a second submittal concerning the

replacement of a safety auxiliaries cooling system pump casing relative to the completeness

of the technical information and the safety basis determination. This occurred early in the

period. Additionally, as previously noted in the Engineering/Technical Support section, the

licensee's responses to NRC GL 89-10 Supplement 3 and the Station Blackout Rule were not

technically adequate.

As discussed in the engineering/technical support section, Engineering and Plant Betterment

(E&PB) generally performed well. However, one major exception was a lack of

management attention and oversight regarding the motor operated valve (MOV) program.

Poor communications among plant maintenance, licensing and E&PB personnel were

contributing factors in this poor performance.

The Station Operations Review Committee (SORC) provided consistent and effective review

of significant plant issues, including design changes, post-scram reviews and reportable

events. Following repeated multiple failures of the filtration, recirculation and ventilation

system (FRVS) heater fuses in May and July, 1991, the SORC met on several occasions to

perform an in-depth review of the root causes, safety implications and proposed corrective

actions. While the licensee was not aggressive in its response to the May 1991 fuse problem,

actions taken following the July 1991 event were thorough.and effective.

The licensee's major event review process, the Significant Event Response Team (SERT),

was effective during this period. In addition to the comprehensive scram review, a review of

the November 1990 high moisture separator level scram led to significant enhancements in

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turbine control valve surveillance testing. Recommendations generated from SERT reviews

were promptly acted upon by management and tracked in the licensee's Action Tracking

System.

The Safety Review Group (SRG) and Station Quality Assurance (SQA) have demonstrated

effective independent reviews of Hope Creek issues. For example, SRG performed a

detailed and effective review of the safety evaluation process. SQA performed a thorough

review of personnel errors and recommended effective corrective actions. Both the SRG and

SQA provided assistance to all SERT efforts, and SRG led and managed the detailed scram

review effort.

The licensee generally took aggressive action to review its reportable events. Licensee Event '

Reports (LERs) were well written and accurate. A large number of the LERs submitted

during this SALP period listed a previous occurrence of a similar reported event (e.g., FRVS

fan automatic starts).

Hope Creek conducted its third refueling outage during the period. Outage preparations

were excellent. The licensee employed many lessons learned from the previous post

refueling outage critique, which resulted in outage completion essentially as scheduled despite

significant emergent work. SQA was effective during all phases of the outage, performing a

large number of performance based surveillance and hold point activities. The continuous

24-hour day coverage provided by SQA was a noted strength, as was management

involvement during all phases of the outage. PSE&G instituted an incentive plan involving

both Hope Creek and Salem personnel in order to increase the focus on plant safety, job

quality and attention to detail. Overall outage performance was very good and no safety

significant concerns were identified.

-

Hope Creek station management, including the General Manager and department heads,

provided effective and safety conscious oversight of station activities on a daily basis. This

was evidenced in daily meetings with the senior nuclear shift supervision and operating crew

and in management accountability meetings. In addition, the General Manager conducted

effective State-of-the-Station meetings twice a year. Corporate management was highly

visible relative to Hope Creek station activities. Operations personnel exhibited a

professional and questioning attitude during the performance of the their duties. A good

safety perspective was noted involving the discovery, evaluation and actions taken when

drywell unidentified leakage significantly increased in September 1990.

Summary

Hope Creek continued to be a well run, safety conscious facility. The licensee's

management of the third refueling outage was a noteworthy strength. The licensee

effectively identified problem areas, and ensured prompt and effective corrective actions.

Individual performance was very good; however, isolated personnel errors continued to be an

-area meriting additional attention. Lack of management attention and poor interdepartmental

20

communications resulted in an inadequate response to the motor operated valve program.

Safety review committees and quality assurance groups provided effective and independent

oversight of activities.

III.G.2

Performance Rating: Category 1

III.G.3

SALP Board Comment

While the Board considered that the licensee, overall, continued to achieve excellent

performance in this area, isolated instances of management inattention and poor

communication contributed to the insufficient quality of PSE&G's responses to generic

communications pertaining to motor operated valves and the station black-out rule. As

expressed in ill.F.3, prompt management attention to this area should prevent performance

decline.

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IV.

SITE ACTIVITIES AND EVALUATION CRITERIA

IV .A Licensee Activities

The Hope Creek unit began the SALP period operating at full power. The unit automatically

scrammed on November 4, 1990, when one main steam isolation valve inadvertently closed

at full power due to a rupture of the primary containment instrument gas line. The unit then

proceeded to cold shutdown to perform maintenance and followup activities for the reactor

scram.

The unit was restarted on November 14, 1990, and the turbine generator was synchronized

on November 15, 1990. On November 17~ 1990, the unit automatically scrammed from

100% power due to a main turbine trip during valve testing. The unit was restarted on

November 18, 1990.

The unit was shutdown on December 26, 1990, to commence the third refueling outage. The

unit restarted from the refueling outage on February 16, 1991. A reactor scram on reactor

water low level from 24% power occurred on February 19, 1991. The unit restarted on

February 21, 1991; however, a shutdown due to excessive generator hydrogen leakage was

performed on February 23, 1991. Restart from this forced outage occurred on March 2,

1991.

On May 7, 1991, the unit automatically scrammed from 100% power due to low water level

caused by a feedwater control malfunction. The unit restarted on May 11, 1991.

Small power reductions were performed throughout the period to perform maintenance and

testing activities. At the end of the SALP period, the unit had operated continuously for 231

days.

IV .B NRC Inspection and Review Activities

Four NRC resident inspectors were assigned to Artificial Island during the assessment

period. NRC team inspections were conducted in the following areas:

Emergency Preparedness Inspection conducted on October 29 through November 2,

1990, to observe the Artificial Island annual exercise.

Training programs team inspection at the Nuclear Training Center on April 1 through

5, 1991.

Motor Operated Valve Inspection conducted at Hope Creek on July 15 through July

19, 1991, to assess licensee response to Generic Letter 89-10.

  • ~;

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IV .C SALP Evaluation Criteria

Licensee performance is assessed in selected functional areas, depending on whether the

facility is in a construction or operational phase. Functional areas normally represent areas

significant to nuclear safety and the environment. Some functional areas may not be assessed

because of little or no licensee activities or lack of meaningful observations in that area.

Special areas may be added to highlight significant observations.

The following evaluation criteria were used, as applicable, to assess each functional area:

1.

Assurance of quality, including management involvement and control;

2.

Approach to the identification and resolution of technical issues from a safety

standpoint;

3.

1Enforcement history;

4.

Operational events (including response to, analysis of, reporting of, and corrective

actions for);

5.

Staffing (including management);

6.

Training and qualification effectiveness;

Based upon the SALP Board assessment, each functional area evaluated is classified into one

  • of three performance categories. The definitions of these performance categories are:

Category 1: Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a superior level of performance. NRC will consider reduced

levels of inspection effort.

Category 2: Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a good level of performance.

NRC will consider

maintaining normal levels of inspection effort.

Category 3: Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in an acceptable level of performance; however, because of the

NRC's concern that a decrease in performance may approach or reach an unacceptable level,

NRC will consider increased levels of inspection effort.

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The SALP report may include an appraisal of the performance trend in a functional area for

use as a predictive indicator. Licensee performance during the assessment period is

examined to determine whether a trend exists. Normally, this performance trend would only

be used if both a definite trend is discernable and continuation of the trend would result in a

change in performance rating.

The trend, is used, is defined as:

Improving: Licensee performance was determined to be improving during the assessment

period.

Declining: Licensee performance was determined to be declining during the assessment

period and the licensee had not taken meaningful steps to address this pattern.