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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. ML18106A2571998-01-19019 January 1998 Nuclear Business Unit Future Objectives. ML18106A2131997-12-15015 December 1997 Safety Evaluation Supporting Rev to TS to Adopt Option B of 10CFR50,App J,For Type B & C Testing & Modify Existing TS Wording for Previous Adoption of Option B on Type a Testing ML18102B3331997-02-28028 February 1997 Rev 0 to Cfcu Return Piping Inside CTMT,221F Temp Effect. ML20133D2201996-12-0606 December 1996 Root Cause Analysis of Struthers-Dunn Operate-Reset Relay Latch Failures for Salem Generating Station ML20133D2251996-10-30030 October 1996 Struthers-Dunn Model 255XCXP Relay Root Cause Evaluation for Salem Nuclear Generation Station ML18102A3231996-07-0101 July 1996 Reg Guide 1.121 Assessment of Indications at Salem Unit 2. ML18102A1591996-06-0404 June 1996 Fuel Handling Accident Analysis Radiological Evaluation. ML20101M6601996-03-24024 March 1996 Supplemental Submittal in Response to NRC GL 87-02/USI A-46, 'Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors.' ML18102A1321996-03-15015 March 1996 Change 2EC-3332 to Rev 0 to Design Analysis, 125 Vdc Battery Charger Replacement. ML18102B0201996-02-28028 February 1996 Rev 0 to Evaluation of Structures for Increased Temps Due to Updated Main Steam Line Break. ML20129K1031995-07-10010 July 1995 Exam of Fasteners from Salem Nuclear Generating Station ML18101A7481995-05-19019 May 1995 Safe Shutdown Equipment List Rept for Salem Generating Station Units 1 & 2 ML18101A7491995-04-25025 April 1995 Relay Evaluation Rept, Volumes 1 & 2, for Salem Generating Station Units 1 & 2 ML18101A7501995-04-20020 April 1995 Seismic Evaluation Rept, for Salem Generating Station ML20134K1031995-03-24024 March 1995 Organizational Effectiveness Assessment Rept for Sngs, ML18102B6541995-03-24024 March 1995 Organizational Effectiveness Assessment Rept for Plant, Redacted Version ML18101A4391994-12-21021 December 1994 Fire Protection Review of Salem Reactor Coolant Pump Oil Collection Sys, Dtd 941221 ML20134C5791994-10-23023 October 1994 Salem/Maint SC.MD-GP.SW-0001(Q) Svc Water Silt Survey, Rev 5 ML18106B0541994-01-31031 January 1994 Criticality Analysis of Salem Units 1 & 2 Fresh Fuels Racks. ML18100A7971993-12-23023 December 1993 Simulator Four-Year Certification Rept. ML20069M2221993-10-15015 October 1993 Flux Thimble Thermocouple Ultrasonic Profilometry & Eddy Current Encircling Coil Insp of Stored Thimble Tubes Jul-Aug 1993 ML18100A6281993-09-16016 September 1993 Updated Page A4-4 of Boric Acid Concentration Reduction Effort Technical Bases & Operational Analysis, Changing Figure Numbers A5-1 & A5-2 to A4-1 & A4-2 at End of First Paragraph ML18100A6801993-08-20020 August 1993 Engineering Evaluation of Sgs 1 & 2 Control Room Evacuation for Fire Induced MOV Hot Shorts as Discussed in NRC Info Notice 92-018. ML20045B8801993-05-21021 May 1993 Boric Acid Concentration Reduction Effort Technical Bases & Operational Analysis for Salem Nuclear Generating Station, Units 1 & 2. ML18100A3401993-04-28028 April 1993 Licensing Rept for Spent Fuel Storage Capacity Expansion Pse&G,Salem Generation Station,Units 1 & 2. ML18096B3561993-02-11011 February 1993 Cycle 8 Peaking Factor Limit Rept. ML20135A8141992-12-29029 December 1992 Control Room Overhead Annunciator Lock-Up of 921213 ML18096B1661992-11-13013 November 1992 Rev 1 to Fracture Toughness Analysis for Salem Units 1 & 2 Reactor Pressure Vessels to Protect Against Pressurized Thermal Shock Events,10CFR50.61. ML18096B0081992-09-0202 September 1992 Analytical Data Rept, for Project 28173 ML18096A8061992-06-17017 June 1992 Rev 0 to Salem Unit 2 Response to Generic Ltr 92-01,Rev 1, 'Reactor Vessel Structural Integrity.' ML18096A8051992-06-17017 June 1992 Rev 0 to Salem Unit 1 Response to Generic Ltr 92-01,Rev 1, 'Reactor Vessel Structural Integrity.' ML18096A5831992-03-31031 March 1992 Rev 1 to Estimated Frequency of Loss of Off-Site Power Due to Extremely Severe Weather & Severe Weather for Salem & Hope Creek Generating Stations. ML18095A5151990-07-31031 July 1990 Vol 1 to Spring 1990 NDE of Selected Class 1 & Class 2 Components of Salem Generating Station,Unit 2. ML18095A3691990-07-26026 July 1990 Unit 1 Decommissioning Rept. ML18095A3681990-07-26026 July 1990 Unit 2 Decommissioning Rept. ML18095A3791990-07-20020 July 1990 Decommissioning Rept of Philadelphia Electric Co. ML18094B2241989-12-28028 December 1989 Simulator NRC Certification, Vols I-III ML18094A3551989-04-30030 April 1989 Assessment of Impacts of Salem & Hope Creek Generating Stations on Kemps Ridley (Lepidochelys Kempi) & Loggerhead (Carretta Caretta) Sea Turtles. ML20086U2571989-03-31031 March 1989 Estimated Frequency of Loss of Offsite Power Due to Extremely Severe Weather & Severe Weather for Salem & Hope Creek Generating Stations ML18093B2021988-09-30030 September 1988 Special Rept on Spare CRD Mechanism Weld Refurbishments. ML18093A7601988-02-18018 February 1988 Appendix R/Breaker Coordination as-Found Review (Pre-Audit 1987). ML18093A5471987-12-10010 December 1987 Breaker Coordination W/Respect to External & Internal Hazards. ML18093A4531987-10-14014 October 1987 Justification for Continued Operation of Salem Units 1 & 2 W/Outstanding Fire Protection Concerns. ML18093A4131987-10-0101 October 1987 Justification for Continued Operation of Salem Units 1 & 2 W/Outstanding Fire Protection Concerns. ML18093A3781987-09-16016 September 1987 Rev 7 to, Westinghouse Engineering Svcs Rept for Salem Nuclear Generating Station Units 1 & 2 Concerning RHR Sys Mid-Loop Operation Re NRC Generic Ltr 87-12. 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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EVALUATION OF SI.CW RESRJNSE RTDs. ON SALEM UNIT 1 SAFETY ANALYSIS Introciuction During the refueling outage fer Salem Unit 1 Cycle 6, PSE&G replaced *.the Rosemont RTDs with RdF RTDs. The RTDs are use to* measure- average coolant -
teinperature (Tavg)in the core. The measured value of Ta~g is used as input-to
. both the central and protection systems. The effect on the protectiol'! system due to the new RTDs must be evaluated in order to show that the safety analysis presented in the FSAR remains valid. Although the control system response may also be affected, -operation Of the control system is not asst.med .in the safety analysis to mitigate* a transient. Thus, the impsct on the control systems* need not be considered.
The origirsl Rosemont RTDs are fast acting _RTDs with a response time of approximately* .5 seconds, whereas the RdF RTDs _have a respon5e time of about 3 seconds. _ Since the new RTDs have a mu:h slcwer response* time, those protection system f1.11ctions which rely on measurement of Tavg may also have a slower response time. The*resil:>nse *times assuned_in the safety analysis are reflected in the plant Technical S~cifications. These must be measured on a pariodic basis. With the increased response time of the RdF RTDs, the ~ssibility exists that the maximun allowable* response times listed in the Tech Spacs cannot be met, thus ~tentially invalidating the safety analysis. The Tech Spec response times are defined as the time interval from when the monitored paraneter exceeds its setpoint 1.11til the rods are free to fall or _the Engineered Safety Feature is capable of parforming its f1.11ction.
Since the Rosemont RTDs have a fast response time, the signal output is processed through an electronic filter to reduce noise. The combined response of the fast RTD with the filter is approximately equal to_ that of the slew response RdF RTDs without a filter. Thus, by removing_ the filter, the overall protection system response times which are based on T input will be similar *
.~~~~----=-=-=-~==-==-:::=~~~~* avg r 8503050216 850225 l PDR ADOC~ 05000272 p PDR
Saiety Eyalyation The T signal is used as input to the overtem~rature/overi::ower delta-T trips avg . .
and to the steanline break protection system signal of high steam fl~
coincident with lcw-Tavg* This signal actuates reactor trip, safety .injection, steamline isolation, and feedline isolation, and initiates auxiliary feedwater.
Thus, those accidents which rely on this signal must be evaluated with respect to a slGJer protection system response time. The evaluation presented here assumes that the overall response time of tile protection signals is increased by 3 seconds over the times assuned in the FSAR safety *analysis. This is a conservative assun~ion, particularly if tile filters on Tavg measurement are removed.
Steamline Rupture - The steamline rupture analyses presented in the Salen FSAR
.do not take credit fer the high steam flGJ/lGJ Tavg signal. In the core analy si~, the high steam flGJ coincident with lGJ steat1 pressure signal is assuned in the analysis of tile double ended rupture (Section 15 .4.2). For *the accidental depressurization of the main steam system (Section 15.2.13), the lGJ
. pressurizer pressure signal is used. These signals are also considered in the contairme.nt analysis presented in Section 15 .4 .8.2 of tile FSAR. In addition, contairment pressure signals are considered. Thus, the_ increased. response time of tile coincident high steam flew/ lGJ Tavg signal will not, imI=Sct the safety analysis.
Note that this additional delay, if considered, would not have a significant imI=Sct on the safety analysis. With respect to the core analysis, the.
steamline break event is a cooldown transient and is primarily dependent on the core reactivity paraneters and the blGJdown rate of the faulted loop. For both steanline break transients presented in the FSAR, it is shown that the DNBR remains above the limit value of 1.30. For the containment analysis, the containnent pressure and tem~rature resp:rnses are a fl.l1ction of.the mass and* energy released during the blcwdown.
In evaluating the core response, the effect on the minimun DNBR must be considered. Prior to steamline isolation, all four loops blGJ down at the same rate, providing uniform cooling to the core. Thus, there is no assymmetric
e e cooling which results in a non-unifcrm power distribution in the core. If steamline isolation is delayed, the time. at which non-uniform cooling begins will also be delayed,- resulting in a more L11ifonn power distribution. This reduces the Il)Wer i:eaking in the core and results in a higher DNBR.
On the other hand, an increased delay in feedwater isolation will cause more feedwater to be delivered to the steam generators and increase the blcwdown. _
. This increased blcwci.own will result in more cooling of the primary siQ.e and consequently, a higher return to power.* This may result in a lcwer DNBR. An evaluation of the increased feedwater isolation time shows that an additional three* seconds will not have an ll'lacceptable effect on the minimun DNBR for the double ended rupture. This evalilation is based upon sensitivity studies presented in WCA.P-9226, "Reactor Core Response to Excessive Secondary Stean Releases" (proprietary), rriere commonly known as the steambreak topical.
Al.though the steanbreak topical was not used in support of. the Salem FSAR (it post-dates the FSAR), the conclusions presented are generic in nature and as such can be applied to Salem. Thus, an increase of three seconds in the delay in feeawater isolation is acceptable fer the core analysis.
The containment analysis performed for Salen assunes both the failure of an MSIV and a feedwater regulating valve. These single failures have a ~imilar effect as an additional three second delay in steamline or feedline isolation since both the single failures and the delay result in more mass being released to the. containment. Hcwever, the limiting transients fer both tani:erature and pressure are not those for which the single failure is either the MSIV or feedwater regulating valve* failure. Rather, the limiting single failure is the failure of a containment safeguards train. Thus, the additional delay is* not is not expected to impact the containment response.
The delay of safety injection will also have a negligible impact on the resul~ts
.of both the core and containment analyses *. The increase in core power ~s tenninated by the dryout (cessation *of bla.Jdbwn) Of the faul ~ed. loop, not by the addition of boron to the core by the safety injection system. The total mass released to the containment is unaffected by the time of safety injection. Thus, the delay of boron by three seconds will have no impact.
Note also that an analysis assuning boron concentration reduction in the BIT
.* has been perfc:nned fer Salen wh~ch shows acceptable results (reference 1). The
. delay of boron injection into the. core fer tilis analysis is more severe than that i:ostulated due to the additional three second delay of the protection system.
Finally, the delay of auxiliary feedwater addition will not irilµact the results because the auxiliary feedwater system is conservatively ass1.111ed to be on at*
the initiation of the transient. This maximizes both the cooldown fer the core analysis and the mass/energy releases to containment. No time response fer auxiliary feedwater initiation is asst.med. Thus, a delay in auxiliary
- feedwater wOuld be a benefit fer both the core and containment analysis.
. In sunmary, the increased protection system response time will not impact the steamline break analyses presented in the FSAR because the Ta vg signal is. not used in the analysis. If the delay is assuned independent of this consideration, there is sufficient margin and/or conservatism in the analysis such that the safety limits will continue to be met.
- Bank Withdrawal at Power .;. This transient relies upon the high neutron flux and overtemi:erature delta-T trips fer protection to ensure that the minimun DNBR remains above 1.30. This event is analyzed in Section 15.2.2 of the FSAR. A range of reactivity- insertion rates I caused by the bank with draw al is considered from several initial p'.)Wer levels to demonstrate that these two trips provide
. adequate protection.. These analyses are also i:erformed assuming minimun and maximun -reactivity feedback. Although the increa5ed resp'.)nse time or' the RTDs . *
- will not impact those cases which trip .
due* to a high neutron flux signal, . those cases resulting in an overtemi:erature del ta-T trip will be delayed. Reactor ti'ip may instead occur due to a high neutron flux signal or by the delayed.
ov~rtemi:erature delta-T signal. For these cases, the minimun DNBR reached during the transient wili be lcwer. Thus, this event must. be reanalyzed to -
show that the DNB design basis continues to be met.
The transient was reanalyzed employing the same digital computer codes and*
assumptions regarding instrunentation and setpoint errors used for the FSAR.
The FSAR assuni;tions on reactivity feedback were *also ass1.111ed. Hcwever, instead of assuming a 6 second delay time for reactor trip on overtani:erature
.del ta-T, a 9 second time delay was assuned. The 9 seconds includes the time to heat the RTD bypass lines, the sensor resp:mse, logic, voltage decay and gripper release of the rods.
Figure 1 shows the minimllll DNBR as a ft11ction of reactivity insertion rate fer the bank withdrawal initiating *from 100 percent power for both maximllll and minimun feedback. S:imilar results were obtained fer the transient initiating from 60 percent and 10 percent power. These* are 1 ess limiting than the results from full power, thus the detailed results are not presented. As expected, mere cases results in a trip due to a high neutron flux signal because the overtanperature del ta-T signal is delayed.. However, fer all cases, the minimllll_
DNBR remains above 1.30~ Thi.ls, the _additional delay of the res!X)nse time is acceptable.
Recently; Westinghouse performed a safety analysis for Salem with a positive moderator tanperature coefficient (reference 2). This* affects the minimun .
reactivity feedback cases _of the bank with draw al at power event. Al though t.his has not -yet been approved by the NRG, an analysis incorporating a +5 pcm1°F moderator tanperature coefficient was al.sO performed asstining a 9 second delay. The results of this analysis also. show that the DNBR design basis is*
met.
In addition, Westinghouse_ also performed safety analyses incor!X)rating an increased Doppler-only power coefficient (reference 3). This* new -coefficient was based on calculations of the coefficient: by PSE&G fer the Salem Unit 1 Cycle 6 design. In this analysis, t.he bank withdrawal at power was reanalyzed fer maximun feedback to account for the increased Doppler coefficient,.
'Iheref cre, in order to complete the evaluation of the increased protection system res!X)nse time, t.he bank withdrawal at power event with maximun feedback and the PSE&G calculated Doppler-only power coefficient was reanalyzed assun+/-ng a 9. :Second response time *.
'Ihe results of the analyses fer the positive moderator tem~rature coefficient and the increased Doppler feedback are presented. in Figure 2 for the event initiated from full power. Again, the minirnun DNBRs reached when the transient initiates f_rom intermedia_te !X)wer levels are less limiting. The minimun
f°eedback cases are those assuning a !X'Si tive moderator tanperature coefficient. The maximun feedback cases are those incor1X>rating the Doppler-only !X>Wer coefficient as calculated by PSE&.G. For all cases, the minimt.m DNBR is above 1.30.
sunmary An evaluation of those accidents relying on measuranent of Tavg for actuation of the protection system has been performed. These accidents are stecrnJ.-ine rupture and uncontrolled bank withdrawal at 1X>Wer. The results of the evaluations and analyses show that all safety limits will be met if an additional 3 second delay is considered in the response time of the protection system.
References
- 1. Letter PSE*00-528, Noon (J:l) to Librizzi (PSE&G), 11Feasibility Report fer BIT Concentration Reduction/BIT Elimira ti on fer Salem Units 1 and 211 ,
September 1980
- Letter PSE-81-509, Noon (J:l) to Uderitz (PSE&G), March 1981, contains additional infermatian.
- 2. Letter 84PS*-G-024, Croasdaile (J:l) to Brenner (PSE&G), "Positive Moderator
- Temperature Coefficient Study", March 1984.
Letters 84PS*-G-057, 84PS*..c;;..072, and 84PS*-G-074 contain additional infermation on the study.
- 3. Letter 84PS*-G-058, Croasdaile (J:l) to-Brenner (PSE&G), "Increased Doppler Coefficient .study*i, June 1984.