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Category:GENERAL EXTERNAL TECHNICAL REPORTS
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Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
C.D.I. Tech Note No. 82-29 VALVE DYNAMIC MODEL PERFORMANCE SIMULATION FOR THE SALEM PWR PLANT (UNIT ONE)
REVISION 0 Prepared by Arthur M. Hecht Continuum Dynamics, Inc.
P.O. Box 3073 Princeton, New Jersey 08540 Prepared for Public Service Electric and Gas Company of New Jersey 80 Park Plaza Newark, New Jersey 07101 Under Purchase Order No. E218736 Approved by Alan J. Bilanin September 1982
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CONTENTS
- Section 1 INTRO DUCT ION Page 1
2 VALVE DYNAMIC MODEL SIMULATION 2 3 BACK PRESSURE ANALYSIS 10 4 CON CL US IONS 15 5 REFERENCES 16
SUMMARY
- A simulation of valve performance using the EPRI/Continuum Dynamics, Inc. valve dynamic model code is made for high quality steam flow for the New Jersey Public Service Electric and Gas Company's Salem PWR Plant, Unit One. The Crosby 6M6 safety valve is predicted to perform stably for upper adjusting ring settings of -190 and -250 notches, both for a lower ring setting of -18 notches. Due to present code limitations flow of loop seal water is neglected. However, code update to include discharge of loop seal water is near completion.
Using the Continuum Dynamics, Inc. 1 s quasi-steady back pressure computer program, a set of back pressure calculations for the Salem Plant, Unit One was carried out for all relief and safety valves open. The back pressure for the lPR-3, lPR-4 and lPR-5 safety valves are predicted to be 635 psia, 688 psia and 616 psia, respectively, for steam initially saturated at 2500 psia and unit quality.
The effort was supported by the New Jersey Public Service Electric and Gas Company under Purchase Order No. E218736 .
- 1. INTRODUCTION At the request of Public Service Electric and Gas Company of New Jersey (PSE&G), Continuum Dynamics, Inc. (C.D.I.) has simulated the performance of the Salem PWR Plant, Unit One safety discharge valves using C.D.I. s Valve Dynamic Model Code. This code was developed under 1
the sponsorship of the Electric Power Research Institute as part of the EPRI SRV.Test Program. The code is presently restricted to valve simula-tions for flow of high quality steam. Modifications to the code to include flow of subcooled water will be made in the near future, which will provide capability to analyze valve performance during loop seal clearing.
The Valve Dynamic Model Code is based on a control volume for quasi-steady steam flow through a spring loaded valve. The control volume analysis provides the net force acting on the valve disc. This force is utilized in a spring/mass/damper system equation to describe the valve stem motion given the reservoir pressure time history. The force contribution due to flow exiting the control volume is a function of the valve guide ring setting in terms of a predetermined geometric model. The steam flow is represented by an isen-tropic, ideal gas approximation. Coupling between the upstream piping acou-stics and the valve motion is included in the model. Reference 1 contains a complete description of the valve model described briefly above.
In addition to the valve dynamic analysis, an evaluation of the Sa*lem Unit One safety discharge piping pressure downstream of the safety valves is reported here. This back pressure was calculated for the plant-unique safety discharge line of this plant, including the effects of pipe fittings, shocks and area changes. The calculations were carried out using the C.D.I. Quasi-Steady Back Pressure Code, Reference 2, which is based on the assumption of steady-state adiabatic homogeneous equilibrium flow with friction. Frictional losses due to the presence of pipe fittings is accounted for by adding equiva-lent lengths of pipe.
The Salem Unit One safety discharge system utilizes Crosby 6M6 safety valves, a valve type tested during the CE/EPRI SRV Tests.
1
- 2. VALVE DYNAMIC MODEL SIMULATION The important design features of a Crosby safety valve are shown in Figure 1, and a cross-section of the Crosby 6M6 internals is shown in Fig-ure 2, approximately to full scale. The flow rates supplied to C.D.I. by PSE&G and which were used in the dynamic and back pressure analyses, are 470,000 lb/hr for the safety valves and 233,333 lb/hr for the relief valves.
The adjusting ring settings used for this analysis were -190 and -250 notches for the upper guide ring and -18 notches for the lower ring. Two of the three Salem safety valve upper rings are set at the -190 value, with the third set at -250. Although the valve dynamic model code is presently being extended to include capability to treat the flow of subcooled water, the operationa 1 code is restricted to fl ow of high qua 1 ity steam. The presence of loop seals is, therefore, neglected for the present.
The valve model was run including acoustic coupling between the valve and the upstream piping. The length of upstream piping used for the dynamic calculations consists of 16.2 feet of 6 inch diameter, schedule 160, derived using PSE&G Drawing Nos. 267PCL and 267PDL, Rev. 1, as supplied to C.D.I. by PSE&G. This length exists upstream of the lPR-3 safety valve. The lengths upstream of the lPR-4 and lPR-5 valves are 14.5 and 13.9 feet, respectively.
The longest existing length was, therefore, used for the performance simula-tion. Upstream piping for all three safety valves is 6 inch diameter.
The valve mass properties, spring rate, and geometric characteristics were assumed equal to the nominal values obtained either from the valve manu-facturer or derived from the manufacturer's assembly drawings during code development. Table 1 presents a partial list of the important characteristics for the Crosby 6M6 valve.
The pressure time history used for the calculation was a linearly de-creasing function of time, starting at 2575 psia and reaching 1700 psia in 4.5 seconds. For a set pressure of 2500 psia the valve, therefore, opens immediately and closes when the force balance on the valve disc yields a net force insufficient to keep the valve open against the spring force and the back pressure. (See Reference 1 for a detailed description of the valve model employed here.)
2
Uncompensated Back Pressure Area Educ tor Ex it Ports Upper Adj Ring Holder Vc:. l ve Outlet Adj Ring Valve Body Bowl Valve Inlet Figure 1. General design features of Crosby spring loaded safety valves 3
Figure 2. Details of the Crosby 6M6 safety valve 4
TABLE 1 Crosby 6M6 Characteristics and Geometric Parameters Item Units Valve Mass of moving parts 1bm 47.5 Spring mass 1bm 43.3 Maximum rated 1i ft in 0.538 Spring rate 1b/i n 15070
. 2 3.6 Nozzle area in Exit area in 2 3.4
. 2 0.4 Eductor area in
. 2 Uncompensated back pressure area in 5. 54 Flange area in 2 1.02
The valve stem position histories which result from the dynamic calculations are shown in Figures 3 to 5. Figure 3 shows the valve position for the -190 notch upper ring setting, including the effects of coupled upstream piping. Figures 4 and 5 are plots of valve posi-tion for an upper ring setting of -250 notches. The results shown in Figure 4 were obtained neglecting upstream piping, while those of Fig-ure 5 include coupling effects.
The opening and closing characteristics predicted by the model are similar to the characteristics of Crosby 6M6 valves tested during the CE/EPRI SRV tests which opened on steam, e.g., test runs 903 and 1411. This code simulation indicates that the Crosby 6M6 valve operates stably on steam flow for the ring settings of the Salem Plant, Unit One.
For the -190 and -18 notch settings on the upper and lower rings the code predicts a blowdown of 8.4%. For settings of -250 and -18 notches, the predicted blowdown in 8.6%.
It might be noted that since instability is more likely to occur as the length of upstream piping is increased, the present calculations using the longest upstream pipe length is conservative in this respect .
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- 3. BACK PRESSURE ANALYSIS
- The Salem Unit One Plant has three safety valves and two relief valves in the safety discharge lines. The back pressure calculations for the Salem Plant were made with all safety and all relief valves open.
A schematic of the Salem Plant piping downstream of safety valve lPR-4, which has the longest actual plus equivalent length piping for this plant, is shown in Figure 6. The pressure profile along this piping is given in Figure 7. The back pressure at the lPR-4 valve exit is predicted to be 688 psia for a pressurizer pressure of 2500 psia and steam quality of one.
Profiles for the lPR-3 and lPR-5 downstream piping are shown in Figures 8 and 9. The piping lengths in these last two figures continue only to their first branch point. The back pressure at the valve exit for these two valves is calculated to be 635 psia for the lPR-3 valve and 616 psia for the lPR-5 valve. Note that the back pressure calculated for one of the Salem Unit One safety valves and reported in Reference 2 \'JaS 478 psia for one safety valve open .
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- 0°40 FEET OF 12 INCH X-STG PIPE 1.00 FEET OF 12 INCH X-STG PIPE 25-40 FEET OF 12 INCH STD PIPE 12 INCH 30 DEG 5°0 R ELBOW
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- * * .. * .. * .... * *. 19-20 FEET OF 12 INCH STD PIPE 12 IHCH 27 DEG 5-0 R ELBO~*I
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-10 0 10 20 30 40 50
- >< DISTANCE CFTJ Figure 9. Downstream piping back pressure for the Salem Unit One lPR-5 safety discharge line
- 4. CONCLUSIONS A simulation of the Crosby 6M6 safety valve performance for the Salem Unit One Plant using the EPRI/C.D.I. Valve Dynamic Model Code has been made and indicates stable performance on discharge of high quality steam. Although loop seal clearing was neglected the simula-tion is felt to be representative of conditions for valve closure on steam flow. The ring settings of -190 notches and -18 notches for the upper and lower rings would, therefore, appear to lead to stable valve performance on steam for two of the valves, while the third is stable for settings of -250 and -18 notches for the upper and lower rings, respectively .
- 5. REFERENCES
- 1. Hecht, A.M., Teske, M.E. and A.J. Bilanin: 11 Coupled Val.ve Dynamic Model Technical Description, 11 (Draft Report), Continuum Dynamics, Inc.,
July 1982. Prepared for participating utilities and the Electric Power Research Institute.
- 2. Hecht, A.M., Teske, M.E. and D.B. Bliss: 11 Quasi-Steady Back Pressure for Pressurized Water Reactor Safety and Relief Valves, 11 Volumes I, II and II. Continuum Dynamics, Inc. Prepared for participating PWR Utilities and the Electric Power Research Institute .