ML14181A997

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Insp Rept 50-261/98-01 on 980104-0214.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML14181A997
Person / Time
Site: Robinson 
Issue date: 03/12/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A994 List:
References
50-261-98-01, 50-261-98-1, NUDOCS 9803230024
Download: ML14181A997 (32)


See also: IR 05000261/1998001

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

50-261

License No:

DPR-23

Report No:

50-261/98-01

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

January 4 - February 14, 1998

Inspectors:

B. Desai, Senior Resident Inspector

E. Girard, Region II Inspector

(Section E1.2)

M. Holbrook, NRC Contractor (Section E1.2)

J. Coley, Region II Inspector

(Section M3.1)

J. Lenahan. Region II Inspector

(Section E8.1)

M. Miller, Region II Inspector

(Section E8.1)

F. Jape, Region II Inspector

(Section E1.1)

Accompanying Personnel: T. Scarborough, NRR

Approved by:

M. Shymlock. Chief, Projects Branch 4

Division of Reactor Projects

Enclosure 2

9803230024 980312

PDR

ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Integrated Inspection Report 50-261/98-01

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection; in addition, it includes the results of

inspections by Region II based reactor safety inspectors, including those

related to the Motor Operated Valve (MOV) program as well as Architectural

Engineering (A/E) followup inspection.

Operations

The conduct of operations was professional, risk informed, and safety

conscious (Section 01.1).

Portions of the Service Water (SW) System and the Control Room Emergency

Filtration (CREFS) System were walked down and no negative observations

were noted (Section 01.2).

Activities related to control of water level of the Ultimate Heat Sink

(Lake Robinson) were appropriately conducted and met Technical

Specification (TS) and UFASR requirements (Section 01.3).

Nuclear Assessment Section and Plant Nuclear Safety Committee continued

to provide strong oversight (Section 07.1).

Maintenance

Maintenance and surveillance activities were performed satisfactorily.

The inspector noted good controls of housekeeping and good supervisor

oversight of work activities (Section 1M1.1 and M2.2).

The process followed by the licensee in handling a pin hole leak in

Component Cooling Water Line 10-AC-41 until a code repair could be

performed was correct and thorough (Section M2.1).

Changes made to maintenance and operation procedures which implemented

the more restrictive requirements delineated in the new Improved

Technical Specifications were found to be effective and thorough

(Section M.3).

Engineering

The inspector concluded that the modification program including

procedures, records, and post modification testing practices to be

technically and administratively adequate (Section E1.2).

Based on the NRC inspections of the licensee's implementation of

GL 89-10 and on the licensee's commitments in its letter dated

February 20, 1998, the NRC is closing its review of the GL 89-10 program

at Robinson (Section E1.2).

.2

The I&C technician exhibited good questioning attitude when he noticed

that the Ronan I/P had behaved differently than what he had remembered

from a previous conversation with the responsible engineer. A non-cited

violation was identified for not adequately considering the failure

modes associated with the installation of new Ronan I/P.

Upon

identification, the licensee immediately stopped the installation

activity and reconsidered the merits of the ESR as written (Section

E3.1).

A violation was identified with three examples of failure to update the

UFSAR in accordance with 10 CFR 50.71 (e). A non-cited violation was

also identified for the six examples of licensee identified UFSAR

discrepancies discussed in IR 50-261/97-201 (Section E8.1).

Overall, the inspector noted that the predictive maintenance program

continued to be on a positive trend (Section E2.1).

Plant Support

The inspectors concluded that radiation control and security practices

were proper (Section R1.1 and S1.1).

Overall licensee performance in 1997 in the Radiological protection area

was excellent (Section R1.2).

Report Details

Summary of Plant Status

Robinson Unit 2 operated at full power for the entire report period without

any significant problems.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended daily operation turnovers,

management reviews, and plan-of-the-day meetings to maintain awareness

of overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with Technical Specifications (TSs).

Instrumentation, computer indications, and safety system lineups were

periodically reviewed from the Control Room to assess operability.

Frequent plant tours were conducted to observe equipment status and

housekeeping. Condition Reports (CRs) were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and

resolved. Good plant equipment material conditions and housekeeping

continued to be observed throughout the report period.

In general, the conduct of operations was risk informed, professional,

and safety-conscious.

01.2 System Walkdown

a. Inspection Scope (71707)

The inspector walked down portions of the Service Water (SW) and the

Control Room Emergency Filtration System (CREFS).

b. Observations and Findings

The portions of the SW system walkdown included the intake. Emergency

Diesel Generator (EDG) supplies, CREFS supplies, a sample of the turbine

building loads, and the Component Cooling Water (CCW) supply. For the

portions walked down, the inspector did not observe any abnormalities.

The inspector did note that at the intake, the licensee had installed a

temporary portable sump pump to periodically pump down the manhole that

houses certain SW pump/valve cables. Due to rain water buildup in the

manhole, the licensee had noted lower than expected normal cable

insulation resistance. The sump pump was installed using a work request

(WR).

The inspector questioned the licensee if this should have been

installed as a temporary modification. The system engineer provided a

list of attributes associ.ated with the pump installation justifying that

a temporary modification was not warranted. The inspector reviewed the

requirements for temporary modification and concluded that licensee

actions were appropriate.

2 .

c. Conclusions

The inspector concluded that for the portions walked down, the SW and

the CREFS system were appropriately aligned. No negative observations

were noted.

01.3 Ultimate Heat Sink

a. Inspection Scope (71707)

The .inspector reviewed licensee actions related to heavy rainfall and

its affect on the Ultimate Heat Sink (UHS).

b. Observations and Findings

Recent heavy rainfall in the area has caused levels in Lake Robinson to

be higher than normal.

Lake Robinson is the UHS for the Robinson

Nuclear Plant. TS 3.7.8 requires a lake level of greater than 218 feet.

Normally, the lake level is maintained at approximately 221 feet. With

the recent heavy rainfall in the area, the lake level had risen above

the normal level.

The licensee controlled the lake level by releasing

water from the Robinson spilling way lake level to below 222 feet on

several occasions (ref. UFSAR section 2.4). The control of the lake

level is performed by the fossil unit (Unit 1).

The inspector monitored

this activity on one occasion and did not identify any problems

associated with the coordination and control of lake level to meet TS

and design requirements. Notwithstanding, the licensee is reviewing

possible ways to better coordinate control of the UHS. This includes

the possibility of having a Unit 2 verses Unit 1 procedure to control

and coordinate maintenance of the lake level.

c. Conclusion

The inspector concluded that the licensee appropriately controlled

activities to maintain the water level in Lake Robinson within required

limits.

07

Quality Assurance In Operations

07.1 Plant Nuclear Safety Committee and Nuclear Assessment Section Oversight

a. Inspection Scope (40500)

The inspector evaluated certain activities of the Plant Nuclear Safety

Committee (PNSC) and Nuclear Assessment Section (NAS) to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements.

b. Observations and Findings

The inspector periodically attended PNSC meetings during the report

period. The presentations were thorough and the presenters readily

responded to all questions. The committee members asked probing

questions and were well prepared. The committee members displayed

understanding of the issues and potential risks.

Further, the inspector

reviewed NAS audits and concluded that they were appropriately focused

to identify and enhance safety.

c. Conclusions

The inspector concluded that the onsite review functions of the PNSC

were conducted in accordance with TSs. The PNSC meetings attended by

the inspector were well coordinated and meetings topics were thoroughly

discussed and evaluated. NAS continued to provide strong oversight of

licensee activities.

08

Miscellaneous Operations Issues (92901, 92702)

08.1 (Closed) Violation 50-261/97-06-01, Inadequate safeguards procedures

that allowed ESF train being out-of-service without invoking a Technical

Specification action statement: The corrective actions presented in the

licensee's response, dated June 24, 1997, were reviewed and verified by

the inspector. The NRC accepted the response by letter, dated June 26,

1997. This violation is closed.

II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726 and 62707)

The inspector reviewed/observed all or portions of the following

maintenance related work requests/job orders (WRs/JOs) and/or

surveillances and reviewed the associated documentation:

WR/JO 97-AEIR1 and PM-420, Votes Testing

OST 401-1, EDG "A"

Slow Speed Start

WR/JO AAQM-001, CCW Heat Exchanger Cleaning

OST-302-1, Service Water System Component Test

WR/JO AAFI1, Replace Installed Fisher I/P with Ronan I/P

EST-124, Response Time Testing of Reactor Coolant System RTDs

b. Observations and Findings

The inspector observed that these activities were performed by personnel

Procedures were present at the work location and being followed.

4

Procedures provided sufficient detail and guidance for the intended

activities. Activities were properly authorized and coordinated with

operations prior to starting. Test and maintenance equipment in use was

properly calibrated, procedure prerequisites were met, and system

restoration was completed.

c. Conclusions

The inspector concluded that routine and corrective maintenance and

surveillance activities were performed satisfactorily.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Review of the Through Wall Flaw Evaluation and Operability Determination

Processes for a Pin Hole Leak in Component Cooling Water (CCW) Line

10-AC-41

a. Inspection Scope(62700)

The inspector observed.a reported pin hole leak in the moderate energy

CCW Line 10-AC-41 and reviewed documentation to determine if actions

taken by the licensee were in accordance with structural integrity

guidance given in NRC Generic Letter (GL) 90-05 for ASME Class 3 piping,

and guidance given for resolution of degraded and nonconforming

conditions and continued operability in NRC GL 91-18. Since this pipe

section could be isolated, code repair was successfully performed during

the week of February 9-13, 1998.

b. Observation and findings

The pin hole leak in the moderate energy CCW pipe 10-AC-41 was between

Valves CC-775 and CC-776. The subject pipe was the return pipe from the

Spent Fuel Pool Heat Exchanger. The thinned area was located downstream

of Valve CC-775, one-inch beyond the weld of the weld neck flange which

supports the valve. The circumferential position of the thinned area on

the pipe coincided with downstream edge of the butterfly valve disk and

was approximately centered at the 12 o'clock pipe position. The valve

was installed with the disk shaft horizonal. The positioning of the

valve make this location susceptible to erosion and would be exacerbated

by the increased turbulence resulting from throttling flow.

The inspector held discussions with cognizant engineers, reviewed the

ultrasonic test data for the remaining wall thickness of the affected

area on the 10-inch schedule 40 carbon steel pipe; verified that the

evaluation/calculation used to evaluate the structural integrity of CCW

Line 10-AC-41 with the through-wall flaw was acceptable based on the

criteria and methodology specified in GL 90-05 for ASME Code Class 3

moderate energy lines: and reviewed the operability determination (ESR

9800050) including the enclosed 10 CFR 50.59 Safety Evaluation

Unreviewed Safety Question Determination form. As a result of these.

reviews, the inspector concluded that the licensee's actions met.the

guidance given in GL 90-05 and GL 91-18 and the pin hole through-wall

5

flaw in CCW Line 10-AC-41, while undesirable, did not reduce the safety

margin for this system or endanger other equipment in the immediate

area.

c. Conclusion

The process followed by the licensee in handling the pin hole leak in

Component Cooling Water Line 10-AC-41 was correct and thorough. A code

repair of the leak was successfully performed.

M2.2 Containment Personnel Airlock Troubleshooting and Semiannual Airlock

Leakage Test

a. Inspection Scope (62707,61726)

The inspector observed portions of Special Procedure, SP-1418,

Containment Personnel Airlock Leakage Troubleshooting, and Engineering

Surveillance Test, EST-010, Containment Personnel Airlock Leakage Test

(semiannual). These tests were performed to comply with 10 CFR 50,

Appendix J, Option A, for Type B testing, and to fulfill the

requirements of TS Surveillance Requirement (SR) 3.6.2 for the

containment personnel airlock.

b. Observations and Findings

Previous airlock test results indicated higher than normal leakage

through the inner door of the personnel air lock. The licensee prepared

SP-1418 to provide a troubleshooting method for identifying the leakage

pathway for the personnel air lock. The inspector reviewed this

procedure and found it to be adequate. The technique utilized was to

pressurize the space between the inner and outer doors to about 20

pounds per square inch gauge (psig), and using a device called

Ultraprobe, detect the leakage location. The Ultraprobe is an

ultrasonic inspection system which detects noise due to the air leakage.

A briefing in the control room was held prior to beginning the

troubleshooting with all personnel involved. The inspector attended the

briefing and found it to be detailed and beneficial. Questions were

raised regarding personnel safety, Health Physics issues. TS compliance

and the test technique. These were all satisfactorily answered. The

test engineer was knowledgeable and very familiar with the

troubleshooting technique and the regulatory requirements.

Following the briefing, workmen proceeded to the job site. The

inspector witnessed the activities at the air lock. The craft personnel

were knowledgeable and experienced for their assigned tasks. The work

proceeded according to the approved procedure without exception.

Containment integrity was maintained throughout the test and no TS

action statements were entered. Communications were maintained between

0

the job site and the control room. In particular, good communications

6

was maintained between the two workmen inside the containment vessel and

those outside.

The licensee concluded that the leakage was located at a seal on the

inner door opening-closing mechanism and was within allowable limits.

Repairs have been scheduled for the upcoming refueling outage.

Following completion of the troubleshooting test, activities were

directed to performance of EST-010. The inspector reviewed EST-010, and

noted that the procedure had been updated with regard to the new

improved TS. This test procedure provided a method to satisfy the

testing requirement of 10 CFR 50 Appendix J, for Type B testing. This

test was required to be completed following maintenance on the air lock

and at least once every six months. Therefore, performing the test on

this date satisfied both requirements.

Discussion of the test was included in the briefing for the

troubleshooting activity discussed above. The inspector witnessed the

following portions of the test:

Installation and removal of the strong back on the inner door.

Achievement of the test pressure of 46.5 psig.

Completion of the stabilization period.

Completion of the test and evaluation of test results.

The test was conducted as prescribed by the procedure. Containment

integrity as well as communication was maintained wi.th the control room

throughout the test period. Upon completion of the test, test results

were reviewed and the acceptance criteria were met. Throughout the test

period, test activities were coordinated with reactor operators and

supervision. Special tools and instrumentation were.noted to satisfy

the test conditions and accuracy requirements as stated within the test

procedure.

c. Conclusions

The inspector concluded that maintenance and surveillance activities

were performed satisfactorily. Coordination between the various crafts

was observed to be excellent. Throughout the job, Health Physics and

security personnel were available to assist in getting the job done

without problems. Work control practices were observed to be

satisfactory. Materials and backup help were available either at the

job site or by phone call.

The procedures and-work instructions were

well prepared, were easy to follow, and were understood by the workmen.

M3

Maintenance Procedures and Documentation

M3.1 Verification that the New Improved Technical Specifications were

Properly Implemented into Maintenance/Operation Procedures

a. Inspection Scope (Technical Instruction 2515/130)(62700)

.7

Robinson Unit 2 has been operating with TS issued with the original

operation license on July 31, 1970, as amended from time to time. By

letter dated August 27, 1996, as supplemented by letters dated

December 18, 1996, January 17, February 18, March 27, April 4,

April 25, April 29, May 30, June 2, June 13, August 8, September 10,

October 2. (RNP RA/97-0216), October 2 (RA/97-0207), October 10, and

October 21, 1997, the licensee proposed to amend Appendix A of Operating

License No. DPR-23 to completely revise the TS. The proposed .amendment

(No. 176) was based upon NUREG-1431, "Standard Technical Specifications

- Westinghouse Plants," Revision 1 dated April 1995, and upon guidance

in the "NRC Final Policy Statement on TS Improvements for Nuclear Power

Reactors" (Final Policy Statement), Published on July 22, 1993 (58 FR

39132). The overall objective-of the proposed amendment, consistent

with the Final Policy Statement, was to rewrite, reformat, and

streamline completely the existing TS for Robinson.

Robinson implemented their new Improved Technical Specifications (ITS)

on November 13, 1997. During inspections documented in this report, the

inspector reviewed the marked-up TS conversion documents, the ITS, the

TS Bases, the Technical Requirements Manual (TRM), the Off-Site Dose

Manual (OSDM), the Core Operating Limits Report (COLR), self-assessments

performed by the licensee, verified TS requirement relocations, reviewed

procedures used to control the relocation of TS requirements, verified

implementation of more restrictive ITS requirements in plant

implementing procedures, and verified the accuracy of the licensee's

computer tracking system. The focus of the inspection however, was to

determine if new more restrictive ITS requirements were properly

implemented into maintenance surveillance test (MST) procedures. This

review also resulted in many operations surveillance test (OST)

procedures being reviewed because the ITS requirements were applicable

to both maintenance and operations.

b. Observations and Findings

Two self-assessment audits had been performed by the licensee to

determine the readiness for implementation of the ITS. Assessment No.

LIC/PR-97-04, dated April 14, 1997, verified the adequacy of more

restrictive requirements implemented in OSTs. Findings identified by

this assessment were effective in improving the ITS implementation

process. The inspection conducted by the inspector ran parallel to this

self-assessment except the inspector focused primarily on maintenance

activities. A sample of TS requirements listed as relocated in the

licensee conversion submittal to NRC were verified and reloc'ated to the

specified location. Thirty-four more restrictive ITS requirements were

verified to be properly implemented into maintenance and operation

procedures.. Procedure additions were accomplished in accordance with

the requirements of Administrative Procedure No. AP-022, Revision 28,

"Document Change Procedure."

Ninety-three implementing procedures were

reviewed by the inspector in the verification process. The more

restrictive changes were chosen from Sections 3.3, 3.4, 3.7, 3.8 and 3.9

of the TS. Correct implementing procedures for 15 more restrictive TS

requirements were also verified in the licensee's surveillance tracking

8

and scheduling system to ensure the accuracy of this system. In

addition, action items for Corrective Action Reports involving

inadequate procedures dated from September 1, 1997, through

January 31, 1998, were reviewed to determine if any examples of improper

implementation of ITS requirements had been detected during the field

use of revised procedures. This review did not reveal any inadequate

procedure discrepancy resulting from the implementation of the new TS.

c. Conclusion

Changes made to maintenance and operation procedures which implemented

the more restrictive requirements delineated in the new Improved

Technical Specifications were found to be effective and thorough.

M8

Miscellaneous Maintenance Issues (92902)

M8.1 (Closed) Violation 50-261/97-09-02:

Failure to properly calibrate OPDT

channels. The inspector verified that the corrective actions described

in the licensee's response, dated October 24, 1997, and accepted by the

NRC on November 6, 1997 to be completed. This issue and the corrective

actions were presented in LER 50-261/97-07-00, which was closed in NRC

Inspection Report 50-261/97-09. Changes were made to the Loop

Calibration procedures and the event was reviewed with appropriate plant

personnel to prevent recurrence. This violation is closed.

III. Engineering

El

Conduct of Engineering

E1.1 Onsite Engineering-Design Changes and Modifications

a. Inspection Scope (37551)

The inspector reviewed the licensee's plans and activities related to

design changes and modifications for the upcoming refueling outage

(RFO-18). Three modification packages were reviewed to access:

Design Control of the original design basis,

Review process of the modification packages,

Interface controls, and

Quality of the design packages.

b. Observations and Findings

The three Engineering Service Request (ESR) selected for review were as

follows:

ESR 9600113, Differential Pressure Transmittal Reorientation,

9

ESR 9700366, Safety Injection Pump Net Positive Suction Head

(NPSH) Improvement, and

ESR 97-00671, Emergency Core Cooling System (ECCS) Sump Screen

Replacement.

Each of these.packages was prepared using the licensee's procedure EGR

NGGC-005, Engineering Service Request. This procedure provides detailed

instruction regarding all aspects of a design change or modification.

ESR-9600113

The objective of this .modification was to improve the task of filling

and venting transmitters identified in Condition Report (CR) 95-0262.

The modification concentrated on minimizing the potential for gas or air

accumulation in the sensing lines and transmitter diaphragm.

The original installations of these Rosemount transmitters were per the

manufactures recommendation, but venting proved to be difficult and time

consuming. A mock setup, at the facility, demonstrated that this change

would be more effective and took less time in completing the venting

process. The problem was recognized by the licensee for several years

and previous corrective actions were not fully effective. Therefore the

licensee was determined to complete this modification of reorienting the

transmitters such that they will easier vent air or gases.

The licensee issued LER 50-261/95-009-00 and -01 which discussed this

problem as it related to the cold leg accumulator level. Also, the NRC

issued violation 50-261/95-30-01.regarding this problem. These reports

have been previously discussed in inspection Report 50-261/97-04.

ESR 96-00113 contains detailed instruction for all transmitters to be

reoriented. A 10 CFR 50.59 safety evaluation was included in the

package, which concluded that no unreviewed safety question resulted as

a result of this change. The safety evaluation also determined that the

UFSAR would require updating as a result of this change. Specifically,

several valves, shown in Fig. 6.3.2-2 of the UFSAR will be removed per

this modification and new supports for some transmitters would be added.

These changes are scheduled for the next UFSAR change submittal.

The package was reviewed by all necessary disciplines. This included

ALARA considerations, electrical design considerations, environmental

qualification, maintenance, outage planning, operations and the system

engineers. The quality of the package was satisfactory for the stated

objective.

ESR 9700366

In inspection report 50-261/97-201 a concern with net positive suction

head (NPSH) requirements for the Safety Injection (SI) system was

identified. Plant engineering personnel promptly began an evaluation to

determine the ability of the SI system to fulfill its intended system

.

10

functions. Upon discovery that a potential discrepancy existed in the

NPSH design calculation, the refueling water storage tank water level

was increased from the original value. This action provided sufficient

NPSH but did not provide a comfortable margin. Investigations continued

and one of the corrective actions presented in LER 50-261/97-008-00 was

to modify the SI system piping to gain additional NPSH and a comfortable

margin.

ESR 97-00366 is an emergent project for implementation in Refueling

Outage, RFO-18 and is intended to increase the NPSH by reconfiguring the

suction piping. The new piping configuration has been determined to

provide about 4 feet of additional head pressure for the "B"

SI pump and

5 feet of additional head pressure for the "C"

SI pump. The "A"

SI pump

was considered to have acceptable NPSH.

The modification package provides detailed instruction for the piping

changes. The replacement and reconfiguration design, material, and

construction requirements applicable to the system have been identified

in the modification package. The package requires a pressure test in

accordance with inservice inspection requirements.

ESR-9600671

During refueling outage 17, (RFO-17), the emergency core cooling system

(ECCS) sump screen in the containment building were noted to be in a

degraded condition. Prior to plant restart the sump screens were

repaired. The licensee issued LER 50-261/96-005-00 and CR 96-02152 to

describe the issue.

This modification was to replace the existing carbon steel ECCS sump

screens with stainless steel material.

The replacement screens, as

described in the modification package, will meet or exceed the total

flow area and wire mesh size as the original screens.

The inspector reviewed the modification package and determined that it

met the functional requirements and complied with the design inputs of

the original installation. It was designated as a configuration change

(CC) per EGR-NGGC-0005, Engineering Service Requests. No category A

drawings are affected and no change to the UFSAR will be required by the

CC.

The package has been reviewed and approved by the appropriate

engineering disciplines, and appropriate plant programs, such as ALARA,

Maintenance Rule, Quality Control, Containment Coatings, Fire Protection

and Maintenance Procedures. Operations and mechanical maintenance have

reviewed and accepted this CC.

The modification package invokes PLP-047, Foreign Material Exclusion

Area (FMEA) Program. PLP-047 prescribes a foreign material exclusion

area, FMEA, to be established based on nuclear safety and risk. Three

levels of control are defined. ESR-00671 states that a Level 2 FMEA is

required for this CC. The FMEA is established prior to beginning any

011

work activity. The inspector reviewed the licensee's plans for this CC

and agreed that a Level 2 FMEA is appropriate. The final step in the CC

is to complete an inspection in accordance with EST-139, Containment

Sump Inspection. This inspection satisfies the post-modification test

requirement.

c. Conclusions

The inspector concluded that the modification program including

procedures, records, and post modification testing practices were

technically and administratively adequate. The three packages reviewed,

by the inspector, were found to contain all of the necessary tools and

controls to be properly implemented. Each of these jobs relies heavily

on the Responsible Engineer (RE) properly performing assigned duties.

The RE is the single point of cbntact and is accountable for all change

activities through closeout.

E1.2 Implementation of Generic Letter (GL) 89-10."Safety-Related Motor

Operated Valve Testing and Surveillance"

a. Inspection Scope (Temporary Instruction 2515/109)

This inspection assessed the licensee's implementation of GL 89-10,

which was previously determined inadequate during NRC Inspection

50-261/96-12. This inspection identified two violations (VIOs) which

addressed the principal deficiencies found in the licensee's

implementation of GL 89-10. The first of these violations, identified

as VIO 50-261/96-12-05, involved inadequately justified design

assumptions and the use of incorrectly determined stem rejection loads

in calculating opening valve factors. The second, VIO 50-261/96-12-06,

involved inadequate evaluations of test results relative to

calibrations, test conditions, and anomalous test data. The interim'

status of the licensee's actions to resolve the violations and complete

implementation of GL 89-10 was reviewed during Inspection 50-261/97-12,

which found that the progress toward correcting the violations was

satisfactory.. The current inspection further evaluated the licensee's

corrective actions for both of the violations. The inspection also

examined several other topics, including the setup of the licensee's

butterfly valves, MOV operability evaluations, and concerns identified

by Inspection 50-261/97-12.

The inspection was conducted through reviews of documentation and

interviews with licensee personnel. In assessing the resolution of

violations and concerns, the. inspectors focused on a sample of valves

selected from a tabulation of MOV test information, valve factors,

capability margins, etc., which the licensee had prepared for its

GL 89-10 valves. The valve sample was as follows:

12

AFW-V2-16A

Auxiliary Feed Water Header Discharge to Steam

Generator "A"

RHR-744A

Residual Heat Removal to Reactor Coolant Cold Leg

Isolation

RC-536

Pressurizer Power Operated Relief Valve (PORV) Block

FCV-626

Thermal Barrier Outlet Isolation

SI-869

Loops "B"

and "C"

Hot Leg Injection Shutoff

SI-845C

Containment Spray Additive Tank Discharge Throttle

V6-16A

Service Water North Header Supply to Turbine Building

V6-16B

Service Water South Header Supply to Turbine Building

The inspectors reviewed the test packages, calculations, and engineering

evaluations for the above MOVs. Other documents reviewed included:

Standard Procedure EGR-NGGC-0203, "Motor-Operated Valve

Performance Predication, Actuator Settings, and Diagnostic Test

Data Reconciliation," Revision 4

Standard Procedure EGR-NGGC-0101, "Electrical Calculation of Motor

Output Torque for AC and DC Motor Operated Valves (MOVs),"

Revision 2

ESR-9700330, "Determination of MOV Valve Factors," Revision 1

ESR-9700328, "Determination of MOV Rate-of-Loading Factors,"

Revision 1

ESR-9700331, "Determination of MOV Stem Factors," Revision 1

Altran Technical Report No. 97111-TR-01, "Summary Report of MOV

Differential Pressure Test Evaluations," Revision 1

Calculation RNP-M/MECH-1245, "Set Up Calculation for MOV FW-V2

6B," Revision 8

Calculation RNP-M/MECH 1452, "Evaluation of Static and Dynamic

Test Data for AFW-V2-16A," Revision 2

Calculation RNP-M/MECH-1237, "Set Up Calculation for MOV RHR

744A," Revision 3

Generic Letter 89-10 Site Improvement Plan, Revision 0

Capability Table (tabulation of MOV test information, valve

factors, capability margins, etc.), Revision 3

b. Observations and Findings

1. Justifications for Assumptions (VIO 50-261/96-12-05)

Violation 50-261/96-12-05 identified that the valve factors (VFs), rate

of loading (ROL), and stem friction coefficients (COFs) assumed in

setting and capability calculations had not been adequately justified.

The inspectors examined the licensee's corrective actions for the

violation during Inspection 50-261/97-12 and verified completion of

several corrective actions specified by the licensee. However, the

Engineering Service Requests (ESRs) being prepared to establish and

justify the VFs, ROL, and COFs and the related corrections to the

licensee's calculations had not been completed at the time and their

adequacy could not be confirmed. During the current inspection, the

inspectors verified that the ESRs and calculations were complete and

reviewed the ESRs and selected calculations to determine if the VFs,

13

ROL, and COFs now being assumed were adequately justified. The findings

of the reviews are described below.

Valve Factors (Established and Justified in ESR 9700330)

The inspectors found that the VFs established for the majority of valve

groups were adequately justified and incorporated into the calculations.

However, several concerns were identified:

The licensee had not been able to test two 1500# Copes-Vulcan

14-inch parallel double-disc gate valves (RHR-750 and 751) to

determine their VF.

Further, there was no industry test data

currently-available for use in establishing their VF. In the

absence of directly applicable test data, the licensee

evaluated Electric Power Research Institute (EPRI) data from

tests of valves with similar disc and seat contact surfaces.

The maximum VF determined using this data was 0.61. Rather

than apply this value, the licensee elected to use higher, more

conservative VFs in its calculations. These valve factors were

based on evaluation of Robinson's overall gate valve test

results. The maximum flow isolation VF of 0.66 was selected

for closing and the maximum opening VF of 0.73 was selected for

opening. The opening VF was further increased to 0.78 to

account for Bernoulli effects. The inspectors found that the

selected valve factors were reasonable in comparison to general

industry results. However, they were concerned that the values

selected were not based on actual testing of this valve design

or a closely similar design. The licensee identified this

concern for resolution in its Generic Letter 89-10 Site

Improvement Plan. The plan indicated that the licensee would

participate in further industry efforts to obtain applicable VF

data for this valve design.

Robinson's PORV block valves (RC-535 and RC-536) were 1500#

Westinghouse 3-inch flex-wedge gate valves. The licensee was

not able to dynamically test these valves but obtained test

results from Comanche Peak testing of similar valves. Based on

the Comanche Peak blowdown test results, the licensee selected

an open valve factor of 0.60 and a close valve factor of 0.68.

These values appeared reasonable to the inspectors, based on

values typically applied in the industry. However, the

inspectors expressed concern that the licensee had not compared

the internals of its valves to the Comanche Peak valves to

assure similar blowdown performance. The licensee identified

this concern for resolution in its Generic Letter 89-10 Site

Improvement Plan, which indicated that it would either use the

EPRI Performance Prediction Methodology (PPM) or would compare

the internal configuration of the Comanche Peak valves to the

Robinson valves to establish the validity of the block valves

VFs.

14

Robinson's GL 89-10 program included five Velan 2-inch globe

valves. The.licensee was not able to dynamically test any of

these valves and selected a VF of 1.10 based on the results of

tests that Turkey Point performed on similar valves. The

inspectors found that the Turkey Point tests were performed

with cold water and were concerned that the test data might not

be directly applicable to Robinson's valves, which had high

fluid temperature operating.requirements. The inspectors'

concern was limited, as the licensee's valves had large thrust

capability margins. The licensee identified this concern for

resolution in its Generic Letter 89-10 Site Improvement Plan,

which indicated that additional industry information would be

obtained to support the VFs used for these globe valves. In

addition, the plan stated that the documented basis for the VFs

would be revised accordingly.

Fire Protection valves (FP-248, 249, 256, and 258) were 900#

Anchor/Darling 4-inch flex-wedge gate valves. The licensee

applied a 0.80 closing VF to these valves in thrust

calculations. No in-plant test results were available to

support this VF. The licensee had evaluated EPRI's prototype

test results and selected data points from four similar

Anchor/Darling valves to support the VF. Use of individual

EPRI prototype test results generally is not acceptable to the

NRC. However, in

this instance, the inspectors' concern was

limited, as the VF selected both satisfactorily bounded the

EPRI results and was conservatively high as compared to overall

industry VF determinations. Additionally, the licensee's

valves had large thrust capability margins (exceeding 40%).

The licensee's Generic Letter 89-10 Site Improvement Plan

addressed this concern and specified further efforts to obtain

applicable industry data for these valves.

Rate.of Loading (Established and Justified in ESR 9700328)

The inspectors found that the licensee used a non-standard but

conservative method for determining the rate of loading. The licensee

statistically analyzed the rate of loading values obtained from the

in-plant testing of Robinson's gate valves and determined that the mean

value was 5.6% with 2 standard deviations equal to 23.8%. The

inspectors found that the values established were satisfactory.

The licensee was not able to dynamically test any of Robinson's globe

valves to determine a rate of loading value to use in thrust

calculations.

Instead, the licensee analyzed the results from a limited

number of globe valves tested by EPRI. Based on this analysis, the

licensee established a mean value of 12.4% and 2 standard deviations

equal to 18.6% for use in its globe valve thrust calculations. The

inspectors found that the applied values were reasonable. As the globe

valves had large available thrust margins, the inspectors did not

identify any significant concern regarding the rate of loading values

selected. The inspectors noted that longer-term the licensee may

receive test results from its own testing or industry testing that will

permit better justification of the rate of loading selected for these

globe valves.

The'inspectors verified that the licensee properly employed the rate of

loading values from its analyses in its thrust calculations.

Stem Friction Coefficient (Established and Justified in ESR 9700331)

The licensee's calculations typically assumed and applied a 0.20 stem

friction coefficient (COF) value if the stem COF was measured under

static conditions and a more conservative 0.22 value if the COF could

not be measured under -any conditions. In isolated cases measured values

exceeded the 0.20 assumption and the measured values were used. The

inspectors found that the values used were reasonable based on COFs

obtained throughout the industry; however, the licensee's test results

did not support these values with a high degree of statistical

confidence. ESR 9700331 attributed this to inaccuracies in the torque

wrench method it had used in determining output torque, which caused the

calculated stem friction coefficients to be unrealistically high. The

licensee supported this assumption with the results of a study conducted

at its Harris plant. In that study, output torque obtained by the

torque wrench method was compared to more precise direct torque

measurements. The study determined that the measured torque values

obtained with the torque wrench method were on average 9% higher than

the direct torque measurements for Limitorque SMB-00 actuators and 25%

higher for SMB-1 actuators. The inspectors expressed concern that the

licensee had no precise direct torque measurements on Robinson's MOVs to

assure the adequacy of the COFs assumed. Robinson personnel stated that

testing was planned during Robinson's Refueling Outage (RO) 18

(March 1998) to verify this assumption. Further, in a letter to the NRC

dated February 20, 1998. the licensee specifically committed to perform

testing during RO 18 to provide more precise static and dynamic stem

factors to support the stem coefficient of friction assumptions

contained in ESR 9700331.

2. Use of Incorrect Stem Rejection Loads (VIO 50-261/96-12-05)

In addition to using inadequately justified assumptions, Violation

50-261/96-12-05 identified that the stem rejection loads used in

calculating opening valve factors were incorrect. NRC inspectors

examined the licensee's corrective actions for the violation during

Inspection 50-261/97-12 and verified completion of several corrective

actions specified by the licensee. However, the licensee had not

completed the revisions to correct the calculations. During the current

inspection, the inspectors verified that these actions were complete.

This verification was based on documented closure of the actions in

Condition Reports 96-3178 and -3179 and review of the calculation

examples listed previously. In addition, the inspectors reviewed the

calculation for a subsequent dynamic test performed January 8, 1998, on

valve AFW-V2-14C and verified that the reconciliation calculation

16

correctly determined and utilized the stem rejection load in determining

the open valve factor.

Inadequate Evaluation of Test Results (VIO 50-261/96-12-06)

Violation 50-261/96-12-06 identified that the licensee had not

adequately evaluated test results to assure that test requirements had

been satisfied. The licensee had not adjusted valve opening thrust

measurements for test measurement calibration errors, had failed to

recognize that test data indicated that the test conditions in some

tests were not as intended. Additionally, the licensee failed to

resolve significant anomalies exhibited in some test data. The

inspectors examined the licensee's corrective actions for the violation

during Inspection 50-261/97-12 and verified completion of the corrective

actions for this violation, except correction of calculations and

additional training of MOV personnel in interpretation of test data.

During the current inspection, the inspectors verified that the

calculations were complete and that they satisfactorily addressed the

inadequately evaluated test results. The verification was performed

through a review of the following calculation examples:

Calculation RNP-M/MECH-1245, Revision 8, "Set Up Calculation

for MOV FW-V2-6B" (revision addressed originally incorrect test

differential pressure)

Calculation RNP-M/MECH 1452, Revision 2, "Evaluation of Static

and Dynamic Test Data for AFW-V2-16A" (revision corrected the

maximum open force selected from test)

Calculation.RNP-M/MECH-1237, Revision 3, "Set Up Calculation

for MOV RHR-744A" (revision corrected actuator efficiency and

provided appropriate open calibration error)

Calculation RNP-M/MECH-1517, Revision 3, "Set Up Calculation

for MOV MS-V1-8C" (revision and provided appropriate open

calibration error)

Calculation RNP-M/MECH-1446, Revision 3, "Set Up Calculation

for MOV RC-536" (revision provided appropriate open calibration

error)

With regard to the additional training of MOV personnel specified as a

corrective action, the inspectors verified that the training was still

scheduled to be performed during RFO-18 (March 1998), was tracked in the

licensee's database, and was shown to be still open.

Butterfly Valves

The licensee.only had three butterfly valves in its GL 89-10 program.

These were identical 16-inch, 150# pressure class, Allis-Chalmers

butterfly valves. The safety function of each was to close and closure

was controlled by torque switch settings with the valves torquing closed

17

into stopnuts. The current capabilities were marginal (0.4-to 16.9%

margin above the required torque). The licensee planned a control

scheme change from torque switch to position control for closing, which

would increase this margin to above 20%. The inspectors verified that

work requests 97-AEIU1, -AEIW1, and -AEIX1 provided for the change to

position control during RFO-18 scheduled in March 1998.

The inspectors reviewed the calculations for two of the three butterfly

valves (V6-16A and B) and found that the torque requirements were

calculated using an industry equation. Packing, seating, and bearing

torque loads were based on static and dynamic tests performed on V6-16B.

The licensee assumed that the hydrodynamic torque was negligible

however, -the dynamic test which the licensee performed to establish the

capabilities of the valves was at too low a flow to validate this. In a

letter to the NRC dated February 20, 1998, the licensee responded to

this issue and committed to perform calculations, tests, and/or

inspections to evaluate the hydrodynamic torque requirements for

butterfly valves V6-16A/B/C. This would establish the validity of the

licensee's assumption that hydrodynamic torque was negligible. The

letter indicated these actions would be complete by June 25, 1998.

MOV Operability Evaluations

In a few cases the licensee's revisions to its calculations resulted in

negative design margins which were documented in operability

evaluations. The following valves were affected:

RHR-744A and B

CC-749A and B

FCV-626

FW-V2-6B

CVC-381

The inspectors reviewed each assessment and agreed with the licensee's

conclusions. The inspectors also reviewed outage plans and verified

that all of these MOVs were scheduled to be modified during the upcoming

RO 18 to increase their actuator capabilities.

6. Concerns Identified by Inspection 50-261/97-12

Inspection 50-261/97-12 documented a number of generally minor concerns

regarding the licensee's procedures, assumptions, etc. The inspectors

re-examined these concerns during the current inspection. With one

important exception, the concerns were satisfactorily addressed by

already completed actions or by planned actions described above. The

exception involved the licensee's use of handwheel turns to establish

closing limit switch control and torque switch bypass settings. The

inspectors noted that a more precise method of verifying these settings

(such as diagnostic trace analysis) would be appropriate, based on

.industry experience. In a letter to the NRC dated February 20, 1998,

verification of close limit switch and torque switch bypass settings for

18

valves that were position-controlled for accident scenarios, if the

valves were capable of being diagnostically tested. The letter

indicated these actions would be complete by June 25, 1998.

c. Conclusions

With the commitments made in the licensee's letter-dated February 20.

1998, the inspectors determined that .the licensee met the intent of

'GL 89-10 in verifying the design-basis capability of the safety-related

MOVs at Robinson. The licensee's letter identified the following

commitments:

Testing will be conducted during Refueling Outage 18 to support

the stem coefficient of friction assumptions contained in ESR

9700331.

The hydrodynamic torque requirements for motor-operated

butterfly valves V6-16A/B/C will be evaluated.

Site procedures will be revised to require diagnostic

verification of close limit switch and torque switch bypass

settings for valves that are position-controlled for accident

scenarios, if the valves are capable of being diagnostically

tested.

Based on the NRC inspections of the licensee's implementation of

GL 89-10 and on the licensee's'commitments in its letter dated

February 20, 1998, the NRC is closing its review of the GL 89-10 program

at Robinson. Resolution of the three outstanding licensee commitments

listed immediately above is identified as inspector followup item

50-261/98-01-01, GL 89-10 Commitments.

E2

Engineering Support of Facilities and Equipment

E2.1 Preventive and Predictive Maintenance Activities

a. Inspection Scope

The inspector reviewed and discussed licensee's preventive and

predictive maintenance activities.

b. Observations and Findings

During a review of the scope of the preventive maintenance (PM)

activities as they apply to major rotating equipment, the inspector

noted that numerous safety related motors, including the motors for the

containment spray pumps, safety injection pumps, EDG lube oil pumps,

and boric acid transfer pumps did not have a PM nor had they been

overhauled since initial installation. Upon questioning, the inspector

was informed that PM and overhaul of motors was not necessary as there

were other means of detecting an impending failure, such as the ASME

Section XI testing as well as predictive maintenance activities

19

performed on these equipment. Further, the inspector was also informed

that some of the motors associated with safety related systems were

normally in the standby mode, and therefore were not subjected to

excessive run times. The inspector reviewed procedure MMM-005,

Preventive Maintenance Program and noted that it did not give any

specific guidance with regard to motor PM and overhaul, including that

based on vendor recommendation. The inspector also noted that the

licensee did not have a documented basis for not.performing PM/overhaul

on certain motors. The inspector discussed this with the licensee and

was informed that this aspect of the PM program would be further

reviewed by the system engineer, including verification of vendor

recommendations. Further, based on plant specific requirements, the PM

would either be performed, or if not, appropriately justified.

The inspector also reviewed activities related to predictive

maintenance. The inspector reviewed a Self Assessment Report, RESS

96-34, that was conducted in late 1996 relative to the predictive

maintenance program, as well as Condition Report (CR) 96-02908 that was

generated to track the corrective actions from the self assessment.

This self assessment had identified several weaknesses: most significant

was that the predictive maintenance program was too segregated, leading

to inconsistent expectations for review and disposition by the system

engineers. Additionally, the self assessment identified weakness in the

overall integration of the predictive maintenance program with other

programs, including PM. Since the self assessment, the licensee had

initiated numerous efforts to address the weaknesses. This includes

management of the program by the rapid response team supervisor within

the site engineering organization, increasing program awareness, and

issuing a monthly status report. Key attributes of the program include

lube oil analysis, 'Vibration analysis, and thermography.. The licensee

currently has three engineers who are primarily responsible for the

implementation of the program. The inspector did note that the licensee

did not have an overall program document that describes and prescribes

the various attributes of the program. Currently, the licensee plans to

develop an overall program document in the middle part of 1998.

c. Conclusion

Overall,.the inspector noted that licensee efforts related to the

predictive maintenance program continue to be on a positive trend. The

absence of a predictive maintenance program document as well as the lack

of PM, including overhaul of certain safety related motors without

adequate justification was discussed with the licensee. The licensee

plans to address these issues in the near future to improve on existing

activities.

20

E3

Engineering Procedures and Documentation

E3.1 Steam Generator Power Operated Relief Valve (S/G PORV) Transducer (I/P)

Replacement

a. Inspection Scope (37551)

The inspector reviewed implementation of ESR 970047. This ESR was

originated to address a problem related to S/G PORV setpoint drift which

the plant experienced, and required frequent calibration. The ESR was

developed to replace the existing I/P with those that would yield better

dependability and accuracy.

b. Observation and Findings

Currently, the three S/G PORVs utilize Fisher 546 electro-pneumatic

signal I/Ps. These I/Ps were noted to be drifting due to sensitivity to

temperature variations as well as vibration. This drift required

frequent calibration to assure correct S/G PORV lift setpoint. The S/G

PORVs were tracked as maintenance rule a(1) category in accordance with

10 CFR 50.65. Consequently, the licensee developed and ESR to replace

the Fisher 546 I/Ps with Ronan X55-600 I/Ps. The Ronan I/P utilizes

advanced solid state technology and were designed to be less succeptable

to drift caused by variatiohs in temperature and vibration. During the

installation of the Ronan model, the licensee discovered'that the

failure mode of the newly installed Ronan model was different than what

was expected as well as required. The Fisher model I/P failure.mode

upon a loss of power was to fail the S/G PORV in the closed position.

The safety function of the S/G PORV is the closed position. The Ronan

I/P was found to default to a low pneumatic output upon loss of loop

current, i.e., loss of power. The low pneumatic output equates to the

S/G PORV failing in the open, i.e., non-safe position, upon loss of

power. The failure mode of the newly installed Ronan I/P was discovered

"co-incidently" by an I&C technician during installation when the loop

power isolated for an unrelated reason. Upon identification of this

problem, the I&C technicians stopped the installation and contacted the

responsible engineer.

The .inspector reviewed the circumstances related to the issue. It was

noted that the ESR had not specified the verification of the failure

mode as part of receipt (from vendor) or post modification testing. The

post modification testing associated with the ESR only included

calibration of the Ronan I/P. The inspector was informed by the

licensee that the manufacturer's documentation had not indicated the

failure mode and that the licensee was erroneously informed by the

manufacturer that the I/P fails with high output, i.e. safe position.

The licensee contacted the manufacturer following the identification of

the failure mode. At this time, the licensee.was informed that the

Ronan I/P failed with a low pneumatic output, i.e., different failure

mode than initially communicated.

21

The inspectors reviewed applicable requirements, including ANSI 45.2.11,

Quality Assurance Requirements for the Design of Nuclear Power Plants

and implementing licensee procedure EGR-NGGC-0005, Engineering Service

Requests. ANSI 45.2.11, Section 3 Design Input Requirements and

procedure EGR-NGGC-005, Attachment 2, Design Inputs, state that "The

design input shall include ... Failure effects requirements of

structures, systems, and components". Additionally, EGR-NGGC-005,

Section 9.4.7.j. Testing Requirements, states that "Testing shall verify

that: the modified system/component functions/performs as intended...".

Contrary to the above, the licensee had not adequately considered the

failure effect of the new Ronan I/P and appropriately prescribed a post

modification. test to verify that the modified system would perform as

intended. The inspector determined that failure to follow EDG-NGGC-005

in considering the failure effects was a violation. This licensee

identified, corrected, and non-repetitive violation is being treated as

an NCV, consistent with Section VII.B.1 of the NRC enforcement policy.

This issue is documented-as NCV 50-261/98-01-02:

Failure to Consider

Failure Modes For S/G PORV I/P ESR.

Upon identification, the licensee made a decision to back out of the ESR

and reinstall the "old" Fisher Model 546 I/P. Additionally, the

licensee decided to further review the availability of other designs

that best suited plant needs. Current licensee plans are to perform the

ESR in May 1998, following the completion of the outage. In the mean

time, the licensee will calibrate the I/Ps as needed, following drift.

Additionally, the S/G PORV will continue to.be monitored as a(1) system

in accordance with 10 CFR 50.65.

c. Conclusion

The I&C technician exhibited good questioning attitude when he noticed

that the Ronan I/P had behaved differently than what he had remembered

from a previous conversation with the responsible engineer. A non-cited

violation was identified for not adequately considering the failure

modes associated with the installation of new Ronan I/P. Upon

identification, the licensee immediately stopped the installation

activity and reconsidered the merits of the ESR as written.

E7

Quality Assurance in Engineering Activities

E7.1 Special UFSAR Review (37551)

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspector reviewed the applicable portions

of the UFSAR related to the areas inspected. The inspector verified

that for the select portions of the UFSAR reviewed, the UFSAR wording

was consistent with the observed plant practices, procedures and/or.

parameters.

22

E8

Miscellaneous Engineering Issues (92903) (37551)

E8.1 (Closed) Unresolved Item 50-261/97-201-05, AFW UFSAR Discrepancies:

Sections E.1.2.6. E.1.3.6. and E.1.4.2.6 of NRC Inspection Report (IR)

50-261/97-201 listed 11 comments/discrepancies in the updated final

safety analysis report (UFSAR). These were as follows:

1)

Changes to design and operation of the safety injection

(SI) and residual heat removal (RHR) pumps and the

effects of the design and operational changes on SI,

containment spray, and RHR pump NPSH were not discussed

in the UFSAR.

2)

UFSAR Table 6.2.4-1 (Table 6.4.2-1 listed in the IR was

the incorrect table number) had not been revised to

indicate that the discs of containment isolation valves

SI-860A, SI-860B. SI-861A, and SI-861B had been drilled

for pressure relief.

3)

UFSAR Table 6.3.2-5 stated that the maximum SI pump flow

rate is 550 gpm, which was less than the actual pump

maximum flow rate.

4)

UFSAR Section 10.4.8.2 did not list Anticipated Transient

Without Scram (ATWS) Mitigation System Actuation

Circuitry (AMSAC) as a start signal for AFW.

5)

UFSAR Table 10.4.8-1 incorrectly stated that the SDAFW

pump was 387 horsepower. The correct horsepower was 733.

6)

UFSAR Section 6.3.2.2.8 implied that a minimum of 300.000

gallons was available for delivery from the RWST. The

correct value was 277,999 gallons. This figure has been

revised again by the modification which increased RWST

level to address the insufficient NPSH problem.

7)

UFSAR Section 6.3.2.2.17 implied that the SI system high

pressure branch lines were designed for a pressure of

1500 psig. The correct value was 1750 psig.

8)

UFSAR Section 8.3.2 stated that station battery A cell

type was NCX. The correct cell type was NCN.

9)

UFSAR Section 8.3.1.1.2 referenced Motor Control Center

(MCC) numbers 5A1,

5A2, and 6A, and implied the number of

phases for the transformer supply was 30.

No MCCs

existed with these number designations. The correct

number of phases for the transformer supply to MCCs 9 and

10 was 3.

23

10)

UFSAR Table 8.3.1 did not reference Calculation RNP-E

8.016, Revision 5. However, this calculation was

referenced in Section 8.3 of the UFSAR.

11)

UFSAR Figures 8.3.1-3 and 8.3.1-4 stated that the CCW

pump motor was 400 horsepower. The correct horsepower

rating for the CCW motor was 350 horsepower.

The inspectors concluded that none of the above discrepancies

resulted in an unreviewed safety question. The inconsistencies in

the UFSAR concerning design and operation of the SI and RHR pumps

and the effects of the design and operational changes on SI,

containment spray, and RHR-pump net positive suction head were

included in resolution of Apparent Violation Item EEI 50-261-98

03-04. After further review of the issue concerning the need to

update UFSAR Table 6.2.4-1 concerning drilling of the discs of

containment isolation valves SI-860A. SI-860B, SI-861A. and SI

861B for pressure relief, the inspectors concluded that this did

not represent an error in the UFSAR. Further review of UFSAR

Section 6.3.2.2.3 disclosed additional inconsistencies in the SI

pump flowrate. The inspectors also noted that the SI pump design

parameters listed in Table 6.3.2-5 differed from those shown in

UFSAR Figure 6.3.2-4.

10 CFR 50.71(e) requires the UFSAR to be revised to include the

effects of all changes made in the facility or procedures as

described in the UFSAR. Examples 3-5 listed above of failure to

revise the UFSAR to include the effects of changes made in the

facility or procedures as described in the UFSAR was identified to

the licensee as violation item 50-261/98-01-03. Failure to Update

the UFSAR.

The licensee identified the discrepancies listed as Examples 6-11,

above, during their UFSAR review program, and corrective actions

were being initiated to update the UFSAR. This licensee

identified, corrected, and non-repetitive violation is being

treated as an NCV. consistent with Section VII.B.1 of the NRC

enforcement policy. This issue is documented as NCV 50-261/

98-01-04: Licensee Identified UFSAR Discrepancies.

E8.2 (Closed) Violation 50-261/97-07-03: ESR design verification

requirements. The corrective actions presented in the licensee's

response, dated August 5, 1997 were reviewed and verified by the

inspector. The NRC accepted the response by letter, dated August 18,

1997. Design verification was performed on the ESRs that had not been

design verified. The inspector verified a sample of these and had no

questions or problems. This violation is closed.

E8.3 (Closed) URI 50-261/97-07-02: Spent Fuel Pool Level Issues. By letter

dated March 27, 1997, the licensee informed the NRC that a discrepancy

had been identified with regard to the basis for the Improved Technical

Specification,-ITS, requirement to maintain 21 feet of water above the

24

spent fuel in the spent fuel pit. The issue was discussed in NRC

inspection report 50-261/97-07, paragraph E2.1. Due to the physical

limitation of the spent fuel pool, the ITS proposed limit of 23 feet

above the spent fuel could not be achieved. The licensee performed an

analysis of the issue and proposed a revision to the UFSAR Section

15.7.4, Design Basis Fuel Handling Accident. By letter dated October 2.

1997, the licensee submitted the issue to the NRC as a Unreviewed Safety

Question and requested the NRC to review and approve the proposed change

to the UFSAR. The licensee's analysis concluded that a significant

hazard would not be created by the change. The NRC reviewed the

methodology used by the licensee and concluded that the requested change

was acceptable. By letter dated January 27, 1998, the NRC informed the

licensee of the acceptance of the change and issued Amendment 177 to the

Facility Operating License No. DPR-23 for the Robinson facility. Unit 2.

The inspector verified the implementation of the change by reviewing the

UFSAR change, which is held in a pending file until six months after

Refueling Outage 18. scheduled for March 7, 1998. Night Order 97-016,

which was issued at the time this issue was discovered was canceled and

activities in the spent fuel pool are no longer restricted due to this

issue. This URI is closed.

E8.4 (Closed) Violation (VIO) 50-261/96-12-05: Unjustified design

assumptions and incorrect stem rejection load. Inspection 50-261/97-12,

determined that the corrective actions to resolve this violation had

been adequately completed, except for completion of assumption

justifications and correction of calculations. The assumption

justifications and calculations were reviewed by the inspectors during

the currentinspection (see E1.2 above).

The inspectors found that the

assumption justifications had been completed and that the calculations

had been corrected as stated in the licensee's response letters for this

violation. Several concerns were identified which are being

appropriately addressed by the licensee's Generic Letter 89-10 Site

Improvement Plan. The inspectors questioned whether the licensee had

sufficiently justified its design assumptions for stem coefficient of

friction. The licensee provided a commitment to address that issue,

which will be reviewed in the future as part of inspector followup item

50-261/98-01-OX, GL 89-10 Commitments.

This violation is closed.

E8.5

(Closed) Violation 50-261/96-12-06:

Inadequate evaluation of test

results.

Inspection 50-261/97-12, determined that the corrective

actions to resolve this violation had been adequately completed, except

for revisions to calculations and certain additional training of MOV

personnel. The calculation revisions were reviewed by the inspectors

during the current inspection (see E1.X above) and found to have been

satisfactorily completed. The training was not completed yet but was

scheduled to be performed in the upcoming outage (March 1998) and was

being tracked as an open corrective action in the licensee's database.

This violation is closed.

25

E8.6 (Closed) Inspector Followup Item (IFI) 50-261/96-12-07: Actions to

preclude pressure locking. This item was identified to verify the

adequacy of the licensee's long term actions to preclude pressure

locking of certain valves. This issue is now being addressed through a

safety evaluation report being prepared by the NRC Office of Nuclear

Reactor Regulation. This item is closed.

IV.

Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 General Comments (71750)

The inspector periodically toured the Radiological Control Area (RCA)

during the inspection period. Radiological control practices were

observed and discussed with radiological control personnel including RCA

entry and exit, survey postings, locked high radiation areas, and

radiological area material conditions. The inspector concluded that

radiation control practices were proper.

R1.2 Radiological Protection (1997 Performance Data)

a. Scope

The inspector reviewed and discussed overall licensee performance for

1997 in the Radiological Protection area.

b. Observations and Findings

For 1997, the cumulative dose at Robinson was 12.991 Person-Rem. This

was the lowest dose ever received at Robinson as well as at any of the

CP&L plants. Of the 775 monitored individuals, 471 individuals had non

measurable exposure. Of the people who had measurable exposure, the

five highest dose recipients had 285, 281, 246, 234, and 220 mRem. Four

of the five individuals were affiliated with the Radiation Protection

organization. The exposure level of the five individuals receiving the

highest dose were well within the 10 CFR 20 exposure limits. The

contaminated floor space was maintained at approximately 1.101 square

feet verses a plant goal of less than 1,500 square feet. There were a

total of 14 personal contamination events verses a goal of 50. The

number of locked high radiation areas remained unchanged at 5.

c. Conclusions

The inspector concluded that overall licensee performance in 1997 in the

Radiological Protection area was excellent.

26

Si

Conduct of Security and Safeguards Activities

51.1 General Comments (71750)

During the period, the inspector toured the protected area and noted

that the perimeter fence was intact and not compromised by erosion or

disrepair. Isolation zones were maintained on both sides of the barrier

and were free of objects which could shield or conceal an individual.

The inspector periodically observed personnel, packages, and vehicles

entering the protected area and verified that necessary searches,

visitor escorting, and special purpose detectors were used as applicable

prior to entry. Lighting of the perimeter and of the protected area was

acceptable and met illumination requirements.

R8

Miscellaneous Radiation Protection -and Controls (92904)

R8.1 (Closed) URI 50-261/97-01-06: Demonstrate Accurate Dose Monitoring and

Dose Assignment Practices and Procedures. An assessment of the

dosimetry program was completed during the report period for NRC

inspection report 50-261/97-01. Issues regarding demonstration of

accurate and reasonable dose tracking and dose assignment practices

were identified. Condition Report 97-00172 was issued by the licensee

to resolve these issues. CP&L corporate dosimetry procedure DOS-NGGC

0002, Dosimetry Issuance was revised on October 23, 1997. In addition,

the location of the thermo-luminescent-dosimeter (TLD) badge rack was

moved from the RCA entrance to a lower background area outside the

Security Building. On January 1, 1998 the licensee instituted the

policy of requiring personnel with access to the RCA to wear their TLD

home with them or store it outside the security fence. The site TLD

background badges are stored at the Visitor's Center to minimize any

contribution from the operating unit when background is subtracted.

These changes were reviewed and verified by the inspector. The

inspector concluded that the licensee had adequately addressed the

issues identified by this URI.

This URI is closed.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on No proprietary

information was identified.

27

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Boska, Manager, Operations

H. Chernoff. Supervisor, Licensing/Regulatory Programs

T. Cleary, Manager. Maintenance

J. Clements. Manager, Site Support Services

J. Keenan, Vice President, Robinson Nuclear Plant

R. Duncan, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outage Management

J. Moyer, Manager, Robinson Plant

D. Stoddard, Manager, Operating Experience Assessment

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Regulatory Affairs

D. Young. Director,. Site Operations

NRC

B. Desai, Senior Resident Inspector

M. Shymlock. Branch Chief, Region II

28

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving,

and Preventing Problems

IP 61726:

Surveillance Observations

  • IP

62700:

Maintenance Implementation

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 92904:

Followup - Plant Support

T12515/109:

Inspection Requirements for Generic Letter 89-10, Safety

Related Motor-Operated Valve Testing and Surveillance

T12515/130:

Improved Standard Technical Specification Implementation Audits

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Oype

Item Number

Status

Description and Reference

IFI

50-261/98-01-01

Open

GL 89-10 Commitments (Section E1.2)

NCV

50-261/98-01-02

Open

Failure to Consider Failure Modes For S/G

PORV I/P ESR (Section E3.1)

VIO

50-261/98-01-03

Open

Failure to Update the UFSAR (Section E8.1)

NCV

50-261/98-01-04

Open

Licensee Identified UFSAR Discrepancies

(Section E8.1)

Closed

Type Item Number

Status

Description and Reference

VIO

50-261/97-06-01

Closed

Inadequate safeguards procedures that

allowed ESF train being out-of-service

without invoking a Technical Specification

action statement.(Section 08.1)

VIO

50-261/97-09-02

Closed

Failure to properly calibrate OPDT

channels (Section M8.1)

NCV

50-261/98-01-02

Closed

Failure to Consider Failure Modes For S/G

PORV I/P ESR (Section E3.1)

URI

50-261/97-201-05 Closed

AFW UFSAR Discrepancies (Section E8.1)

29

NCV

50-261/98-01-04

Closed

Licensee Identified UFSAR

Discrepancies (Section E8.1)

VIO

50-261/97-07-03

Closed

ESR design verification requirements

(Section E8.2).

URI

50-261/97-07-02

Closed

Spent Fuel Pool Level Issues

(Section E8.3).

VIO

50-261/96-12-05

Closed

Unjustified Design Assumptions and

Incorrect Stem Rejection Load

(Section E8.4)

VIO

50-261/96-12-06

Closed

Inadequate Evaluation of Test

Results (Section E8.5)

IFI

50-261/96-12-07

Closed

Actions to Preclude Pressure Locking

(Section E8.6)

URI

50-261/97-01-06

Closed

Demonstrate Accurate Dose Monitoring

and Dose Assignment Practices and

Procedures (Section R8.1)