ML17174A797

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Insp Repts 50-237/91-16 & 50-249/91-15 on 910517-0628. Violations Noted.Major Areas Inspected:Ler,Operational Safety,Monthly Maint,Monthly Surveillance,Safety Assessment & Quality Verification
ML17174A797
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 07/12/1991
From: Burgess B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17174A795 List:
References
50-237-91-16, 50-249-91-15, NUDOCS 9107230173
Download: ML17174A797 (14)


See also: IR 05000237/1991016

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports No. 50-237/91016(DRP); 50-249/91015(DRP)

Docket Nos.

50-237; 50-249

Licenses No.

DPR-19; DPR-25

Licensee:

Commonwealth Edison Company

Opus West I II

1400 Opus Place

Downers Grove, IL

60515

Facility Name:

Dresden Nuclear Power Station, Units 2 and 3

Inspection At:

Dresden Site, Morris, IL

Inspection Conducted:

May 17 through June 28, 1991

Inspectors:

W. Rogers

D. Hills

M. Peck

Approved By:

M. Phillips

J. Schapker

D. Butler

R. Lerch

R. Zuffa, Site Resident Engineer

Illinois Department of Nuclear Safety

c~~

B. L. Burg~

Projects Section lB

Inspection Summary

Date'

'

Inspection from May 17 through June 28, 1991 (Reports No. 50-237/91016(DRP);

50-249/91015(DRP)).

Areas Inspected:

Routine unannounced safety inspection by the resident

inspectors, regional inspectors, and an Illinois Department of Nuclear Safety

inspector of licensee action on previously identified items; licensee event

report; operational safety; monthly maintenance; monthly surveillance; safety

assessment and quality verification; events; training effectiveness; and report

review.

Results:

Two cited violations were identified.

One involved a failure to

incorporate appropriate instrumentation into the periodic calibration program.

The other involved a failure to meet reporting requirements.

One non-cited

violation was identified involving inadequate preparation of a 10 CFR 50.59

safety evaluation.

One open item related to the emergency diesel generators*

output .breaker logic design was identified.

9107230173 910715

PDR

ADOCK 05000237

Q

PDR

  • *

Operations

Performance appeared adequate with LCOs met and tew personnel errors.

However, some reporting evaluation weaknesses were observed.

Maintenance/Surveillance

Maintenance activities were properly accomplished.

However, weaknesses were

apparen~ in the breadth and coverage of the instrument calibration

program.

Ra.die l ogi cal Protection

While observations were limited, no program or implementation weaknesses were

observed.

Emergency Preparedness

This SALP functional area was not addressed in this inspection period.

Security

While observations were limited, performance in this area remained good.

Safety Assessment ana Quality Verification

Performance appeared adr:quate with some weaknesses in the safety evaluation

process.

Engineering and Technical Support

This area was not addressed.

DETAILS

1.

Persons Contacted

Commonwealth Edison Company

  • E. Eenigenburg, Station Manager
  • L. Gerner, Technical Superintendent

J. Kotowski, Production Superintendent

E. Mantel, Services Director

D. Van Pelt, Assistant Superintendent - Maintenance

J. Achterberg, Assistant Superintendent - Work Planning

  • G. Smith, Assistant Superintendent-Operations

K. Peterman, Regulatory Assurance Supervisor

  • M.- Korchynsky, Operating Engineer
  • 8. Zank, Operating Engineer
  • J. Williams, Operating Engineer
  • R. Stobert, Operating Engineer

T. Mohr, Operating Engineer

  • M. Strait, Technical Staff Supervisor

L. Cartwright, Q.C. Supervisor

J. Mayer, Station Security Administrator

D. Morey, Chemistry Services Supervisor

D. Saccomando, Health Physics Services Supervisor

F. Kanwischer, Services Superintendent

  • D. Gulati, Master Instrument Mechanic
  • 8. Viehl, Nuclear Engineering Department Supervisor
  • K. Yates, Onsite Nuclear Safety Group Administrator

K. Kociuba, Nuclear Quality Programs Superintendent

  • T. Gallaher, Nuclear Quality Programs Engineer
  • Denotes those attending the exit interview conducted on June 28, 1991,

and at other times throughout the inspection period.

The inspectors also talked with and interviewed several other licensee

employees, including members of the technical and engineering staffs,

reactor and auxiliary operators, shift engineers and foremen, electrical,

mechanical and instrument maintenance personnel, and contract security

personnel.

2.

Previously Identified Inspection Items (92701 and 92702)

(Open) Open

I~em (50-237/90027-14(DRP)):

Perform sample inspection of

Systematic Evaluation Program (SEP) topic resolutions.

The inspector

completed verification of an SEP item during this inspection period as

discussed in paragraph 10.

This open item will remain open for remaining

SEP items pending completion of licensee confirmation of topic closures

and verification by the resident staff.

(Closed) Open Item (50-237/91003-03(DRP)):

Review the root cause and

planned corrective actions of an Advanced Nuclear Fuels (ANF) Spent Fuel

Pool (SFP) reload calculational error.

The error resulted from an ANF

3

core management engineer selecting the wrong xenon condition for the SFP

K-infinity calculation.

The error was not identified by CECo engineers

because their review was based on verifying that the K-infinity value was

reasonable and within Technical Specification requirements.

Planned

corrective actions included enhanced awareness within the ANF neutronics

team, regarding the quality of its work product, a change in calculational

methodology to reduce input requirements and the addition of a checklist

to provide greater sensitivity to calculational parameters.

In addition,

the Dresden Nuclear Engineering Group will develop formal guidelines for

reviewing reload documents.

The inspectors have no other concerns in

this area.

(Closed)

Unresolved Item (50-237/91009-03(DRP)):

Temporary alteration

(TA-II-7-91) on the Unit 2 high pressure coolant injection (HPCI) system

provided a direct interface between class IE electrical equipment and

non-safety measuring and test equip~ent (M&TE).

The 10 CFR 50.59 safety

evaluation for the temporary alteration did not address the potential

degradation of the Class IE circuit as a result of the interface.

The

issue was unresolved pending clarification of a March 6, 1985, CECo

commitment (letter from 8. Rybak (CECo) to R. Gilbert, (NRR)) to

incorporate the isolation philosophy of IEEE-384 and Regulatory Guide 1.75

for plant modifications whenever practical.

Subsequently, the NRC

concluded that IEEE 384 should have been considered in the safety

evaluation process.

The failure to consider the probability of an

occurrence of a malfunction of equipment important to safety in the

temporary alterations safety evaluation is considered a violation

(50-237/91016-0l(DRP)) of 10 CFR 50.59.

The root cause of the violation

was a failure of the plant staff to recognize the need to evaluate and

incorporate the requirements of IEEE-384 into the safety evaluation

process.

Following NRC identification of this concern, Dresden Administrative

Procedure (OAP) 10-02,

11 10 CFR 50.59 Reviews Screening and Safety

Evaluation,

11 was revised to incorporate a Safety Evaluation/Screening

Review Worksheet which specifically addressed electrical separation

criteria.

Also, in response to a previous violation (50-237/90022-01) of

10 CFR 50.59, CECo committed to implement a program to rebaseline the

Updated Final Safety Analysis Report (UFSAR).

The rebaseline scope should

include all applicable correspondence associated with the Integrated Plant

Safety Assessment Systematic Evaluation Program (SEP).

The licensee

indicated that the UFSAR would be prepared in accordance with Regulatory

Guide 1.70, "Standard Format and Content of Safety Analysis Reports for

Nuclear Power Plants", Revision 3, which specifically addressed Regulatory

Guide 1.75 electric separation requirements.

This issue was considered to

be of minimum safety significance and the appropriate corrective actions

were completed or planned prior to the end of the inspection period.

'Therefore, a Notice of Violation is not being issued in accordance with

10 CFR 2, Appendix C, Section V.A.

The inspectors have no further

concerns in this area.

(Closed) Unresolved Item (50-237/91010-03(DRP)):

The inspector noted that

several safety-related pressure switches which provided input to the

reactor building ventilation air operated isolation damper/closure logic

4

circuitry for Units 2 and 3 were not included in a periodic calibration

program.

These switches were associated with the following components:

2(3)-1601-21

2(3)~1601-22

2(3)-1601-56

2(3)-1601-60

2(3)-1601-23

2(3)-1601-24

2(3)-1601-63

2(3)-5741A(B)

2(3)-5742A(B)

Drywell Purge Inboard Primary Containment (PC)

Isolation Valve

Drywell Purge Outboard (PC) Isolation Valve

Torus Purge (PC) Isolation Valve

Torus Vent (PC) Isolation Valve

Drywell Vent Inboard (PC) Isolation Valve

Drywell Vent (PC) Outboard Isolation Valve

Drywell SBGT (PC) Isolation Valve

Reactor Building Ventilation System (RBVS)

Secondary Containment Isolation Valve

RBVS Secondary Containment Isolation Valve

UFSAR section 5.2.2.6 indicated that air operated valves, which close for

the normal containment isolation mode, failed closed on loss of motive

force.

Although not specifically mentioned in the UFSAR, this function

also was designed for the RBVS isolation valves, in light of the

importance of valve closure to standby gas treatment system (SGTS)

operability.

The pressure switches provided the closure signal prior to

system pressure becoming sufficiently low such that normal system air

would not close the valve under isolation conditions.

Although these switches did receive periodic functional testing, this

alone would not ensure the absence of accumulated non-conservative

setpoint drift over repeated testing intervals.

The licensee had not

determined a minimum setpoint required to ensure sufficient air pressure

to close the valves, the expected drift over a period of time, or an

acceptable calibration interval.

Finally, the licensee had not performed

an analysis to justify the absence of periodic calibration requirements.

Failure to establish these safety-related devices in the test program for

calibrations is a violation (50-237/91016-02(DRP)) of 10 CFR 50, Appendix 8,

Criterion XI.

The inspectors noted that local flow indication for the Unit 2 emergency

diesel generator cooling water lines, installed by modification

Ml2-2-87-054 to meet a Regulatory Guide (RG) 1.97 commitment was also not

in a periodic calibration program.

The new flowmeter was to be used for

inservice testing (IST) testing measurements because of the difficulty in

utilizing installed instrumentation.

Failure to include this device

within the periodic test program for calibrations is another example of

violation 50-237/91016-2(DRP).

One cited and one non-cited violation and no deviations were identified

in this area.

3.

Licensee Event Reports Followup (90712 and 92700)

Through direct observations, discussions with licensee personnel, and

review of records, the following event reports were reviewed to determine

5

that reportability requirements were fulfilled, immediate corrective

action was accomplished, and corrective action to prevent recurrence had

been accomplished in accordance with Technical Specifications.

(Closed) LER 50-237/91002 - Reactor Head Closure Stud Outside FSAR

Allowables for Material Toughness Due to Unknown Cause.

On

January 16, 1991, with Unit 2 in a refueling outage, the licensee

determined through analysis that a reactor head closure stud replaced

during a previous outage did not meet the material toughness requirements

of the FSAR, Appendix D, paragraph 10.10.

The LER was submitted for any condition that resulted in the plant being

outside the design basis (10 CFR 50.73(a)(2)(ii)(B)).

Not meeting the

material specification for a primary cooling system pressure boundary

represented a principal safety barrier in a unanalyzed condition and

outside the design basis.

Requirements for immediate notifications for

operating reactors, 10 CFR 50.72(b)(2)(i), also required notification

within four hours of any event that, if found while operating, would have

resulted in its principal safety barriers being seriously degraded, or

being in an unanalyzed condition, that significantly compromises plant

safety.

This four hour notification was not made and was considered a

violation (50-237/91016-03(DRP)) of reporting requirements.

Subsequent

licensee engineering analysis, completed on March 22, 1991, concluded

that sufficient structural margin existed for operation of the reactor.

Also, the inspector reviewed the licensee's Deviation reports (DVRs)

generated during the inspection period for potential adverse trends in

personnel and equipment performances.

DVRs were also reviewed for

initiation and disposition as required by the applicable procedures and the

QA manual.

One cited violation and no deviations were identified in this area.

4.

Operational Safety Verification (71707 and 42700)

During the inspection period the inspectors verified daily, and randomly

during back shift and on weekends, that the facility was being operated

in conformance with the licenses and regulatory requirements and that the

licensee's management control system was effectively carrying out its

responsibilities for safe operation.

This was done on a sampling basis

through routine direct observation of activities and equipment, tours of

the facility, interviews and discussions with licensee personnel,

independent verification of safety *system status and limiting conditions

for operation action requirements (LCOs), corrective action, and review

of facility records.

On a sampling basis the inspectors daily verified proper control room

staffing and access, operator behavior, and coordination of plant

activities with ongoing control room operations; verified operator

adherence with the latest revisions of procedures for ongoing activities;

verified operation as required by Technical Specifications (TS);

including compliance with LCOs, with emphasis on engineered safety

6

features (ESF) and ESF electrical alignment and valve positions;

monitored instrumentation recorder traces and duplicate channels for

abnormalities; verified status of various lit annunciators for operator

understanding, off-normal condition, and corrective actions being taken;

examined nuclear instrumentation (NI) and other protection channels for

proper operability; reviewed radiation monitors and stack monitors for

abnormal conditions; verified that onsite and offsite power was available

as required; observed the frequency of plant/control room visits by the

station manager, superintendents, assistant superintendents, and other

managers; and observed the Safety Parameter Display System (SPDS) for

operability.

During tours of accessible areas of the plant, the inspectors made note

of general plant/equipment conditions, including control of activities in

progress (maintenance/surveillance), observation of shift turnovers,

general safety items, etc.

The specific areas observed were:

a.

Engineered Safety Features (ESF) Systems

Accessible portions of ESF systems and components were inspected to

verify:

valve position for proper flow path; proper alignment of

power supply breakers or fuses (if visible) for proper actuation on

an initiating signal; proper removal of power from components if

required by TS or FSAR; and the operability of support systems

essential to system actuation or performance through observation of

instrumentation and/or proper valve alignment.

The inspectors also

visually inspected components for leakage, proper lubrication,

cooling water ~upply, etc.

b.

Radiation Protection Controls

The inspectors verified that workers were following health physics

procedures for dosimetry, protective clothing, frisking, posting,

etc., and randomly examined radiation protection instrumentation for

use, operability, and calibration.

c.

Security

Each week during routine activities or tours, the inspector

monitored the licensee's security program to ensure that observed

actions were being implemented according to their approved security

plan.

The inspector noted that persons within the protected area

displayed proper photo-identification badges and those individuals

requiring escorts were properly escorted.

The inspector also

verified that checked vital areas were locked and alarmed.

d.

Housekeeping and Plant Cleanliness

The inspectors monitored the status of housekeeping and plant

cleanliness for fire protection, prote~tion of safety-related

equipment from intrusion of foreign matter and general protection of

equipment from hazards.

7

e.

Plant Procedure Review

The inspector reviewed approximately 100 temporary changes made to

various procedures and concluded that the corresponding safety

evaluations met the requirements of Dresden Administrative Procedure

(OAP) 10-02,

11 10 CFR 50.59 Review Screening -and Safety Evaluation, 11

OAP 09-06,

11Temporary Changes to Procedures 11 and 10 CFR 50.59.

The

evaluations provided an adequate bases for determining that an

unreviewed safety question did not exist.

The inspectors also monitored various records, such as tagouts, jumpers,

shiftly logs and surve~llances, daily orders, maintenance items, various

chemistry and radiological sampling and analysis, third party review-

results, overtime records, QA and/or QC audit results, and postings -

required per 10 CFR 19.11.

No violations or deviations were identified in this area.

5.

Monthly Maintenance Observation (62703)

Station maintenance activities affecting the safety-related systems and

components listed below were observed/reviewed to ascertain that they

were conducted in accordance with approved procedures, regulatory guides,

and industry codes or standards and in conformance with Technical

Specifications.

The following items were considered during this review:

the Limiting

Conditions for Operation (LCOs) were met while components or systems w~re

removed from service; approyals were obtained prior to initiating- the

work; activities were accomplished using approved procedures and were

inspected as applicable; functional testing and/or calibrations were

performed prior to returning components or systems to service; quality

control records were maintained; activities were accomplished by

qualified personnel; parts and materials _used were properly certified;

radiological controls were implemented; and, fire prevention controls

were implemented.

Work requests were reviewed to determine status of

outstanding jobs and to assure that priority is assigned to

safety-related equipment maintenance which may affect system performance.

The inspectors monitored the licensee's work in progress and verified

that it was being performed in accordance with proper procedures, and

approved work packag~s, that applicable drawing updates were made and/or

planned, and that operator training was conducted in a reasonable period

of time.

The following maintenance activities were observed and reviewed:

Unit 2

Rebuild of Diesel Generator Air Start Motors

125v DC Ground Checking

8

Unit 3

Repair of the 3B LPCI Heat Exchanger Bypass Valve (3-1501-llB)

Repair of the 3C Instrument Air Compressor

No violations or deviations were identified in this area.

6.

Monthly Surveillance Observation (61726)

The inspectors observed surveillance testing required by Technical

Specifications during the inspection period and verified that testing was

performed in accordance with adequate procedures, that test

instrumentation was calibrated, that LCOs were met, that removal and

restoration of the affected components were accomplished, that results

conformed with Technical Specifications and procedure requirements were

reviewed by personnel other than the individual directing the test, and

that any deficiencies identified during the testing were properly

reviewed and resolved by appropriate management personnel.

The inspectors witnessed portions of the following test activities:

Unit 2

DOS 6600-1, Diesel Generator 2/3 Monthly Operability Run

DIS 1500-18, Low Pressure Cooling Injection (LPCI) Monthly Flow

Calibration Surveillance

DOS 1500-2, Quarterly Containment Cooling Service Water Pump Test

for Inservice Test (IST) Program

DOS 1500-3, Containment Cooling Service Water Pump Test

DOS 1500-6, LPCI System Pump Operability Test with Torus Available

DOS 1500-5, LPCI System Quarterly Flow Rate Test

DOS 1500-10, Quarterly LPCI Pump Operability Test with Torus

Available for the IST Program

Unit 3

DOS 6600-1, Diesel Generator 3 Monthly Operability Run

DOS 1400-1, Core Spray Pump 3A Test with Torus Available

DOS 1600-1, Quarterly Valve Timing

DOS 1600-2, Valve Operability Check

DOS-250-1,

Main Steam Isolation Valve (MSIV) 10% Closure

DOS 300-1,

Control Rod Drive Exercise

DOS 500-3,

Average Power Range Monitor (APRM) Rod Block and Scram

Functional Test

DOS 5600-2, Monthly and Weekly Turbine Checks

During the performance of quarterly LPCI and core spray surveillances,

the inspector noted that one Nuclear Station Operator (NSO) was keeping

track of procedural evolutions and data recording in as many as five

procedures at one time.

The inspector identified this complex procedural

matter to the licensee.

The licensee indicated that the matter will be

evaluated for streamlining .

9

While reviewing diesel generator (DIG) surveillance activities, the

inspector questioned the D/G output breaker logic design.

During

conditions when the output breaker was closed~ such as the case during*

full load testing, a DIG overload condition could develop following the

loss of offsite power (LOOP).

Per the UFSAR, following a LOOP

(undervoltage) condition, the engineered safety features bus feeder

breaker opens, the DIG receives a start signal, and load shedding occurs.

The DIG output breaker closes after the D/G reaches rated speed and

voltage.

If a loss of coolant accident (LOCA) signal was present, the

essential loads would be sequenced on to the bus.

However, if the D/G

output breaker was closed prior to the LOOP, the bus voltage may be

maintained above the undervoltage (UV) relay trip settings.

The added

demand resulting from the connection of non-safety/non-essential loads

would result in an overload condition of the D/G.

If the LOOP condition

was coincident with an accident signal, then the D/G protective devices,

except generator fault and mechanical overspeed, would be disabled.

The

end result could be damage to the D/G units and the total loss of AC

power to .the safety bus.

Current design did not ~rovide for automatic

opening of the D/G output breaker upon a LOCA signal to ensure the initial

undervoltage condition and subsequent load shedding occurs.

During conditions when one of the D/Gs or an offsite pbwer source is

inoperable, Technical Specifications require the operable D/G(s) to be

paralleled to the offsite power system for at least one hour.

In this

case, the Technical Specifications prescribed actions could result in an

increased probability of a station blackout (total loss of AC power).

The

licensee reviewed the concern and concluded that the p~obability of a

spurious accident signal (or design basis event) in conjunction with a

LOOP while all available emergency onsite D/Gs were being operated, was

small.

Also, the licensee considered this scenario reviewed by the NRC

under the SEP.

A review of the General Design Criteria (GDC) 17 Safety Evaluation

Reports (SER) and the Systematic Evaluation Program (SEP) Topic VIII-2,

110nsite Emergency Power Systems (Diesel Generator)

11 indicated system

response, when the D/G output breaker is initially closed,

was not

specifically addressed.

However, Standard Review Plan, Section 8.3.1 and

Regulatory Guide 1.108,

11 Periodic Testing of Diesel Generator Units Used

as Onsite Electric Power Systems at Nuclear Power Plants

11 , referenced as

review criteria specified that periodic testing of the D/G units should

not impair the capability of the unit to respond to challenges within the

required time. This issue is considered an open item (50-237/91016-04(DRS))

pending on NRC determination of whether the current DIG breaker logic

design is consistent with existing regulations/commitments.

No violations or deviations were identified.

7.

Safety Assessment and Quality Verification (35502 and 40500)

Inspectors were given a presentation by the Onsite Nuclear Safety Group

(ONSG) which included a discussion of activities ongoing within ONSG.

One of these activities included a program entitled

11 Lessons Learned

10

Initial Notification.

11

This program provided subjective information on

significant events at other CECo nuclear plants which would be

disseminated to all the CECo nuclear stations within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of its

occurrence.

Such information provided an enhanced level of awareness for

the remaining faciliti.es, and lowered the probability for recurrence of

the same type event at another nuclear unit.

No violations or deviations were identified in this area.

8.

Events ( 93702)

a.

Between May 16 and May 29, 1991, the Unit 2 circulating water (CW)

inlet temperature indication reflected a value in excess of

95 degrees F.

The inspector asked whether the CW inlet temperature

was representative of the ultimate heat sink temperature available to

the LPCI and DIG heat exchanger following a design basis event due to

the relative locations of the suction sources.

The LPCI and the

dies~l generator heat removal analysis were bounded by 95 F cooling

water.

In a response to the concern, the licensee performed

independent temperature monitoring at the 28 LPCI heat exchanger and

at the crib house to verify actual inlet temperature was less than or

equal to 95 F.

In addition, the results of the special test was used

to reference the screen house temperature recorder to ensure the

design basis temperature limit of 95 degree F is not exceeded in the

future.

b.

On June 9, 1991, a Unit 2 reactor scram occurred from 42 percent

rated thermal power due to high reactor pressure.

The pressure

transient resulted from an unexpected turbine trip while performing

the weekly surveillance on the turbine thrust bearing wear detector.

All turbine bypass valves performed as designed; however, the scram

setpoint was still reached.

During the two minutes between the

turbine trip and reactor scram, control room operators partially

inserted one control rod in an attempt to limit the reactor

power/pressure transient.

The turbine trip resulted from the thrust bearing wear detector

being out of adjustment when the trip setpoint was reached prior to

activation of the bypass testing interlock.

Although data from

earlier steps in the surveillance could have alerted the operators to

a danger of continuing the test, the procedure did not alert the

operators to the signif1cance of this data.

The need for detector

adjustment had been identified in earlier surveillances and a work

request was written, but the work was delayed.

This adjustment was

made following the scram.

The inspector will r~view the licensees' post scram investigation

process and scram report when generated.

c.

On June 13, 1991, during the routine calibration surveillance, two

emergency core cooling system (ECCS) level switches and were found

non-conservatively out of calibration.

These switches were

recalibrated as part of the same procedure.

The switches (one out of

11

two taken twice logic) provided input into the core spray system and

low pressure coolant injection system initiatiori logic.

The two

other switches in the trip system were within tolerance.

The time

of discovery for the out-of-tolerence switches was recorded on the

deviation report as 8:00 p.m. on June 13, 1991.

The SCRE received

the.DVR sometime after the shift turnover (approximately 11:00 p.m.)

and notified the NRC via the Emergency Notification System at

00:52 a.m. on June 14, 1991.

At the time of notification, the licensee believed that the two

out-of-tolerance switches would have resulted in ECCS actuation at

1/2 inch of reactor vessel level below the TS specified setpoint.

Based on this, the ENS call was made as a 24-hour requirement for a

violation of TS as required by the operating license, condition 2.G.

The justification provided on the DVR for classifying the call was

that activation would be 1/2 inch below the setpoint.

Further. review by the licensee found that the actual logic

arrangement ihcluded parallel switches which would have provided the

ECCS actuation within the required level setpoints.

Based on this

information, this event was no longer reportable and the licensee

withdrew the notification call.

Review by the NRC concluded that the event, as interpreted at the

time, would have required a 4-hour notification in accordance with

10 CFR 50.72 (b)(2)(iii)(D) for any condition that alone could have

prevented the safety function of a system needed to mitigate the

consequences of an accident.

Once the operating shift evaluated the

consequences of the out of calibration switches, contact via the ENS

was made in less than 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

However:

(1)

(2)

(3)

Transmittal of information from the IM staff to the operating

staff was not timely; nor was assessment of the impact such as

the direction or magnitude of the setpoint drift provided in

the DVR.

The operations staff did not appear to have

aggressively pursued the ramifications of the DVR until after

shift turnover.

The operations staff did not accurately assess the implication

of the two switches being out-of-toi'erance.

The SCRE 1 s

knowledge of ECCS logic appeared to be weak.

A sound engineering basis was not provided in classifying this

event as a license condition instead of 10 CFR 50.72.

It

appears that instead of an engineering judgement, a great deal

of discussion was held with plant managers which concluded with

a decision that the condition did not meet a limiting safety

system setpoint as defined in 10 CFR 50.36.

10 CFR 50.36

references reportability in accordance with 50.72.

No violations or deviations were identified in this area.

12

Training Effectiveness (41400, 41701)

The effectiveness of training programs for licensed and non-licensed

personnel was reviewed by the inspectors during the witnessing of the

licensee

1 s performance of routine surveillance, maintenance, and

operational activities and during the review of the licensee 1s response

to events which occurred during the inspection period.

Personnel

appeared to be knowledgeable of the tasks being performed, and nothing

was observed which indicated any ineffectiveness of training.

No violations or deviations were identified in this area.

10.

Systematic Evaluation Program Items (92701)

NUREG 1403,

11Safety Evaluation Report Related to the Full-term Operating

License for Dresden Nuclear Power Station, 11 Table 2.1, identified 22 SEP

Integrated Plant Safety Assessment Report (IPSAR) topic resolutions to be

confirmed by the NRC Region III office.

The following item in that report was confirmed as closed by the

inspectors:

Item 6 - Topic VI-4/4.18.6

The completion for Item 2 for Topic II-3.b.l/4.l.4 is being tracked as

Open Item 50-237/89019-04.

The following three items remain to be verified

as closed by the licensee and confirmed by the NRC.

They are tracked

under Open Item (50-237/90027-14(DRP)).

Item 13 - Topic III-2/2.2.2 (Supp. 1)

Item 14 - Topic III-4.A/4.5.3 and 2.2.2 (Supp. 1)

Item 16 - Topic VI-4/4.18.2; Topic VI-6/4.19

Each of these items were in some stage of verification review by the

licensee.

No violations or deviations were identified.

11.

Report Review (90713)

During the inspection period, the inspector reviewed the licensee's

Monthly Operating Report for April 1991.

The inspector confirmed that

the information provided met the requirements of Technical Specification 6.6.A.3 and Regulatory Guide 1.16.

The inspector also reviewed the

Dresden Nuclear Power Station Monthly Plant Status Report for April 1991.

A NRC specialist inspector reviewed the D2R12 IS! report of activities

performed from September 23, 1990 through February 10, 1991, and determined

that the data presented in the !SI report was consist~nt with inspector

observations documented in inspection report 50-237/90024(DRS).

No violation~ or deviations were ide~tified.

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' *

12.

13.

OQen Items

Open items are matters which have been discussed with the licensee which

will be further reviewed by the inspector and which involved some actions

on the part of the NR~ or licensee or both.

Open items disclosed during

the inspection are discussed in paragraph 6.

Exit Interview

The inspectors met with licensee representatives (denoted in paragraph 1)

during the inspection period and at the conclusion of the inspection

period on June 28, 1991.

The inspectors summarized the scope and results

of the inspection and discussed the likely content of this inspection

report.

The licensee acknowledged the information and did not indicate

that any of the information disclosed during the inspection could be

considered proprietary in nature.

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