Similar Documents at Salem |
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LER-1979-059, Forwards LER 79-059/03L-0 |
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| 2721979059R00 - NRC Website |
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Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 i430-7000 March 27, 1980 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
Dear Mr. Grier:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 79-59/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 79-59/03L.
Following a review of 1979 Incident Reports, it was determined, in conjunction with the Resident Inspector, that the enclosed incidents are reportable as Licensee Event Reports.
Sincerely yours, Al,~
F. P. Librizzi General Manager -
Electric Production CC:
Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control (3 copies)
Report Number:
79-59/03L Report Date:
3/27/80 Occurrence Date:
April 24, May 8, June 30, 1979 Facility:
Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Loss of Residual Heat Removal (RHR) Pump CONDITIONS PRIOR TO OCCURRENCE:
Refueling Mode 6 DESCRIPTION OF OCCURRENCE:
On April 24 and May 8, 1979, during Unit 1 first refueling outage, Relay Department personnel were performing tests on vital bus breakers.
During the testing evolution, the vital bus supplying the operating RHR Pump inadvertently de-energized, causing loss of RHR flow.
In each case, operating personnel were aware of the relay work and alerted to the possibility of loss of the operating RHR Pump.
No core alterations or dilutions were in progress.
RHR flow was restored within two minutes on April 24, 1979, and within four minutes on May 8, 1979.
On June 30, 1979, also during the refueling outage, the operating RHR Pump started to lose suction and was removed from service.
The
.reactor vessel water level was checked at 97 feet 1 inch.
The reactor vessel water level was increased to 97 feet 6 inches and the RHR Pump was returned to service.
RHR flow was lost for 34 minutes.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of the occurrences on April 24, 1979 and May 8, 1979 was due to improper Relay Department action during the relay testing.
On June 30, 1979, due to maintenance being performed on plant equipment, the reactor vessel water level was lowered to approximately one inch above the low operating level for the RHR Pump.
This incident showed that the low operating level did not provide sufficient suction for the RHR Pump.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.9.8 states, "At least one residual heat removal loop shall be in operation." Action Statement a.requires that "with less than one residual heat removal loop in operation, except as provided in b. below, suspend all operations involving an increase in the reactor decay heat load or a reduction in boron concentration of the Reactor Coolant System.
Close all containment penetrations providing direct access from the containment atmosphere to the outside atmosphere within four hours."
c.-..
LER 79-59/03L 2 -
Action Statement b requires, "The residual heat removal loop may be removed from operation for up to 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> per 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> period during the performance of core alterations in the vicinity of the reactor vessel hot legs."
During all three occurrences, no core alteration or reactivity changes were in progress.
The Technical Specification limiting condition for operation was not exceeded as the maximum time RHR flow was lost was 34 minutes.
As a point of interest, Amendment 24 to Salem Technical Specifi-cations 3.4.1.1 in all modes except Refueling Modes, with reactor power below P-7 and with K ff < 1.0, all Reactor Coolant Pumps and Residual Heat Removal Pumps may be de-energized for up to one hour, provided no operations are permitted which could cause dilution of the Reactor Coolant System boron concentration.
CORRECTIVE ACTION
The Relay Department has reviewed and corrected their procedures and operating practices to prevent recurrence of this problem.
An on-the-spot change has been implemented which changes the low reactor water level alarm set point from the centerline of the hot leg pipe (approximately 97 feet) to 97 feet 6 inches.
These occurrences are considered isolated incidents and no further corrective action is required.
FAILURE DATA:
. Not applicable Prepared By A. W. Kapple SORC Meeting No.
'20-80'
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| 05000272/LER-1979-001-03, /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | | | 05000272/LER-1979-001, Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | | | 05000272/LER-1979-002-03, /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | | | 05000272/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000272/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000272/LER-1979-003-03, /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | | | 05000272/LER-1979-004, Forwards Updated LER 79-004/03X-1 | Forwards Updated LER 79-004/03X-1 | | | 05000272/LER-1979-004-03, /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | | | 05000272/LER-1979-005-03, /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | | | 05000272/LER-1979-005, Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | | | 05000272/LER-1979-006-03, /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | | | 05000272/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000272/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000272/LER-1979-007-03, /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | | | 05000272/LER-1979-008-03, /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | | | 05000272/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000272/LER-1979-009-03, /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | | | 05000272/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000272/LER-1979-011, Forwards LER 79-011/01X-2 | Forwards LER 79-011/01X-2 | | | 05000272/LER-1979-011-01, /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | | | 05000272/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000272/LER-1979-012-03, /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | | | 05000272/LER-1979-013-04, /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | | | 05000272/LER-1979-013, Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerat | Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerations | | | 05000272/LER-1979-014-03, /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | | | 05000272/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000272/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000272/LER-1979-015-03, /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | | | 05000272/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000272/LER-1979-016-03, /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | | | 05000272/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000272/LER-1979-017-03, /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | | | 05000272/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000272/LER-1979-018-03, /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | | | 05000272/LER-1979-020-03, /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | | | 05000272/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000272/LER-1979-021-03, /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | | | 05000272/LER-1979-022-03, /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | | | 05000272/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000272/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000272/LER-1979-024-03, /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | | | 05000272/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000272/LER-1979-025-03, /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | | | 05000272/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000272/LER-1979-026-03, /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | | | 05000272/LER-1979-027-01, /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | | | 05000272/LER-1979-027, Forwards LER 79-027/01X-1 | Forwards LER 79-027/01X-1 | | | 05000272/LER-1979-028, Has Been Voided | Has Been Voided | | | 05000272/LER-1979-029-03, /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | | | 05000272/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | |
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