Similar Documents at Salem |
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LER-1979-077, /03L-0:on 791224,during Startup,Breaker 11ASD tripped,de-energizing 4 Kv Vital Bus 1A & Supplied Plant Loads.Caused by Failure of Components in Logic Circuit.Five Logic Boards & One Relay Replaced |
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| 2721979077R03 - NRC Website |
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Report Number:
79-77/03L Report Date:
1/23/80 Occurrence Date:
12/24/79 Facility:
Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
lA Safeguard Equipment Control (SEC) Inoperable CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 3 DESCRIPTION OF OCCURRENCE:
At 1004 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.82022e-4 months <br />, the llASD infeed breaker to the lA 4kV vital bus tripped, de-energizing the bus and causing loss of various plant equipment.
The lA emergency diesel generator started but did not go through the loading sequence.
The control room operator initiated recovery of de-energized equipment and an equipment operator went to the relay room to investigate and reset the lA SEC panel.
Indicated trouble was bus undervoltage and underfrequency brit the operator had no difficulty resetting the panel.
At 1008 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.83544e-4 months <br />, the llASD breaker was reclosed and the lA emergency diesel was secured.
Recovery from loss of de-energized equipment was complete by 1013 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.854465e-4 months <br />.
Maintenance electricians investigated the occurrence; and at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, declared the lA SEC inoperable.
Technical Specifications 3.8.1.1 and 3.3.2.1 Action Statements were implemented.
At 2020 hours0.0234 days <br />0.561 hours <br />0.00334 weeks <br />7.6861e-4 months <br />, the lA SEC was returned to service and the Action Statements were terminated.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of this occurrence was a failure in the lA SEC logic circuitry which incorrectly monitored an undervoltage condition on the lA vital bus and tripped the llASD infeed breaker.
The SEC operated as designed by unloading the bus and starting the emergency diesel generator and not initiating the auto load sequence which requires a fault on two of the three vital busses.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.3.2.1 requires that with the number of operable SEC channels one less than the total number of channels, be in Hot Standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Cold Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
The reactor was in Hot Standby throughout this occurrence.
The lA SEC channel was repaired and returned to service in 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 16 minutes.
8001290 ~~
tER 79-77/03L Technical Specification 3.8.1.1 requires that with a diesel generator inoperable, remaining AC sources shall be demonstrated operable by performing 4.8.1.1.la and 4.8.l.l.2a2 surveillances within one hour and at least once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> thereafter.
This Technical Specification was implemented and the surveillances performed as required although the offsite-onsite transmission distribution systems and the diesel generators were operable throughout this occurrence.
CORRECTIVE ACTION
The entire logic drawer was replaced with a spare unit and tested satisfactorily before returning the lA SEC to service.
Trouble-shooting of the failed drawer resulted in five logic boards and one faulty relay in the relay stack being replaced.
FAILURE DATA:
Safeguards Equipment Control System Automation Industries, Inc.
Silver Springs, Maryland Prepared By A. W. Kapple Manager -
Salem Generating Station SORC Meeting No.
05-80
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(())] I During startup operations, the llASD breaker tripped, de-energizing the lA 4kV
((II) I vital bus and supplied plant loads.
The lA SEC panel was reset and the llASD breaker was reclosed.
Maintenance electricians declared the lA SEC inoperable and Action Statements for T/S 3.8.1.l and 3.3.2.1 were implemented.
The lA *SEC was repaired, tested and returned to service in 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> and 16 minutes.
The plant was!
C£:I:I:J I in Hot Standby th~oughout this occurrence.
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Failed components in the logic circuit sensed an erroneous undervoltage condition on lA vital bus and opened the llASD infeed breaker.
The entire logic drawer was replaced to expedite recovery of the lA SEC.
Further troubleshooting of the IJ:II] I failed drawer resulted in five logic boards and one relay beinq replaced.
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| 05000272/LER-1979-001-03, /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | | | 05000272/LER-1979-001, Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | | | 05000272/LER-1979-002-03, /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | | | 05000272/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000272/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000272/LER-1979-003-03, /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | | | 05000272/LER-1979-004, Forwards Updated LER 79-004/03X-1 | Forwards Updated LER 79-004/03X-1 | | | 05000272/LER-1979-004-03, /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | | | 05000272/LER-1979-005-03, /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | | | 05000272/LER-1979-005, Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | | | 05000272/LER-1979-006-03, /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | | | 05000272/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000272/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000272/LER-1979-007-03, /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | | | 05000272/LER-1979-008-03, /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | | | 05000272/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000272/LER-1979-009-03, /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | | | 05000272/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000272/LER-1979-011, Forwards LER 79-011/01X-2 | Forwards LER 79-011/01X-2 | | | 05000272/LER-1979-011-01, /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | | | 05000272/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000272/LER-1979-012-03, /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | | | 05000272/LER-1979-013-04, /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | | | 05000272/LER-1979-013, Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerat | Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerations | | | 05000272/LER-1979-014-03, /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | | | 05000272/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000272/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000272/LER-1979-015-03, /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | | | 05000272/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000272/LER-1979-016-03, /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | | | 05000272/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000272/LER-1979-017-03, /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | | | 05000272/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000272/LER-1979-018-03, /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | | | 05000272/LER-1979-020-03, /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | | | 05000272/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000272/LER-1979-021-03, /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | | | 05000272/LER-1979-022-03, /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | | | 05000272/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000272/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000272/LER-1979-024-03, /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | | | 05000272/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000272/LER-1979-025-03, /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | | | 05000272/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000272/LER-1979-026-03, /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | | | 05000272/LER-1979-027-01, /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | | | 05000272/LER-1979-027, Forwards LER 79-027/01X-1 | Forwards LER 79-027/01X-1 | | | 05000272/LER-1979-028, Has Been Voided | Has Been Voided | | | 05000272/LER-1979-029-03, /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | | | 05000272/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | |
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