ML17056B968
| ML17056B968 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 08/25/1992 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17056B969 | List: |
| References | |
| 50-220-91-99, 50-410-91-99, NUDOCS 9209010185 | |
| Download: ML17056B968 (72) | |
See also: IR 05000220/1991099
Text
ENCLOSURE
SALP REPORT
V.S. NUCLEARREGULATORYCOMMISSION
4
REGION I
~~ AEQ~~
~o
Cy
SYSTEMATIC ASSESSMENT OF LICENSEE
PERFOMIAINCE
REPORT NOS. 50-220/91-99 AlND50-410/91-99
NjlAGAI4kMOHAWKPOWFK CORPORATION
NIIMMILEPOINT XPlITS 1 AND 2
ASSESSMENT PERIOD: APKE 1, 1991 - MAY23, 1992
BOARD MEETINGDATE: JULY 9, 1992
9209010185
920825
ADOCK 05000220
8
4
(1
TABLEOF CONT1PlTS
INTRODUCTION
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
1
II.
SUMMARYOF RESULTS................
II,,A
Overview
II.B
Facility Performance Analysis Summary....
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
2
2
4
IV.
PERFORMANCE ANALYSIS..............
III.A Plant Operations
III.A.1
Unit 1
III.A.2
Unit 2-
III.B Radiological Controls
III.C
Maintenance/Surveillance
.- .. ~.........
III.D Emergency Preparedness
III.E
Security
III.F
Engineering/Technical Support
III.G
Safety Assessment/Quality Verification.....
SITE ACTIVITIESAND EVALUATIONCRITERIA
IV.A Licensee Activities.................
IV.B
Unplanned Shutdowns, Plant Trips and Forced
IV.C NRC Inspection and Review Activities.....
IV.D Escalated Enforcement Action ..........
IV.E
SALP Evaluation Criteria.............
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
Outages
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
5
5
5
7
10
12
~
18
21
23
26
29
29
29
31
32
32
It
I.
INTRODUCTION
4
The Systematic Assessment of Licensee Performance (SALP) is a periodic, integrated Nuclear,
Regulatory Commission (NRC) staff effort to evaluate licensee performance on the basis of
'collected observations
and data.
The SALP process
is supplemental
to normal regulatory
processes
used to ensure compliance with NRC rules and regulations.
SALP is to be sufficiently
diagnostic to provide a rational basis for allocating NRC resources
and to provide meaningful
feedback to licensee management
to promote quality and safety of plant operations.
An NRC SALP Board, composed of the staff members listed below, met on July 9, 1992, to
assess
the performance of the Niagara Mohawk Power Corporation (NMPC) at Nine MilePoint
Units
1 and 2.
This assessment
was based on the collection of performance observations
and
data for the period of April 1, 1991, to May 23, 1992, and was conducted in accordance with
the guidance in NRC Manual Chapter 0516, "Systematic Assessment of Licensee Performance."
A summary of the guidance and evaluation criteria is provided in Section IV.Ein the Supporting
Data of this report.
The SALP Board was composed of:
Chairman:
J. Wiggins, Deputy Director, Division of Reactor Projects (DRP)
Members:
W. Lanning, Deputy Director, Division of Reactor Safety (DRS)
J. Durr, Acting Deputy Director, Division of Radiation Safety and Safeguards
(DRSS)
R. Capra, Director; Project Directorate I-l, Office of Nuclear Reactor Regulation (NRR)
L. Nicholson, Chief, Reactor Projects Section No. 1A, DRP
D. Brinkman, Senior Project'Manager, NMP Unit 1, NRR
J. Menning, Project Manager, NMP Unit 2, NRR*
W. Schmidt, Senior Resident Inspector, DRP
Each of the Project Managers supplied a vote in the determination of the Category Rating
for their respective units in the Plant Operations functional area,
In the other functional
areas the Project Managers provided one vote which represented
their consensus
on the
Category Rating.,
Others in Attendance
C. Cowgill, Chief, Projects Branch No. 1, DRP
R. Laura, Resident Inspector
W. Mattingly, Resident Inspector
C. Beardslee,
Reactor Inspector, Intern
II.
SUMMARYOF RESULTS
U.A Overview
During this period, performance was generally good and both plants continued to be operated
safely. However, some instances ofinattention-to-detail and failure to followprocedures caused
problems.
These instances indicated that NMPC had not been fullyeffective at correcting these
longstanding performance
issues.
While the number of reactor scrams
caused by personnel
errors was very low, the total number of scrams caused by equipment failures, particularly at
Unit 1, was high.
Good operator response
to the events ensured the continued safe operation
of the plants.
Overall the functional area
category
ratings
were consistent
with the last SALP period.
However,
a
declining
performance
trend,
since
the
last
period,
was
noted
in
the
Maintenance/Surveillance
functional areas.
In the Operations area, Unit 1 staff demonstrated
good performance and exhibited good safety
perspective in routine operations and in responding to challenges caused by equipment failures.
However, operating shifts were involved in the isolation of the unit from its ultimate heat sink
and in the inadvertent bypassing of a reactor protection system function. Incr'eased management
attention to these concerns was observed late in the assessment
period.
The Unit 2 operations
staff demonstrated
very good performance
and competently
maintained
the plant in a'safe
condition.
Some minor incidents of inattention-to-details occurred, but management
continued
strong, effective oversight of activities, and implemented good corrective action.
In the Radiological Controls area, an effective ALARAprogram continued to be maintained at
Unit 1, with significant improvements made in this area at Unit2. Some weaknesses
were noted
in the radiological controls program at both units. The radwaste transportation and radiological
environmental monitoring program for both units continue to be strong.
The liquid and gaseous
effluent control programs continue to be very effective. Management attention and commitment
to safety were noted in this area.
In the Maintenance
and Surveillance
area, -the Unit
1 staff demonstrated
generally
good
performance.
However, this overall performance
was overshadowed
by a breakdown in the
implementation of the maintenance work control program which led to*the isolation of the unit
from its ultimate heat sink. Unit 1 staff effectively implemented the'surveillance test program.
The Unit 2 maintenance
staff also showed good performance
and demonstrated
proper safety
perspective.
There were however,
a few instances of poor work practices and inattention-to-
detail, which included
dropping two new fuel bundles.
The Unit 2 staff appropriately
implemented the surveillance program, contributing to the safe operation of the plant.
Overall,
the maintenance
and surveillance programs were effectively implemented.
However, a decline
in performance at both units was observed due to an increased number of equipment failures and
significant personnel errors.
Performance in the Emergency Preparedness
area continues to be excellent. The implementation,
, of the Site Emergency Plan (SEP) was observed during drills and actual events and found to be
excellent.
NMPC continues to maintain an effective drill/exercise program and well qualified
station and corporate management.'he
emergency response facilities, equipment, and supplies
were very well maintained.
However,
a declining trend
was
noted
since
management
'involvement was not always evident in the timely resolution of several issues which have either
been recurring or open for long periods of time.
The Security program continued to be a strength; this consistent performance over previous
SALP periods was recognized by the board. The program was performance-based
and was
effectively implemented. The training program was well developed'and administered. Significant
upgrades
completed demonstrated
management
commitment to maintaining a.state of the art
security program.
In the Engineering/Technical
Support area, the engineering staff continued the support of safe
plant operations with high quality work. The engineering department took effective actions to
improve the oversight, quality, and timeliness of its products.
Some instances of inadequate
engineering
involvement during unplanned
events,
such
as the inadvertent isolation of the
ultimate heat sink at Unit l, were noted. There were also some instances of inadequate control
over temporary modifications and inconsistences
in the quality of submittals to the NRC. The
training. program
was
improving
and
seemed
comprehensive.
Increased
management
involvement, controls, and initiatives to assure quality of engineering products were noted.
In the Safety Assessment/Quality
Verification area, good management
oversight and extensive
supervisor involvement in activities were noted.
Normal oversight group activities and quality
assurance
department activities were good..However, in some cases management failed to take
effective actions on quality assurance identified deficiencies.
Further, as noted above, personnel
performance issues and equipment failure continued to cause problems at both units.
II.B Facility Performance Analysis Summary
F N TI NALAREA
1 ~
Plant Operations - Unit 1 '
Plant Operations - Unit 2
Rating, Trend
L~ar Period
2
2
Rating, Trend
~Thi
Period
2
2
2.
Radiological Controls
3.
Maintenance/Surveillance
4.
2 (Declining)
1 (Declining)
5.
Security
6.
Engineering/Technical
Support
7.
Safety Assessment
and
Quality Verification
2.
Previous Assessment
Period:
March 1, 1990 through March 31, 1991
Present Assessment
Period:
April 1, 1991 through May 23, 1992
III.
PERFORIVGLNCE ANALYSIS
III.A
III.A.1
Plant Operations
Vnit 1
During the previous SALP period, Unit 1 Plant Operations was rated as Category 2. The Unit 1
operations department demonstrated
significant improvement in performance.
The operations
staff successfully met the challenges of a transition from the prolonged shutdown, through the
extensive
power
ascension
test program
(PATP), to full power operations.
Operations
management
improved
oversight
and
assessment
capabilities
as
reflected
in the PATP
self-assessment
and the successful application of lessons learned.
III.A.1.1
Analysis
Overall, the Unit 1 operations staff demonstrated
good performance
during this assessment
period.
The operators performed well despite challenging equipment failures.
A good safety
perspective was evident during routine plant operations.
However, the isolation of the ultimate
heat sink and the failure to address
a problem with the reactor protection system reflected
significant weaknesses
in adherence
to program requirements
and attention-to-detail
~ Strengths
were noted in training and operations support.
Strong performance was demonstrated by the absence ofunplanned shutdowns or reactor scrams
resulting from operator error.
In addition, operators
responded
well when challenged
by
equipment failures, which caused five of six automatic reactor scrams and one forced shutdown.
The remaining reactor scram occurred when an operator closed the main steam line drain valves,
in accordance with procedure,
at low power during a shutdown.
The procedure was changed
to prevent closing these valves at low power levels.
Excellent operator response
to these
shutdowns maintained the unit in a safe condition.
Several other equipment failures did not
result in plant transients
due to prompt identification and very effective operator actions.
In
another instance, early detection and trending of an increasing unidentified drywell leakage rate
allowed for shutdown of the unit before exceeding the technical specification limit.
Operators exhibited a good safety perspective during the conduct of routine plant operations.
During rounds,
operators
identified equipment problems
and initiated work requests
and/or
deviation event reports to obtain corrective actions.
Operators responded promptly to alarms
according
to response
procedures.
Control room briefings conducted
by the station shift
supervisor at the start of each shift provided a sufficient amount of information to understand
the shift goals and objectives.
Utilization of repeat-backs
during oral communications and use
of self-checking techniques resulted in better control ofoperational activities. The performance
ofroutine activities in a professional manner demonstrated
good operator attitudes and the desire
for error-free operation.
Also, significant improvement late in the period in the content and
quality ofoperator logs, including the documentation of the basis for operability determinations,
allowed operators
and management
to maintain better awareness of plant activities.
Eg
t
Two significant instances ofpoor operator performance occurred during non-routine evolutions.
. A temporary loss of the ultimate heat sink resulted, in part', from an inadequate plant impact
assessment
of a maintenance
activity in that the operating crew did not fully consider
the
potential consequences
of testing a screenhouse
gate while shutdown.
Also, an improper
assessment of a turbine first stage pressure annunciator resulted in operation with less than the
minimum technical specification required reactor protective instrumentation.
Operators failed
to recognize the significance of the annunciator and thus, did not record this event in operating
logs and did not initiate a deviation/event report to obtain corrective actions.
An inadequate
annunciator response procedure and weak training in the design of the reactor protection system
turbine first stage pressure switches contributed to this event. Collectively, these events indicate
that operations management
was less than fullyeffective in enforcing adherence
to established
program requirements
and attention-to-detail when performing plant impact assessments,
In response to these and other minor problems, prompt corrective actions were taken.
Further,
the operations
department
conducted
an
assessment
of its effectiveness
at analyzing
and
controlling plant operations.
A reorganization of operations
supervision and crew personnel
better matched
operator experience
levels and leadership
abilities.
Training on procedural
adherence
and attention-to-detail resulted in better operator awareness of system status.
Operations
management
implemented
several
new
initiatives
to
improve
performance,
Relocation of the station shift supervisor and assistant station shift supervisor desks provided for
inc'reased
visibility and oversight of control room activities.
The implementation of an
operations
department
self-assessment
program
was
an
excellent
initiative to
identify
performance
trends and initiate corrective actions when warranted.
However, this initiative
needed further development to become fullyeffective. To allow more focused attention on the
reduction of control room deficiencies, the operations manager developed a deficiency tracking
and trending program for meters, annunciators,
chart recorders
and components.
The long term effectiveness of the above corrective actions remains a concern because of the
long-standing
nature of the deficiencies
involved.
Improvements
to attention-to-detail
and
procedural adherence
were principle elements of the licensee's
Results Improvement Program
and the Nuclear Business Plans.
Although routine operations performance was generally good,
the performance breakdowns during non-routine evolutions indicate that additional management
attention is warranted.
The total number of licensed
operators
remained
consistent with the previous period and
supported
a five shift rotation
bolstered
by a permanent
day-shift relief crew.
The
implementation of a separate shift technical advisor position allowed the assistant
station shift
supervisor to be more effective in directing activities during operational
events.
An NRC
requalification program evaluation examined
13 operators who successfully passed all portions
of the examinations.
The requalification training program attained a satisfactory rating with no
generic weaknesses,
which indicated that NMPC continued to maintain an effective training
program.
The radwaste
operations
and fire protection personnel
performed well this period.
The
operations
support
group
assisted
in resolution of complex technical
issues
such
as
the
emergency
ventilation testing issue.
Good performance of these groups indicated effective
operations management
involvement and oversight.
umma
-
ni
1 Plan
In summary, Unit 1 operations personnel performed well with some notable exceptions.
Good
performance was evident during operator response to equipment failures, problem identification,,
and routine plant operations.
In two instances,
weaknesses
in plant impact determinations and
procedural adherence
caused plant problems.
The operator training department performed well
and strong management
oversight was evident.
III.A.1.2
Performance Rating:
Category
2
III.A.1.3
Board Comment:
The occurrence ofproblems with procedural adherence
and
attention-to-detail suggest that the licensee's past actions to
address these long-standing performance problems have not
been
fully effective.
Continued
licensee
and
NRC
emphasis in these areas is appropriate,
III.A.2
Unit 2
The previous SALP report rated Unit 2 Plant Operations
as Category 2.
Overall performance
was good, having improved substantially. While several personnel errors occurred, they resulted
in events of low safety
significance and were not indicative of poor operating
practices.
Licensed operators understanding ofand ability to use the emergency operating procedures were
considered
strengths and indicated effective training.
III.A.2.1
Analysis
The Unit 2 operations department continued to perform well this assessment
period.
Operating
crews successfully responded
to several challenging events.
Operator response
to scrams and
forced shutdowns
was prompt and proper, however,
one scram
was the direct result of an
operator error. Routine operation ofthe plant was generally good, with only occasional isolated
instances ofoperator inattention-to-detail.
The operations department management
changes and
the assistant station shift supervisor watch station relocation, as discussed below, were positive
initiatives.
Management continued noteworthy involvement in daily activities.
The operator
training and requalification programs supported safe operation of the plant.
The operating
crews
generally
responded
well to challenging
plant transients.
A main
transformer fault in August 1991, caused
a turbine trip, reactor scram,
and a simultaneous
common-mode loss offive non-safety related uninterruptible power supplies (UPS) that powered
non-safety
related control room instrumentation
and plant equipment.
The NRC Incident
Investigation Team which reviewed this event determined that the operators correctly classified
these circumstances
as a Site Area Emergency
and properly completed
many high priority
actions in a high stress,
time-sensitive environment, while many of their normal indicato'rs,
alarms,
and communications were misleading or not available.
The operators
diagnosed
the
instrumentation losses as UPS-related and then promptly restored the UPS loads.
In summary,
the operators successfully coped with this difficultsituation.
Operators performed well during the March 1992 loss of both 115kV off-site power lines, which
caused a second loss of control room annunciators.
The operating crew correctly classified the
loss of control room annunciators
as an Alert.
Operators
relied on incomplete information
provided by technicians after the loss of the first off-site power line, that led to the total loss of
off-site power.
Operators
made reasonable
decisions to restore electrical power following the
complete
loss.
The station shift supervisor
exhibited good command
and control while
conducting plant restoration.
However, the NRC Augmented Inspection Team which reviewed
this event determined that NMPC management
had not adequately considered
the effects of a
loss of off-site power on the instrument air system while shutdown,
the need for enhanced
electrical system recovery procedures,
and the time required for a non-site operator to close the
off-site power breakers.
The team found that, because
these issues were not fully considered,
the operator's
response to this event was unnecessarily
complicated.
The operating crews demonstrated
good performance during the unit startups and shutdowns.
During the three automatic reactor scrams and one forced shutdown, the operators competently
and professionally maintained the plant in a safe configuration.
The operating crews properly
conducted the subsequent
unit startups with excellent communication and supervisory control.
Equipment failures led to two of these
three scrams.
The third scram
resulted
from an
inadequate procedure and a breakdown in communication betw'een the station shift supervisor,
the assistant station shift supervisor,
and the chief shift operator.
Operators
conducted
routine activities in a well controlled
manner.
The operating
staff
satisfactorily controlled component and system status, monitored plant conditions, and identified
problems'during
maintenance,
surveillance,
and
outage
activities,
A diligent operator,
investigating a hissing sound, identified a shattered main generator sight glass leaking hydrogen
into the turbine building. In another example, an operator demonstrated good system knowledge
and a questioning attitude in identifying a problem with the air start receiver pressure during a
tour of an emergency diesel generator room.
Excellent shift crew turnovers, log keeping, and
proper use of the deviation/event report system provided management
with a good awareness
of daily problems and operating concerns.
l
(
In contrast to the above,
several minor instances of personnel
inattention-to-detail occurred
which resulted in several engineered
safety feature actuations,
a configuration control problem
with a secondary containment unit cooler, and a loss of condenser vacuum due to an operator
not following an approved procedure.
Although these instances were minor they indicated that
the actions taken previously by NMPC to address
these performance problems have not been
fully effective, and that there is a continued need for heightened supervisory and management
oversight.
Operations department management demonstrated good performance through aggressive problem
identification and resolution.
Corrective actions developed from event critiques were generally
thorough and appropriately implemented.
NMPC management successfully implemented a self-
assessment
program to detect and correct performance
issues.
Although management
changes
were made, including a new department manager and several new supervisors,
a high level of
experience
and
technical
knowledge
was
maintained.
Moving the assistant
station shift
supervisor from the station shift supervisor's
office to the control room floor enhanced
the
supervisory presence in the control room and allowed both the assistant station shift supervisor
and
station shift supervisor
a more broad
and independent
perspective of the operational
conditions affecting plant safety.
Management
committed
adequate
resources,
regularly
reviewed,
and made satisfactory progress
in reducing the number of nuisance control room
alarms.
The implementation of the operator training and requaliflication programs were effective this
period.
Operator performance following the failure-of the station transformer and the loss of
off-site power events reflected positively on the training department.
Overall, licensed personnel
performed
well during
an NRC-administered
requalification
examination.
Planning
and
administration of the examination
and crew teamwork in the simulator were good.
Ample
staffing existed this assessment
period with the operators in a five-shift crew rotation and a
permanent day-shift relief crew.
ummar
- Unit 2 Plant 0 erations
In summary, the operations department demonstrated
good performance with the exception of
some minor instances of inattention-to-detail.
The operating staff encountered
and successfully
met a number ofsignificant challenges to their capabilities, caused mainly by equipment failures.
Operations department
management
was strongly involved in daily activities.
Staffing levels
were ample and the training department performed well.
III.A.2.2
Performance Rating:
Category
2
t
4
10
III.BRadiological Controls
In the previous SALP period, this functional area was rated as Category 2. Performance in the
area of ALARAwas generally good with some ALARA shortcomings identified during the
Unit 2 first refueling outage.
Radioactive
waste
(radwaste)
processing
and transportation
remained a strength.
Radiological chemistry controls were good and progress was noted in the
area of effluent monitoring.
III.B.1
Analysis
Radi lo ical Controls
NMPC continued to maintain an effective radiological controls program at both units. ALARA
performance was good with notable improvements in the program and performance at Unit 2.
Minor areas of mixed performance
were noted at both units.
Radiation protection staffing
remained good with several organizational changes.
Training remained highly effective.
The
external and internal dosimetry and respiratory protection programs performed well. The quality
assurance
program continued to be a notable strength in this area.
The radwaste programs at
both units performed very effectively.
Significant improvements were made by NMPC in its corporate ALARAprogram and in its
ALARAperformance at Unit 2, while maintaining an outstanding ALARAprogram at Unit 1.
NMPC senior management
developed
a corporate ALARA policy, which included specific
performance goals for all major departments
at the site, and clearly demonstrated
its support of
the ALARAprogram to all workers.
During the second refueling outage, Unit 2 established
a
challenging ALARAgoal which was one-third lower than its total dose during the first refueling
outage.
This outage was completed with a total dose 10% lower than this goal.
Strong support
for the ALARAprogram and its goals by the major department
heads and plant manager was
observed.
While performance was generally good, several instances of poor performance occurred.
Both
units had problems in late 1991 with operations department personnel making improper High
Radiation Area entries.
At Unit 2, plant personnel were observed exiting the Radiologically
Controlled Area (RCA) without properly frisking and in one case radiation protection technicians
did not properly assess
the cause for alarming airborne activity monitors in the Unit 2 reactor
building. Radiological safety postings and surveys ofareas within the RCA were generally good
at both units.
However, radiological housekeeping
was a problem at Unit 2, where multiple
instances of poor worker housekeeping
practices were noted.
11
NMPC internal dosimetry and respiratory protection programs were determined to be generally
good, and the licensee took corrective actions to upgrade its procedures in this area to address
concerns raised during the previous SALP period.
The external dosimetry program was also
conducted well.
Late in the assessment
period, NMPC began a program to fully review all
dosimetry records to validate data in preparation for the implementation of a computerized
radiation protection
records
system.
Errors identified by the end of the period involved
improperly prepared and documented worker dosimetry forms.
Staffing levels remained good, with all key positions filled by competent professionals.
In late
1991,
NMPC disestablished
the
site radiological
support
organization,
which had
been
implementing the transportation, dosimetry and respiratory protection programs for both units
and gave responsibility for these programs to the unit Radiation Protection Managers (RPMs).
This move improved the RPMs'ontrol over all areas of the radiation protection program.
No
changes in staffing levels within these functional areas occurred as a result of this action.
Each
unit now has responsibility for its own transportation activities, while Unit 1 supports both units
for internal dosimetry and respiratory protection, and Unit 2 supports both units for external
dosimetry..
Ahighly effective training program forboth radiation protection and radwaste personnel was also
continued.
A minor weakness identified during the last assessment,
involving training of the
training department staff, was corrected during this assessment
period. Awell developed training
program for contractor radiation protection
technicians
was also implemented
during this"
assessment
period, as demonstrated by the lack of personnel errors.
The NMPC quality assurance program in the radiological protection and radwaste areas continued
to be a notable strength, with exceptional scope and technical depth in the audit and surveillance
program. NMPC management continued to utilize this program to improve its own performance
by taking prompt actions on all findings and recommendations
contained in these reports.
NMPC continued to implement a very effective radwaste program at both units.
Radwaste
operators maintained strict access control of personnel and oversight ofactivities in the radwaste
buildings,
A new radwaste general supervisor position provided increased
oversight of that
group. Allshipments were made in accordance with the applicable DOT and NRC
'regulations,
and all waste shipments were found to be acceptable to the disposal sites.
NMPC also exhibited
a high degree of sensitivity with regard to problems involving a shipping cask utilized in the
transport of highly irradiated reactor components
from the Unit
1 spent fuel pool.
Despite
significant problems associated
with the use and decontamination of this shipping cask,
the
licensee made several successful shipments.
12
R
i
1
i
1Environmen
1
nd Effl ent M ni
rin
Pr
rams
NMPC continued to implement a strong radiological environmental monitoring program. NMPC
operated
an extensive surveillance program for the collection and analysis of environmental
samples and for the meteorological monitoring instrumentation.
A programmatic weakness involving the operability of effluent monitors was identified during
the last two SALP periods, with several effluent radiation monitoring systems (RMS) out of
service due to design deficiencies.
Special management attention was provided, and initiatives
to improve the operability of effluent monitors were developed.
Management's commitment to
maintaining the operability and reliability for all effluent RMS was demonstrated
effectively
during this SALP period, with significant improvement noted in the operability of the effluent
RMS. Liquid and gaseous effluent sampling, analysis, and reporting were good. Aircleaning
systems were well maintained and tested.
Quality assurance
audits covered the stated objectives and were of excellent technical depth to
assess the off-site dose calculation model radiological environmental monitoring, and radiological
effluent monitoring programs.
ummar
- Radiolo ical Controls
In summary, NMPC has made significant improvements in its ALARAprogram at Unit 2, while
maintaining
a very effective ALARA program at Unit 1, together with strong
radwaste,
transportation
and
radiological
environmental
monitoring programs
at both
units.
The
radiological controls program was generally good at Unit 1, while continued weaknesses
in this
area
at Unit 2 were
observed,
with examples
of this
weakness
evident in radiological
housekeeping,
a High Radiation Area entry, and improper RCA exiting. The operability of the
effluent RMS was significantly improved, while continuing to maintain very effective liquid and
gaseous effluent control programs.
III.B.2
Performance Rating:
Category
2
III.B.3
Board Comment:
The Board recognized that significant improvement in the
performance of the Unit 2 ALARAprogram was achieved.
III.C Maintenance/Surveillance
During the last assessment
period the combined
Maintenance/Surveillance
functional area
received a Category 2 Rating.
At Unit 1, maintenance performance improved, in part, due to
good procedural adherence. 'owever, some instances of poor maintenance practices resulted in
unplanned
shutdowns.
Progress
in reduction of the work request
backlog
was
made.
Performance in the surveillance area demonstrated
improvement.
Good planning and effective
management
oversight resulted in proper execution of the start-up test program.
1
4-
~
~
13
Unit 2 demonstrated
generally
good performance
in maintenance
and efforts to improve
procedural controls and personnel procedural adherence were evident.
Maintenance personnel
significantly reduced operational events involvingpreventive or corrective maintenance.
Progress
was noted in reducing the work request backlog,
Surveillan'ce testing was generally good.
The
maintenance
department
satisfactorily implemented inservice inspection and inservice testing
programs during the period.
III.C.1
Analysis
IH.C.1.1
Unit 1
Maintenance
The Unit 1 maintenance staff demonstrated generally good performance during this assessment
period.
Maintenance personnel performed well during corrective and preventative maintenance
activities. A few noteworthy instances of poor maintenance performance occurred due to weak
procedural adherence
and inattention-to-detail.
These included a significant breakdown in the
implementation of the work control program leading to the temporary isolation of the unit from
its ultimate heat sink.
Strong management
oversight maintained a low maintenance
backlog,
improved in-field supervision, and good overall plant material condition.
Several operational
events resulted from various causes including age-related degradation of non-safety equipment.
The outage planning organization functioned well over the period.
Maintenance workers generally demonstrated good performance during corrective and preventive
maintenance.
During preventive maintenance on containment spray heat exchangers and on the
emergency
diesel generators,
maintenance
personnel exhibited good work practices and good
safety perspective..
Maintenance
personnel
exhibited
a questioning
attitude by identifying
improperly operating equipment and potential problems during plant tours.
Staffing remained
at a suitable level. Detailed post-maintenance
tests verified effective completion of maintenance
work.
Excellent housekeeping
practices and the overall condition of the plant equipment and
areas reflected a conscientious
attitude.
The painting of the walls and floors in the reactor
building represented
a significant effort to improve plant housekeeping.
A few instances of poor performance occurred due to inattention-to-detail and poor procedural
adherence.
Also, a significant breakdown in the implementation of the work control process
occurred in February 1992, which resulted in the temporary isolation ofthe unit from its ultimate
heat sink. This latter event resulted from failure to follow established work control processes,
inadequate
management
attention in assuring that procedures were being followed, inadequate
communications between several NMPC organizations, and from inadequate consideration of the
risks associated with the activities being performed.
Other minor examples ofpoor performance
also occurred, which reflected weaknesses in supervisor and management oversight. In contrast,
good management oversight led to maintaining preventive and corrective maintenance backlogs
.
low. Further, managers
and supervisors were frequently present in the field to oversee work
practices.
4
a
~
14
NMPC management took prompt and thorough corrective actions to address the causes for the
breakdown in the work control process discussed above.
These actions included a high quality,
self-critical assessment
that developed
corrective actions for the identified causes.
implemented a monitoring process which provided management
assessments
of work control
activities.
Managers
and supervisors
conducted
this activity at both units to develop
an
understanding of the weaknesses
and the need for more management oversight of the process.
The overall scope ofthis program appeared good; however, its long term effectiveness remained
a concern.
Failures of balance-of-plant equipment challenged plant operators by causing five of the six
. reactor scrams, the one forced outage, and.several forced reductions in power. NMPC identified
the need to increase the effectiveness of preventive maintenance performed on balance-of-plant
equipment and initiated short and long-term corrective actions. The effectiveness ofthese actions
in reducing plant scrams and transients has yet to be demonstrated.
Aggressive planmng and scheduling during routine operations
ensured
the safe and effective
completion of work. During forced outages the planning department quickly developed detailed
work and contingency schedules.
Pre-planned
outage work was coordinated and implemented
effectively.
Increased
management
oversight, during outages,
resulted from the addition of a
shift manager responsible for tracking work and maintaining an overall status.
urv illance - Unit I
The NMPC staff effectively implemented the Unit 1 surveillance test program. Testing identified
conditions needing correction before equipment failure occurred.
The NMPC staff conducted
testing well, in accordance with approved procedures.
Scheduling and tracking of surveillance
tests
continued to be effective.
The inservice testing /ST) and inservice inspection
(ISI)
activities were properly scheduled
and conducted.
During the period, surveillance testing was properly conducted and led to the identification of
equipment
needing
repairs.
The NMPC staff effectively documented
surveillance
testing
problems on work requests
and/or deviation/event
reports
as necessary
to allow corrective
actions. A review of the reactor building emergency ventilation system testing identified that the
test acceptance criteria during a secondary containment drawdown test was not in conformance
with the design requirements of the system fans.
Prompt actions to develop a new acceptance
criteria resolved this issue.
The NMPC staff generally used properly prepared test procedures
and correctly recorded test
data.
Three inadvertent engineered safety feature actuations occurred relating to testing.
These
actuations
were minor, not directly related
to personnel
errors,
and did not i'ndicate any
programmatic
problems.
However,
in one instance
maintenance
personnel
installed
test
instrumentation on several core spray system pressure control valves. This installation was done
informally, not in accordance with the temporary modification procedure, and without regard for
~ ~
15
the impact on system operability. NMPC took adequate actions to ensuie the installation of test
equipment in accordance with an approved procedure.
In another instance NMPC identified and
properly dispositioned
an issue that timers in the automatic initiation logic for the reactor
building emergency ventilation system had not been tested.
The scheduling and tracking of sur veillance testing remained very good.
A computerized data
base provided an effective management tool.
The ISI/IST program was generally effective over the period,
Changes to the structure of the
programs occurred during efforts to streamline the nuclear division. The ISI/IST group, which
previously reported to site engineering, divided such that ISI reported to the quality assurance
department,
and IST reported to the operations department.
There have been no observable
impacts of these changes
on performance in the surveillance test area.
During the period ISI
activity was low because of the unit outage scheduling.
NMPC enhanced
the program by
providing dedicated IST personnel to perform the ultrasonic flow and vibration measurements
on all equipment.
This action and special technician training- on the use of ultrasonic flow
instrumentation significantly reduced the possibility for inaccurate data.
III.C.1.2
Unit 2
Maintenance
The Unit 2 maintenance department continued to demonstrate good performance this assessment
period. Maintenance personnel knowledgeably performed activities and demonstrated the proper
safety perspective;
although, inattention-to-detail resulted in several operational events.
The
maintenance work request backlog remained high; with few exceptions, management effectively
tracked
and properly dispositioned
work requests
to ensure
system
operability.
Material
condition throughout the plant remained good.
Maintenance supervisors generally performed
well and satisfactorily monitored daily maintenance activities.
The training and qualification
programs
were effective and
maintenance
staffing levels remained
stable.
The planning
department provided good support for planned and forced outage work.
Maintenance
personnel
were knowledgeable
and experienced
and they generally performed
corrective and preventive maintenance in a professional manner.
However, performance overall
was inconsistent.
While there were no plant transients related to performance of maintenance
activities, maintenance personnel performance was poor related to the dropping oftwo new (non-
irradiated) fuel assemblies.
In addition, several other personnel errors occurred that caused
engineered
safety feature actuations.
NMPC took good corrective actions in response to these
events.
These maintenance errors were not indicative ofprogrammatic maintenance failures, but
were isolated examples of poor work practices and inattention-to-detail.
I
IL
16
The maintenance request backlog remained high throughout most ofthe assessment
period. Plant
events and the increased
scope of the refueling outage precluded a net reduction in the total
backlog, however,
management
prioritized and dispositioned the work requests in a manner
consistent with continued safe operation of the plant.
Oversight of activities by maintenance
management
and supervision was generally good this
assessment
period, but with notable exceptions.
The maintenance management established clear
standards for supervisor work observations.
First line supervision positively contributed to the
work quality by clearly communicating management expectations and consistently observing daily
maintenance activities.
The supervisor's knowledge and oversight were considered
strengths,
especially during the recirculation loop sample line corrective maintenance.
Maintenance management
demonstrated
a good safety perspective during the emergency diesel
generator cylinder liner replacements
due to tin smear.
However, maintenance
management
oversight was not fully effective at preventing significant errors as evidenced by the event in
which new fuel bundles were dropped and by the events in which offsite power and control room
alarms were lost.
The maintenance technical training and qualification programs functioned well as exemplified by
a strong maintenance welding training program.
The mechanical maintenance training program
was good.
In general, the material condition of plant equipment was good.
The maintenance
staffing levels remained stable this period.
urv ill nce- Unit 2
The Unit 2 staff appropriately implemented
the surveillance testing program and positively
contributed to the continued
safe operation of the plant.
Knowledgeable
and professional
personnel successfully completed technical specification surveillance tests within the specified
frequencies with few exceptions.
However, inattention-to-detail contributed to several minor
errors.
For example, a technician error caused
an inadvertent start of the high pressure core
spray pump and its associated
emergency
diesel generator.
Once identified, NMPC took
adequate corrective actions to address each of these instances. The surveillance testing prob!ems
encountered over the period were isolated and of minor safety consequence.
The surveillance testing program, including IST, properly demonstrated
the operability and
availability of safety
systems
to perform their intended
function.
Management
properly
dispositioned equipment deficiencies identified during surveillance test. A service water system
check valve failure identified during an IST reverse flowtest was properly resolved.
Testing and
subsequent
troubleshooting
on the standby
gas treatment
system
allowed identification and
correction of a condition which could have caused
system valves to fail in a non-conservative
position.
~ g
17
Review of the ISI program for the recirculation system piping and a sample of nondestructive
examination data indicated that the program met the applicable requirements
and was well
managed.
These instances
were evidence of good quality control of inspector qualifications,
proper procedures,
and resolution of indications.
The erosion/corrosion
program for high
energy piping systems properly addressed
the effects of flow assisted phenomena.
The snubber
testing and local leak rate testing (LLRQ programs continued to be implemented well.
v rail
umma
- Main
n n
n
urv illan
ni
1
nd 2
The maintenance
staff at Unit l generally performed well with some
notable exceptions.
Increased
supervisory and management
presence in the field, low work request and preventive
maintenance
backlogs,
and good team work between
the maintenance
department
and other
working groups
indicated
generally
good management
oversight.
However,
a significant
program
implementation
breakdown
during maintenance
activities
on a screenhouse
gate
occurred which resulted in a temporary loss of the ultimate heat sink which challenged
the
operations staff.
Although short and long term corrective actions were initiated to address
the
high number of maintenance-related
scrams and events, their continued occurrence indicates that
the efforts have been less than fullyeffective. The surveillance test program, including ISI and
IST activities, was effective at identifying and correcting equipment deficiencies.
The maintenance department at Unit 2 continued to demonstrate
generally good performance.
Maintenance
personnel
knowledgeably
performed
maintenance
and
surveillance
activities,
demonstrating the proper safety perspective.
However, a poor plant impact assessment
led to
a loss of off-site power and poor supervision contributed to the dropping of two new fuel
bundles.
The plant material condition and overall management of work planning was good.
Maintenance department
management
oversight was considered
a strength.
The surveillance
testing program, including the ISI and LLRT programs, consistently confirmed the operability
of safety systems.
III.C.2
Performance Rating:
Category
2
Trend:
Declining
III.C.3
Board Comment:
In general, the station performance in the maintenance area
was good, but inconsistent.
Based on repeated instances of
maintenance-related
scrams and events, which occurred at
both units throughout the period, the board concluded that
overall effectiveness of the program was declining.
~ 1
18
III.DEmergency Preparedness
For the last SALP period, Emergency Preparedness
was rated as Category 1. Strengths included:
appropriate and timely classification of six Unusual Events, sufficient emergency planning (EP)
department staffing, Emergency
Response
Organization (ERO) depth, and effective training.
One exercise
weakness
resulted from failure of an ERO manager
to request
core damage
assessments
and another resulted from failure to consider plume trajectory variability when
calculating projected doses.
Subsequent inspection found that appropriate corrective action was
taken for these matters.
Slowness in resolving 1988 Emergency Response Facility Appraisal
items indicated a lack of proper management attention to certain items.
Analysis
NMPC implemented
an excellent EP program over the period.
When challenged by actual
events, including a Site Area Emergency (SAE), the emergency
plan functioned effectively.
Further, each event was analyzed by the EP staff and actions were taken to address
areas for
improvement.
Management, including EP, site and corporate, involvement in this program was
good.
However, actions to address deficiencies identified related to the drill/exercise program
were
not fully effective.
Additionally, no
assurance
of periodic
Emergency
Response
Organization member participation in drills/exercises was identified.
Emergency facilities and
equipment were properly maintained, and the resolution to facility issues was acceptable.
The
quality assurance
program remained effective in auditing this area.
The Nine MilePoint Site Emergency Plan (SEP) was shown to be effective during several actual
events, including a SAE at Unit 2 as a result of a plant transient with a loss of control room
and a partial loss of plant instrumentation.
During these events operator and
management
response
was excellent, and event classifications were timely and proper.
There
was good assignment of emergency responsibilities by the Shift Supervisor and overall actions
taken by response
personnel
were effective.
Personnel
accountability
was not, however,
accomplished for about three hours (as'compared
to a 30-minute goal). Also, notification of the
Emergency Response
organization was initiated one hour after SAE declaration.
The licensee
critiqued its response,
compiled a comprehensive list of items for corrective action, and made
good progress on item correction.
An Alert and several Unusual Events also required Unit 2 SEP implementation.
Again, event
classifications and operator and management
responses were proper.
During the Alert, turnover
of Emergency
Director duties
from the
station
shift supervisor
to Emergency
Response
Organization Emergency Director was conducted well, and personnel in the Technical Support
Center functioned effectively.
Timely corrective actions initiated to address
weaknesses
identified by NMPC's self-critique
following the SAE indicated effective management
control.
Good progress
was made in the
resolution of the SAE action plan high priority items. In particular, the licensee tasked Security
I ~
19
with personnel
accountability
instead of that responsibility
being
shared
by Operations,
Maintenance,
and Security.
This change appeared beneficial to ongoing accountability and the
licensee reported that three drills have since found accountability is not a problem.
However,
the NRC has not yet had the chance to observe accountability effectiveness during an exercise
,or actual event.
Two station drills were conducted in 1991 in addition to the smaller scale drills required by the
emergency. plan, meeting NRC requirements.
However, drill/exercise weaknesses
were evident.
The licensee did not effectively review repetitive problems identified during these drills/exercises
for common cause factors; an example was the late notifications for the February 26,
1991
licensee drill, the August 1, 1991 licensee drill, and the August 13, 1991 SAE.
In addition,
ERO member participation in drills was voluntary, with no assurance of peribdic participation
identified.
Based on the actual response to the Unit 2 SAE, NMPC requested and was granted an exemption
from the required 1991 annual emergency exercise.
The request and the response to the NRC
staff request
for additional
information were thorough,
complete,
and
timely.
demonstrated
an understanding of the regulatory issues involved as well as the method and bases
for their satisfactory resolution.
The exemption request justification contained sound technical
judgements based on thorough analysis.
Ample ERO staffing was maintained, with all positions filled at least three deep.
Also, at the
end of the period, the NMPC EP Branch was creating a scenario development committee to
prepare the 1992 emergency exercise scenario, which was a good initiative. Classroom training,
held throughout the year, was well defined and lesson plans were properly controlled, accurate
and well detailed. Apositive initiative to shift from classroom-based
toward performance-based
training was in progress.
NRC walk-through drills of on-shift dose assessors
confirmed training
effectiveness in that function.
The EP program was administered by the Director, Emergency Planning, with good station and
corporate management
involvement in EP activities.
The EP staff held regular meetings with
State and local officials, and maintained a good, close relationship with off-site groups.
The EP
department was sufficiently staffed by eight individuals, including an SRO-qualified individual
(responsible for drill/exercise development)
and a meteorologist.'he
EP staff implemented
essential program tasks.
Although there was no assigned health physicist in the EP Branch, the
obstacle of obtaining
health
physics
support for drill/exercise
scenario
development
was
overcome
by the use of temporary
contractor
support
and
good EP staff knowledge of
Emerg'ency
Plan
Implementing
Procedures
(EPIPs)
~
Station
and
corporate
management
maintained
emergency
response
qualifications,'eviewed
and approved
emergency
plan and
procedure
changes,
participated in drills and exercises,
and interfaced with State and local
agencies.
Senior management
assumed both Site Emergency Director and support roles during
the SAE and the March 1992 Alert and performed well.
J
~I
20
Emergency response facilities, equipment, and supplies were well maintained.
The Operations
Support Center,
which was a multiple use facility, became
dedicated
solely to emergency
response
and improved in-plant response
activities.
EPIPs were well-stated.
EPIP changes
initiated in response to areas needing improvement from the SAE were generally appropriate,
properly reviewed, approved, and distributed.
Resolution ofthe 1988 Emergency Response Facility (ERF) appraisal items continued to progress
acceptably.
Three items were closed in April 1992.
Three other items (safety parameter signal
isolation, plant computer reserve capacity, and Emergency Operations Facility shielding) remain
open.
Safety parameter isolation and plant computer reserve capacity items appear to be on track
for completion during 1995.
The commitment to complete a revised EOF shielding analysis is
now scheduled for completion by the end of 1992.
NMPC's quality assurance program conducted effective EP audits.
Unannounced QA checks of
EP, e.g., carrying of Oswego County cards for expedited transit through roadblocks,
were
assessed
as a strength.
The technical specification audit was combined with the 10 CFR 50.54(t)
review and was appropriate in scope, thorough, and received wide management distribution. The
audit report was provided to state and county officials.
NRC review noted opportunities for
improvement in the information contained in the audit/review plan, such
as the absence of
specific direction as to the evaluation of the adequacy of off-site interface required by 10 CFR
. 50.54(t).
umma
- Emer enc
Pre aredne
s
NMPC continued to implement an effective EP program as demonstrated by responses
to actual
plant events.
Management involvement in EP was good.
Audits/reviews, quality assurance
checks, and readiness ofemergency response facilities were strengths.
EP staffing was sufficient
to support overall response activities. Resolution ofERF appraisal items progressed acceptably.
However, weaknesses in the drill/exercise program, including the indication ofinadequate review
of repetitive problems for common cause factors, were noted.
III.D.2
Performance Rating:
Category
1
Trend:
Declining
III.D.3
Board Comment
Although no specific performance problems have been identified, the Board was concerned with
the voluntary nature of participation of ERO personnel in drills and exercises.
II
III.E Security
During the previous assessment
period; the licensee's performance was rated Category 1. That
rating was based on excellent security practices; a sound performance-oriented training program;
. effectively installed and well-maintained equipment; and a very competent management team who
assured implementation of a high quality program..
III.E.1
Analysis
During this assessment
period, the security program continued to be carried out effectively and
in accordance
with NRC requirements
and NMPC commitments.
Corporate
and plant
management
support continued
to be a notable strength
as evidenced by the planning and
budgeting for program upgrades, active participation in groups engaged in nuclear plant security
matters,
and continued
excellent rapport and liaison with state and local law enforcement
agencies.
Although a corporate staff reduction policy resulted in a significant reduction in
security staffing, previously planned upgrades were completed on schedule, which indicated the
ability of the NMPC security program to adjust to changing circumstances.
The more significant
of these upgrades
was the addition of state of the art equipment to the assessment
system, the
installation of a card reader system to enhance vehicle and driv'er access to the protected area,
and the enhancement of the tactical firearms training course.
A notable strength in this program area was the continued assignment of instrumentation
and
controls g&C) technicians
to the security organization
to maintain security equipment
and
implement upgrades.
The ISAAC technicians effectively maintained systems and equipment and
thereby reduced
the need for compensatory
measures
and personnel overtime.
Although the
number of technicians was reduced, the licensee maintained an excellent testing and maintenance
program.
The training program
was well developed
and
administered
by a staff of experienced,
knowledgeable professionals.
Training facilities and training aids were appropriate and well
maintained.
The effectiveness of training was apparent by the limited number of personnel
errors.
However, exterior patrol officers did fail to detect, for an indeterminate period,
damage'o
the intrusion detection
system
caused
by inclement weather.
The Training Department
promptly reemphasized
patrol officer duties during shift turnover in an effort to prevent
~ recurrence.
The Training Department also enhanced the contingency response training by placing
emphasis on tactics and weapons handling. Additionally, all lesson plans and crucial tasks were
revised to be more performance-based
and a new tracking system was implemented to ensure all
requalification requirements
were met.
The Training Department was actively involved in all
security drills and utilized the feedback from the drills to enhance
the effectiveness of the
program.
Interviews of security officers indicated that the training received was effective and
directed to ensuring that security objectives were properly met. Security officers displayed high
morale and were knowledgeable of their post assignments
and responsibilities.
II
I
22
Based on the initial inspection of the licensee's
Fitness-for-Duty (FFD) program during this
period, it was determined
that the development
and implementation of, the program
was
aggressive,
comprehensive,
and directed toward public health and safety.
Management support
for the program was demonstrated by the high quality of the facilities and personnel responsible
for program implementation.
Corrective actions taken to resolve potential program weaknesses
were prompt and effective, indicating a quality program with appropriate management attention.
NMPC quality assurance
audit program for security audit was comprehensive
in scope and
performance-based.
The licensee used a consultant to provide technical expertise to the Quality
Assurance audit team.
No adverse
findings were identified and recommendations
made to
strengthen the=program were promptly and effectively implemented.
Additionally, the licensee
continued the initiatives of self-assessments
and appraisals
to provide oversight of security
program implementation and personnel performance.
A review of the loggable events demonstrated
that the self-assessments
and appraisals
were
effective in that few events were repetitive and personnel errors were rare. In addition", loggable
events were appropriately analyzed, tracked and corrective actions, where required, were timely
and effective.
Event reporting procedures
were clear and consistent
with NRC reporting
requirements.
No prompt reportable security events occurred during the period.
The reporting
procedures
were well understood
by security
supervisors
and were consistent. with NRC
regulations.
The licensee submitted two revisions to the Physical Security Plan, one revision to the Training
and Qualification Plan and one revision to the Contingency Plan under the provisions of 10 CFR 50.54(p).
The revisions were technically sound
and reflected well-developed policies and
procedures.
Summa
- Securit
The licensee continued to maintain a very effective and performance-based
security program.
Management support and effective program oversight continued to be evident throughout the
period.
The continuing efforts expended
to upgrade
the
security
program,
to resolve
discrepancies
before they became
problems,
and to maintain an effective training program
demonstrated
the licensee's commitment to maintaining a high quality program.
III.E.2
III.E.3
Performance Rating:
Category
1
Board Comment:
The
Board
noted
the
consistent
excellent
security
performance over the last several SALP periods.
)
23
III.F Engineering/Technical
Su pport
Last period this functional area was rated
as a Category 2.
NMPC showed evidence of
increased management involvement in engineering activities compared to the previous assessment
period. The addition'of the system engineers to each of the plant staffs was shown to have been
an asset to the overall quality of engineering support,
However, a few examples during the
assessment
period indicated performance inconsistencies and minor shortcomings in engineering
management
oversight.
The following areas
were identified
as
needing
improvement:
implementation of a technical training program; quality and review of engineering work; and
engineering management oversight. Overall, engineering and technical support performance was
good and generally improved.
III.F.1
Analysis
The NMPC engineering organization generally provided high quality work products, in support
of safe operation of both units.. Effective actions were taken to address previous concerns over
the quality and review of work, amount of oversight by engineering
management,
and the
adequacy of the technical training program.
However, there were weakness
noted in the
administration and implementation ofthe temporary modification process.
The system engineers
continued.to perform well in addressing day-to-day issues and the interface between them and
the other engineering organizations was good.
The modification and design control processes
functioned well.
Inconsistencies
were noted in the quality of the engineering basis for some
submittals to the NRC.
Engineering/technical
support to assure safe plant operation was provided by the site, system,
and corporate engineers for each unit. The site engineering group with design authority stationed
at each
unit provided
good
representation
of corporate
engineering
which expedited
the
engineering and technical support for the station.
The engineering support for the Unit 2 second
refueling. outage was good and design changes needed for the upcoming Unit 1 refueling outage
were on schedule.
The system for assigning priorities to plant nuclear projects had the proper
safety emphasis.
Priority safety significant projects were on schedule
and completed
when
necessary.
Engineering
management
took effective actions
to improve the timeliness
and quality of
engineering work through a performance monitoring and measurement system and an independent
assessment
process.
The engineering organizations,
dedicated to each unit, properly set goals
and measured their performance.
However, the backlog of deficiency/event reports, temporary
modifications, and plant change requests requiring engineering review and disposition remained
high and required continued management
attention.
Improvement was demonstrated
by the
capability to resolve technical
issues
and to deliver quality engineering
products.
Notable.
examples at Unit 1 include:
a sound safety evaluation for operation above 80% power with only
two feedwater heater strings operable; and the investigation of the root cause and scope of cracks
in the emergency cooling system valves. AtUnit 2, some notable examples include: resolution
tg
24
of a crack in the high pressure core spray safe end extension nozzle weld; good evaluation and
corrective action for a recirculation loop sample line failure; and very effective analysis and
corrective actions following determination of a design deficiency in the cooling water system
which supplies the Division IIIemergency diesel generator.
Increased management oversight of engineering work was evidenced by the implementation and
monthly review of the top 10 list of issues at each unit. The configuration management program
at Unit2 was also effective. Task managers and a senior engineering review team were assigned
to resolve
and followup the technical
issues
developed
during the Unit
1
design
basis
reconstitution effort, which was well controlled.
The completed
system design descriptions
clearly addressed
the system
design
requirements,
operating limits, test
and surveillance
requirements,
maintenance considerations,'and
regulatory requirements.
Increased engineering
management involvement, controls and initiatives to assure quality ofengineering products were
observed
during this assessment
period.
A Safety Review and Audit Board engineering
subcommittee
was
formed to assess
the engineering
activities.
The Independent
Safety
Engineering Group monitored engineering work activities and performance. Further, when the
deviation/event report process was used it was effective at identifying and correcting problems.
While the above actions were generally effective, the backlog of temporary modifications for
both units remained high and in need of,continued management attention.
The NRC found that
there have been instances ofinadequate controls over temporary modifications at both units. For
example, the installation of temporary ventilation equipment in the reactor building at Unit 1 was
not processed
as a temporary modification.
Also, temporary equipment installed between the
make-up water system
and service water radiation monitors in Unit 2 was not removed
as
required by the temporary modification procedures.
A technical training and qualification program was effective at ensuring the technical competency
and familiarityof the corporate and site personnel with their responsibilities.
In response to the
previous weakness
in this area, NMPC established
and implemented
a broad-based
technical
training program for the corporate engineering staff in January 1992. This training program was
comprehensive
and enhanced the knowledge and skills of engineering personnel.
A continuing
training program for corporate
engineers
was being developed
by an engineering
training
. advisory committee.
System
engineers
continued to provide good support for the operation of both units.
For
'xample,
system engineers
demonstrated:
excellent knowledge of the loss of uninterruptible
power supplies (UPS) during the event at Unit 2 and provided clear explanation of their design
during several
meetings
with the NRC; good support during system
troubleshooting
and
determination
of root
causes
.following reactor
and
unexpected
events;
timely
identification ofcylinder liner tin smear during the emergency diesel generator (EDG) overhauls
at Unit 2; and good determination of control rod drives needing replacement and establishment
of an EDG reliability enhancement program at Unit 1. The reactor engineering group conducted
post scram reviews ofconsistently high quality, and provided effective oversight of the spent fuel
pool cleanup effort and fuel performance activities.
J
25
An effective interface between the station and corporate engineering personnel existed at both
units.
The staffing of site and system
engineering
groups for each plant to support
the
engineering/technical
needs ofthe plant contributed to the effectiveness ofthis interface. NMPC
effectively improved
communications
between
the corporate
engineering
staff and other
organizations on-site, through routine meetings to resolve issues.
The active participation of
management
representatives
from different organizations at these meetings facilitated effective
communication.
However, poor engineering involvement was noted during NRC review of the
inadvertent isolation of the ultimate heat sink at Unit 1.
Modifications and design changes were of good quality and technically accurate.
Engineering
management
involvement, project team oversight, and oversight of consultants
used to resolve
issues
were
observed
to be
good.
Engineers
and
project
team
members
were
very
knowledgeable of their modifications and design changes and the 10 CFR 50.59 process.
The
Station Operation Review Committee (SORC) review, engineering
technical reviews,
post-
modification testing, and adherence
to the procedures for the modifications were found to be
good.
Good interaction between system engineers
and corporate engineers were noted during
this process.
Examples of good modifications included:
a snubber reduction program
and
resolution of the feedwater stratification issues
at Unit 2; and feedwater flow control valve
inspection/modification and the installation of the static invertor battery chargers at Unit 1. Both
units developed a comprehensive approach to limitthe impact of zebra mussel intrusion on plant
water systems.
Inconsistencies in the quality of engineering submittals to the NRC were identified during this
period.
For example,
the
calculations
supporting
a proposed
revision
to
the Unit
1
pressure/temperature
limits were well prepared.
Also, analysis of the flaw in the Unit 2 high
pressure core spray nozzle safe end extension weld was excellent and responses
to requests for
additional information on this issue were promptly provided.
However, in contrast to this good
performance,
the no significant hazards consideration analysis in the Unit 2 license amendment
request related to the automatic depressurization
system test pressure contained only a minimally
adequate analysis.
The license amendment request to operate with a control rod uncoupled did
not have an adequate
safety evaluation.
Furthermore,
the NRC staff found the repair plan for
the cracking identified in the Unit 1 emergency cooling system condensate valves did not provide
sufficient engineering
basis to allow non-ASME code repair to the reactor coolant pressure
boundary.
Ip
26
mrna
- En ineerin
nd T hni
I
u
In summary,
the engineering
and technical 'support organization
continued to provide good
support to the station.
The quality of engineering
and management
involvement improved
compared
to the previous SALP period. System
engineers
have continued
to provide good
support at both units.
There have been some instances of inadequate control over temporary
modifications.
Inconsistencies
in the quality of engineering
submittals
to the NRC were
identified during the period.
III.F.2
Performance Rating:
Category
2
III.G
Safety Assessment/Quality Verification
The previous SALP report rated Safety Assessment/Quality
Verification as
a Category
2.
NMPC demonstrated
an'improved
approach
to assuring
quality and
assessing
the safety
significance of issues
affecting plant operations.
Self-assessment
programs
became
more
effective during the latter portions of the assessment
period. The new standards ofperformance
and their methods of implementation were found to be effective in articulating management
expectations
and requirements
and to be generally well understood
and followed by Nuclear
Division personnel.
Licensing action submittals were generally considered
to be technically
adequate and timely. Overall performance in this functional area improved during the previous
'ALP period.
III.G.1
An~al ~
While NMPC demonstrated
generally good performance in this functional area during this
assessment
period, the implementation of programs and policies for correcting the causes for
repeated
inattention-to-detail
and procedural
adherence
errors
has not been fully effective.
Management involvement in day-to-day events was evident, but not fully effective in reducing
the number of scrams or significant operating events.
Activities of the off-site, on-site, and
independent engineering review groups were good.
QA audits and surveillances were generally
effective in the identification of problems; however, management failed to take action on some
identified problems.
NMPC actions in response
to industry information were good.
Self-
assessment
and other performance review activities provided effective evaluations of facility
operations.
Submittals and reports made to the NRC were generally of good quality.
The NMPC Nuclear Division Policy and associated
Nuclear Division Directives were well
written,
assisted
in clarifying management
expectations,
and
defined
responsibilities
and
accountabilities.
However, implementation of these directives in some cases
has not been fully
effective.
For example, the inadvertent isolation of Unit 1 from its ultimate heat sink and the
dropping of two new fuel assemblies
at Unit 2 were due to breakdowns in the control of work
activities.
These
events
and others
discussed
in the operations,
radiological control,
and
Ci
27
maintenance/surveillance
sections of this report demonstrated
that station management
was not
fully effective in ensuring that supervisors
and managers
enforced the expectations
defined in
these procedures.
Significant corrective actions were taken in response
to these and other
events.
However, these issues continued to adversely affect performance and are indicative of
longstanding problems.
The Executive Vice President-Nuclear moved his office from Syracuse,
New York, to the site in late February
1992,
as
a positive initiative to increase
senior
management
oversight of site activities.
Management involvement in day-to-day events has been good and there has been a significant
level of supervisory presence in the field. Despite this involvement, communications within and
among organizations participating in work activities have not always been fully effective,
For
example,
the on-duty station shift supervisor
was not informed of operations
department
concerns about performing the Unit 1 screenhouse
gate tests which led to the loss of ultimate
heat sink event.
Likewise, the loss of off-site power at Unit 2 was caused by a combination of
inadequate
work package
plant assessment
and the reliance by control room operators
on
incomplete information provided by the relay technician after loss of the first off-site line.
Further, there were six automatic scrams in Unit 1 and three automatic scrams in Unit 2 during
this assessment
period.
Seven of the nine automatic scrams
were attributed to equipment
failures, The number of scrams indicates that management
focus on the area of scram reduction
is needed.
The safety oversight committees
(Site Operations Review Committee and Safety Review and
Audit Board) continued to perform thorough and effective reviews of issues
and exhibited a
strong safety perspective.
Most members actively participated in committee discussions
and
exhibited
conscientious
and questioning attitudes.
Topics presented
for review, including
significant operational events, were thoroughly evaluated.
The
Independent
Safety
Engineering
Group
gSEG)
continued
to provide NMPC with
comprehensive
and effective self-assessments
and root cause evaluations.
ISEG review of the
dropped new fuel event at Unit 2 was an example of this, as was the thorough root cause
analysis of temporary modification process
at both units.
The results of these reviews were
presented in an organized manner and the root causes were correctly identified.
NMPC responses
to 10 CFR Part 21 notifications and other industry notifications were prompt,
thorough, and proactive.
When NMPC management
was informed by the NRC staff of a
10 CFR Part 21 notification to the NRC from another licensee regarding potential defective fuel
injectors in Cooper-Bessemer
diesels, the NMPC technical staff had already been apprised of
the issue and had preliminary indications that the suspect injectors were not installed in the Unit
2 diesels.
NMPC also made a proactive decision to immediately verify the Unit 1 EDG rotor
pole mounting bolt torques rather than waiting to perform this check during an upcoming
refueling outage.
Likewise, NMPC took prompt action to inspect the Cooper-Bessemer
diesels
in Unit 2 for tin smearing
following the receipt of new inspection
guidance
from the
manufacturer,
C
<
~
28
Self-assessments
performed during the period provided objective and thorough assessments
of
performance to management.
The operation department self-assessment
programs were excellent
initiatives, which require some enhancements
to be fully effective.
The NMPC assessment
of
the Unit
1 loss of ultimate heat sink event was good.
Generally, the deviation/event report
system functioned as an effective tool to improve plant performance.
However, this system was
not utilized by site personnel to identify and correct a piecursor event to the dropping of the two
new fuel assemblies,
nor to identify the inoperability of the two turbine first stage pressure
sensors,
When the system was used, corrective actions were appropriate and the system was
properly monitored and audited for effectiveness.
Quality Assurance (QA) audits and surveillances were generally good;
The scope and number
of QA surveillances of radwaste activities were exceptional.
However, QA activities in some
cases were not fullyeffective in obtaining performance improvements.
During evaluation of the
loss of ultimate heat sink event, it was determined that NMPC had not been fully effective in
correcting the root causes of instances of failure to follow procedures
and inadequate
work
requests after these types of problems had been repeatedly identified in QA surveillances.
The
root causes ofQA-identified problems were in some cases not effectively corrected or acted upon
by site and corporate management.
With some exceptions as discussed in the Engineering and Technical Support area, a significant
number of licensing actions were effectively processed
by NMPC during this assessment
period.
These effectively processed actions included license amendment requests, exemptions, code relief
requests,
responses
to generic letters and bulletins, multi-plant issues,
and other regulatory
initiatives. Generally, these submittals reflected good safety perspective, were technically sound,
and supported resolution of the requested
actions or safety issues.
However, weaknesses
were
noted in the administrative review of retyped technical specification pages.
Licensee Event Reports (LERs) continued to be well-written and adequately described details of
the subject events.
For one report, however,
several key points were not fully developed.
When this issue was identified, NMPC promptly developed these points'and issued a supplement
to the LER.
29
umm
-
afe
Assessment/
uali
Verifi
i n
In summary,
management
oversight and supervisor involvement in day-to-day activities have
been extensive.
However, the high number of reactor scrams and significant events indicated
that management
had not been
fully effective at addressing
equipment
failures
and
the
longstanding personnel performance problems associated with attention-to-detail and procedural
adherence.
The safety oversight committees continued to perform a thorough and effective
~
review of issues.
The ISEG provided comprehensive
and effective self-assessments
and root
cause evaluations.
Responses
to 10 CFR Part 21 notifications and other industry notifications
'ere prompt, thorough, and proactive.
Although QA audits and surveillances were generally
good, the root causes of QA-identified problems were in some cases not effectively acted upon
by site and corporate management.
Most licensing actions continued to be technically sound,
and supportive of resolution of the requested action or safety issue; however, several exceptions
were noted which required additional interaction.
ID.G.2
III.G.3
Performance Rating:
Category
2
Board Comment:
NMPC should implement a focused effort to monitor and
reduce the number of scrams and significant events.
C
30
IV.
SlTEAC~
IV.ALicensee Activities
ANDEVALUATIONC
During this assessment
period Unit 1 operated at power until July 18, 1991, when increasing
unidentified drywell leakage resulted in an unplanned shutdown.
The cause of the leakage was
identified and repaired, and the unit was returned to power operations.
A number of additional
forced shutdowns occurred as highlighted in Section IV.B. Following a May 1, 1992, reactor
the unit remained
shutdown through the end of this assessment
period due to the
identification of significant cracks in the emergency cooling system condensate
return valves.
Reactor fuel was off-loaded to facilitate weld repairs and-replacement of the valves.
Unit 2 began the SALP period shutdown in an unplanned outage to facilitate repair to a leaking
reactor coolant system pressure boundary flexible hose.
A modification replaced the flexible
hose with piping that contained an expansion loop and the unit returned to power operations on
April 12, 1991. A number of forced shutdowns occurred as highlighted in Section IV.B. The
unit was shutdown on March 4, 1992, to commence
the second
refuel outage.
The unit
remained shutdown through the end of this assessment
period.
IV.B Unplanned Shutdowns, Plant Trips and Forced Outages
IV.B.1
nit 1
Date
1.
7/18/91
Power Level
3%
Root Cause
Unknown
Functional, Area
N/A
Increasing unidentified drywell leakage resulted in the initiation of a plant shutdown.
At 3%
reactor power a high neutron flux reactor scram occurred due to either a pressure surge caused
by isolation of an auxiliary steam load or due to a spurious spike of the intermediate range
neutron monitor (LER 91-08).
The unidentified drywell leakage initiated from a recirculation
pump motor cooler mechanical joint, main steam isolation valve packing, and the packing of a
recirculation loop isolation valve.
2.
9/26/91
97%
Equipment Failure
Maintenance
A reactor scram resulted from a turbine trip/generator load reject caused by a failed generator
phase differential current transformer (CT) (LER 91-12).
The failed CT was replaced.
Date
3.
12/4/91
Power Level
96.5%
31
Root Cause
Equipment Failure
Functional Area
Maintenance
A low water level reactor scram occurred following the failure of a solder connection in the
feedwater level control total steam flow meter.
The steam flow signal went to zero, which
generated
a large flow/error signal and closure of the feedwater control valves.
The total steam
flow meter was replaced with a new meter which had a shunt across
the input.and output
terminals to prevent reoccurrence of a zero output signal (LER 91-14).
4.
2/16/92
94%
Equipment Failure
Maintenance
A reactor
resulted
from a turbine
stop valve
10%
closure
signal
during weekly
surveillance testing of turbine stop valves.
A sticking pivot point and worn pin connection on
turbine stop valve 13 initiated the event (LER 92-04).
5.
4/18/92
98%
Equipment Malfunction
Maintenance
A high neutron flux reactor scram occurred due to failure of the mechanical pressure regulator
in the turbine control system (LER 92-08).
6.
5/1/92
97%
Equipment Malfunction
Maintenance
A high neutron flux reactor scram occurred due to failure of the electronic pressure regulator
in the turbine control system (LER 92-03).
IV.B.2
U~ni 2
Date
1.
8/13/91
Power Level
100%
Root Cause
Random Failure
Functional Area
N/A
An internal fault in the "B" phase main transformer caused
a turbine trip/generator load reject
resulting in a reactor scram,
The transformer fault created an electrical disturbance throughout
the normal electrical system, resulting in the loss offive non-safety related uninterruptible power
supplies.
As
a result,
the control room lost annunciation
and
most
balance of plant
instrumentation.
A Site Area Emergency was declared.
(LER 91-17)
2.
12/7/91
N/A
90%
Equipment Failure
During performance of the weekly turbine valve cycling surveillance,
the turbine stop and
combined intermediate valves inadvertently closed resulting in a reactor scram.
The most
probable cause of the event was a malfunctioning relay in the speed select circuit of the turbine
electro-hydraulic control system.
(LER 91-22)
lp
32
Date
Power Level
3.
12/12/91
55%
Root Cause
Personnel Error
Functional Area
Operations
During the start of a second feedwater pump to support raising plant power, a condensate
and
feedwater system transient occurred resulting in the loss of both feedwater pumps.
The loss of
all feedwater to the vessel resulted in a reactor scram on low vessel level.
The cause of this
event was attributed to poor work practices
and mis-communications
between operating shift
personnel.
Specifically, an inadequate
number of condensate
and condensate
booster pumps
were running to support operation of a second feedwater pump.
(LER 92-23)
4.
1/25/92
65%
Equipment Failure
Maintenance
A manual shutdown
was initiated due to excessive
leakage
from degraded
pump seals
on
feedwater pumps B and C.
IV.C NRC Inspection and Review Activities
Three NRC resident inspectors were assigned
to Nine MilePoint during the assessment
period.
NRC team inspections were conducted in the following areas:
Safety
related
check
valve
audit
performed
at
Unit 2
during
the
week
of
August 5, 1991.
Augmented inspection coverage of the Unit 2 site area emergency which occurred
on
August
13,
1991.
The augmented
inspection
team was
supplanted
by an incident
inspection team.
Restart
readiness
inspection
at Unit 2 conducted
the week of September
3,
1991
concerning restart following the site area emergency.
Electrical distribution system functional inspection conducted at Unit 1 from October 9
through 25, 1991.
. Augmented inspection coverage from February 22 through 28, 1992, at Unit 1 following
the loss of the ultimate heat sink event.
Reactive inspection conducted intermittently between March 28 and April 18, 1992, at
Unit 1 to assess
the effectiveness of NMPC short term corrective actions
taken in
response
to the loss of the ultimate heat sink event.
Augmented inspection coverage at Units
1 and 2 between March 24 and 27, to inspect
the Unit 2 loss of control room annunciators
and subsequent
loss of all off-site power.
4T
33
IV.DEscalated Enforcement Action
An enforcement conference was held on October 17, 1991 to discuss the ability of the Unit 2
'tandby gas treatment system to perform its containment drawdown function with a secondary
containment unit cooler inoperable.
A Severity Level IV violation was issued for loss of
configuration control on the unit cooler service water values during the markup process.
An enforcement conference
was held on February 6, 1992 in NRC Region I to discuss
the
dropping of two new fuel bundles at Unit 2.
A Severity Level IV violation was issued for
failure to follow procedural instructions.
'Two Severity Level IIIviolations and civilpenalties were issued on May 21, 1992 at Unit.1 near
the end of the period.
One violation concerned the failure of maintenance workers to implement
written procedures which resulted in the loss of the ultimate heat sink event. A $75,000.00 civil
penalty was issued.
The second violation concerned
operating
the unit with less than the
minimum number of operable instrument channels ofprotective instrumentation, and inadequate
corrective actions.
A $ 125,000.00 civilpenalty was issued.
IV.E SALP Evaluation Criteria
Licensee performance is assessed
in selected functional areas, depending on whether the facility
is in a construction or operational phase.
Functional areas normally represent
areas significant
to nuclear safety and the environment.
Some functional areas may not be assessed
because of
little or no licensee activities or lack of meaningful observations.
Special areas may be added
to highlight significant observations.
The following evaluation criteria were used,
as applicable, to assess
each functional area:
1 ~
Assurance of quality, including management involvement and control;
2.
Approach to the identification and resolution of technical issues form a safety standpoint;
3.
Enforcement history;
4.
Operational events (including response to, analysis of, reporting of, and corrective action
for);
5.
Staffing (including management);
6.
Training and qualification effectiveness.
Based upon the SALP Board assessment,
each functional area evaluated is classified into one of
three performance categories.. The definitions of these performance categories
are:
1
34
~C:
Ll
g <<'l l
l
l
yy
safeguards
resulted in a superior level of performance.
NRC will consider reduced levels of
inspection effort..
ogdgddgg: L'
<<
'
yly
yg
d
activities resulted in a good level ofperformance.
NRC willconsider maintaining normal levels
of inspection effort.
ggttggry 3: Licensee management attention to and involvement in nuclear safety or safeguards
activities
resulted in an acceptable
level of performance;
however;
because of the NRC's
concern that a decrease in performance may approach or reach an unacceptable level, NRC will
consider increased
levels of inspection effort.
The SALP report may include an appraisal of the performance trend in a functional area for use
as a predictive indicator.
Licensee performance during the assessment
period is examined to
determine whether a trend exists.
Normally, this performance trend would only be used ifboth
a definite trend is discernable
and continuation of the trend would result in a change
in
performance rating.
The trend, ifused, is defined as:
~Im rovin:
Licensee
performance
was determined
to be improving during the assessment
period.
D~ectinin: Licensee performance was determined to be declining during the assessment
period
and the licensee had not taken meaningful steps to address
this pattern.
HJ
I