ML060300256

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IR 05000255-05-012; on 10/01/2005 - 12/31/2005; Palisades Nuclear Plant; Operator Performance During Non-routine Evolutions and Events; Operability Evaluations
ML060300256
Person / Time
Site: Palisades Entergy icon.png
Issue date: 01/25/2006
From: Christine Lipa
NRC/RGN-III/DRP/RPB4
To: Harden P
Nuclear Management Co
References
FOIA/PA-2006-0082 IR-05-012
Download: ML060300256 (36)


See also: IR 05000255/2005012

Text

January 25, 2006

Mr. Paul A. Harden

Site Vice President

Nuclear Management Company, LLC

Palisades Nuclear Plant

27780 Blue Star Memorial Highway

Covert, MI 49043-9530

SUBJECT: PALISADES NUCLEAR PLANT

NRC INSPECTION REPORT 05000255/2005012

Dear Mr. Harden:

On December 31, 2005, the U. S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Palisades Nuclear Plant. The enclosed report documents the inspection

findings which were discussed on January 5, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, two NRC-identified findings of very low safety (Green)

were identified. Both of these findings were determined to involve a violation of NRC

requirements. Additionally, a licensee-identified violation which was determined to be of very

low safety significance is listed in the report. However, because the violations were of very low

safety significance and because the issues have been entered into your corrective action

program, the NRC is treating these findings as a non-cited violations (NCVs) consistent with

Section VI.A.1 of the Enforcement Policy.

If you contest the subject or severity of a NCV, you should provide a response with a basis for

your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the

Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville

Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Palisades facility.

P. Harden -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRC's

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Christine A. Lipa, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket No. 50-255

License No. DPR-20

Enclosure: Inspection Report 05000255/2005012

w/Attachment: Supplemental Information

cc w/encl: J. Cowan, Executive Vice President

and Chief Nuclear Officer

R. Fenech, Senior Vice President, Nuclear

Fossil and Hydro Operations

D. Cooper, Senior Vice President - Group Operations

L. Lahti, Manager, Regulatory Affairs

J. Rogoff, Vice President, Counsel and Secretary

A. Udrys, Esquire, Consumers Energy Company

S. Wawro, Director of Nuclear Assets, Consumers Energy Company

Supervisor, Covert Township

Office of the Governor

L. Brandon, Michigan Department of Environmental Quality -

Waste and Hazardous Materials Division

Michigan Department of Attorney General

DOCUMENT NAME: E:\Filenet\ML060300256.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RIII

NAME CLipa:dtp

DATE 01/25/06

OFFICIAL RECORD COPY

P. Harden -2-

ADAMS Distribution:

HKN

LMP

RidsNrrDirsIrib

GEG

KGO

JAL3

JAE

CAA1

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

JRK1

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-255

License No: DPR-20

Report No: 05000255/2005012

Licensee: Nuclear Management Company, LLC

Facility: Palisades Nuclear Plant

Location: Covert, MI 49043-9530

Dates: October 1 through December 31, 2005

Inspectors: J. Ellegood, Senior Resident Inspector

J. Giessner, Resident Inspector

G. O'Dwyer, Reactor Engineer

R. Alexander, Emergency Response

Coordinator/EP Analyst

J. House, Senior Radiation Specialist

W. Snell, Senior Radiation Specialist

M. Gryglak, Reactor Inspector

S. Bakhsh, Health Physicist

Approved by: C. Lipa, Chief

Branch 4

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000255/2005012; 10/01/2005 - 12/31/2005; Palisades Nuclear Plant; Operator

Performance During Non-routine Evolutions and Events; Operability Evaluations

This report covers a 3-month period of baseline inspections. The inspections were conducted

by Region III inspectors and resident inspectors. This report includes two green findings with

associated NCVs. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination

Process (SDP)." Findings for which the SDP does not apply may be "Green" or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor

Oversight Process," Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealed Finding

Green: The inspectors identified one finding of very low safety significance and an

associated non-cited violation when plant personnel performed activities outside the

scope of the work package used to inspect the spent fuel pool crane. On

October 11, 2005, while raising a dry fuel storage (DFS) cask from the spent fuel pool

following loading of the cask, the emergency brake on the crane engaged. The

engaged emergency brake stopped movement of the load resulting in suspension of the

load partially out of the pool. During troubleshooting activities, the workers exceeded

the bounds of the approved work package by manipulating the brake release. This

finding represented a violation of the license by performing work contrary to

requirements specified by NUREG-0612. Corrective actions included reinforcing site

standards for procedural adherence as well as successfully lowering the DFS cask. The

licensee entered the item in the Corrective Action Program.

The finding was not suitable for evaluation under the SDP. However, because the

actions by the worker did not result in any load motion and both crane brakes remained

set, NRC management determined the finding to be of very low safety significance

(Green). This finding also affected the cross cutting area of human performance.

Cornerstone: Barrier Integrity

  • Green. The inspectors identified a finding of very low significance (Green) when the

licensee failed to declare the containment air cooler, VHX-4, SW piping inoperable and

take action in accordance with licensee procedures and technical specifications when a

through-wall (pressure boundary) leak existed. This finding represented a non-cited

violation of Technical Specifications 5.4, "Procedures," in that procedures were not

properly implemented which would have resulted in declaration of inoperability of

component. Corrective actions included conducting repairs to stop the leak. The

licensee entered the item in the Corrective Action Program. The deficiency was also an

issue in the cross-cutting area of human performance in that personnel did not properly

follow the procedure for determining operability.

1 Enclosure

The inspectors determined that the issue was more than minor because the finding

impacted the barrier integrity cornerstone attribute for containment barrier performance.

The deficiency affected the barrier integrity objective of providing reasonable assurance

that physical design barriers for the containment protect the public from radionuclide

releases in that part of the boundary to a closed system for a containment penetration

was breached. The finding was of very low safety significance since the breach in the

containment boundary was small and would have very little impact on offsite dose

evaluations. (Section 1R15)

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee has been

reviewed by the inspectors. Corrective actions taken by the licensee have been entered

into the licencees corrective action program. This violation and corrective actions are

discussed in Section 4OA7 of this report.

2 Enclosure

REPORT DETAILS

Summary of Plant Status

The plant operated at or near full Rated Thermal Power (RTP) during the inspection period with

the following exceptions:

  • On October 18, 2005, the licensee reduced power to 35 percent power when

high vibration was indicated on the main turbine. After determining the vibrations

were related to an indication problem and not actual turbine vibration, the plant

returned to 100 percent power on October 19.

  • On November 13, 2005, the licensee reduced power to 52 percent due to fouling

of cooling tower screens. The licensee returned the reactor to 100 percent

power on November 15.

  • On December 14, 2005, a spurious actuation of the 1-1 EDG load sequencer

resulted in a power reduction to 81 percent due to boron addition. The licensee

returned the reactor to 100 percent power on December 15.

  • On December 30, 2005, the plant shutdown to repair 3 leaking control rod drive

mechanisms and remained shutdown for the rest of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather (71111.01)

a. Inspection Scope

The inspectors reviewed the plants preparation for cold weather. This included a review

of the plants documentation including USAR and Technical Specifications (TSs),

walkdown activities, review of past adverse conditions and corrective actions as well as

a walkdown by the inspectors of equipment which could be adversely affected by cold

weather. The inspectors also reviewed the licensees cold weather procedures. The

safety system focus was on the safety injection system from the safety injection and

refueling water tank (SIRWT) and auxiliary feed water system. The documents

reviewed during this inspection are listed in the attachment.

This constitutes one sample.

b. Findings

No findings of significance were identified.

3 Enclosure

1R04 Equipment Alignment

.1 Partial Walkdowns (71111.04Q)

a. Inspection Scope

The inspectors completed two equipment alignment inspection samples by performing

partial walkdowns on the following risk-significant plant equipment:

During the walkdowns, the inspectors verified that power was available, that accessible

equipment and components were appropriately aligned, and that no open work orders

for known equipment deficiencies existed which would impact system availability.

The inspectors also reviewed selected condition reports related to equipment alignment

problems and verified that identified problems were entered into the corrective action

program with the appropriate significance characterization and that planned and

completed corrective actions were appropriate and implemented as scheduled. The

documents reviewed during this inspection are listed in the attachment.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Fire Area Walkdowns (71111.05Q)

a. Inspection Scope

The inspectors completed six fire protection inspection samples by touring the following

areas in which a fire could affect safety-related equipment:

C Condensate Pump Room (Fire Area 23)

C Emergency Diesel Room 1-2 (Fire Area 6)

C Emergency Diesel Room 1-1 (Fire Area 5)

C 1-C Switchgear Room (Fire Area 4)

C AFW Pump Room (Fire Area 24)

C East Engineering Safeguards Room (Fire Area 28)

The inspectors verified that transient combustibles and ignition sources were

appropriately controlled, and that the installed fire protection equipment in the fire areas

corresponded with the equipment which was referenced in the Updated Final Safety

Analysis Report, Section 9.6, "Fire Protection." The inspectors also assessed the

material condition of fire suppression systems, manual fire fighting equipment, smoke

detection systems, fire barriers and emergency lighting units. For selected areas, the

4 Enclosure

inspectors reviewed documentation for completed surveillances to verify that fire

protection equipment and fire barriers were tested as required to ensure availability.

The inspectors reviewed selected condition reports associated with fire protection to

verify that identified problems were entered into the corrective action program with the

appropriate significance characterization. The inspectors also verified that planned and

completed corrective actions were appropriate. The documents reviewed during this

inspection are listed in the attachment.

b. Findings

No findings of significance were identified.

.2 Fire Protection - Drill Observation (71111.05A)

a. Inspection Scope

The inspectors completed the annual inspection of evaluating the fire brigades

performance during an unannounced fire drill on December 18, 2005. The drill was

observed to evaluate the readiness of the plant fire brigade to fight fires. In addition,

reviews of procedures, fire fighting equipment, and corrective action for adverse

conditions were conducted. The inspectors evaluated the licensees critique of the drill

and actions taken as a result of the critique to verify the self-critical manner at the

debrief. Specific attributes evaluated were: (1) proper wearing of turnout gear and self-

contained breathing apparatus; (2) proper use and layout of fire hoses; (3) employment

of appropriate fire fighting techniques; (4) sufficient fire fighting equipment brought to

the scene; (5) effectiveness of fire brigade leader communications, command, and

control; (6) search for victims and propagation of the fire into other plant areas;

(7) smoke removal operations; (8) utilization of pre-planned strategies; (9) adherence to

the pre-planned drill scenario; and (10) drill objectives. This constituted one sample.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07B)

a. Inspection Scope

Regional inspectors reviewed documents associated with maintenance and inspection

of the mechanical seal heat exchangers and the bearing oil coolers for the high pressure

safety injection (HPSI) pumps (P66A & B). The heat exchangers count as two samples.

These heat exchangers were chosen based on their operational support function of

removing heat generated by the risk significant HPSI pumps. These heat exchangers

were also chosen based on the importance of the safety functions performed by the

risk-significant HPSI pumps during accidents. These heat exchangers had not been

inspected by any previous heat sink performance biennial inspection. While on site, the

inspector reviewed operability determinations, completed surveillances, vendor manual

information, associated calculations, and preventive maintenance activities; and

5 Enclosure

performed independent assessments to verify that these activities adequately ensured

proper heat transfer. The inspector also reviewed documentation to confirm that

methods used to maintain and monitor the operational effectiveness of the heat

exchangers were consistent with expected degradation and that the established

acceptance criteria were consistent with design accident requirements and accepted

industry standards. The inspectors walked down the HPSI pumps to ensure proper

installation and configuration of these heat exchangers. The inspectors verified that the

nameplates on the pumps' mechanical seal heat exchangers matched the licensees

vendor manual information.

The inspectors also reviewed documentation to verify performance of two attributes of

the ultimate heat sink (UHS.) The inspectors verified that the licensee had adequate

controls to ensure that UHS system and subcomponents were free from clogging due to

macrofouling and UHS would function properly during adverse weather conditions,(e.g.,

icing or high temperatures).

In addition, the inspectors reviewed condition reports concerning heat exchanger or heat

sink performance issues to verify that the licensee had an appropriate threshold for

identifying issues and to evaluate the effectiveness of the corrective actions to the

identified issues. The documents that were reviewed are included at the end of the

report.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11Q)

.1 Quarterly Review

a. Inspection Scope

The inspectors completed one inspection sample pertaining to licensed operator

requalification by observing licensed operator actions in the control room simulator on

November 2, 2005. The inspectors assessed the operators ability to use plant

procedures to respond to simulated plant alarms and emergency conditions. The

inspectors assessed the operators ability to evaluate plant conditions and determine the

proper emergency action level. The inspectors assessed the licensee evaluators' ability

to evaluate the operators performance and to identify operator performance

deficiencies.

b. Findings

No findings of significance were identified.

6 Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13Q)

a. Inspection Scope

The inspectors completed five inspection samples. The inspectors reviewed the

following five activities to verify that the appropriate risk assessments were performed

prior to removing equipment for work. The inspectors verified that risk assessments

were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete.

When emergent work was performed, the inspectors verified that the plant risk was

promptly reassessed and managed. The inspectors verified the appropriate use of the

licensees risk assessment tool and risk categories in accordance with Administrative

Procedure 4.02, Control of Equipment, revision 29, and Fleet Procedure FP-OP-RSK-

01, Risk Monitoring and Risk Management, revision 0. Documents reviewed are listed

in the attachment.

  • planned in service testing of P66A (HHSI pump) for the week of 10/2-10/8/2005;
  • planned in service testing of P66B (HHSI pump) and planned P-55B (charging

pump) repack during the week of10/15-10/21/2005;

  • planned work for EDG 1-2 90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> outage during the week of10/22-10/28/2005;

November 9, 2005; and

  • unplanned work on EDG 1-2 due to fuel leak on November 21, 2005.

The inspectors also verified that condition reports related to emergent equipment

problems were entered into the corrective action program with the appropriate

significance characterization. Specific condition reports related to risk management

during maintenance activities were reviewed to verify that planned corrective actions

were appropriate and had been implemented as scheduled.

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-routine Evolutions and Events (71111.14)

A. Inspection Scope

The inspectors completed four samples of non-routine events. For the non-routine

events described below, the inspectors reviewed operator logs, plant computer data,

and strip charts as appropriate to determine what occurred and how the operators

responded, and to determine if the response was in accordance with plant procedures:

  • On October 11, 2005, during dry fuel storage loading activities, an emergency

brake for the crane engaged, suspending a dry fuel storage cask partially out of

the pool. The inspectors observed licensee activities to determine the cause of

the brake's engagement and to lower safely the load back into the pool.

  • On October 19, 2005, a plant downpower to 35 percent was required by plant

alarm response procedures due to high indicated main turbine vibrations. After

7 Enclosure

investigation and troubleshooting, the high vibrations were determined to be an

indication problem and not actual vibration problem. The indication problem was

the result of a failed power supply.

  • On November 13, 2005, a plant downpower to about 50 percent power was

required due to the loss of the B cooling tower caused by leaf intrusion. The

debris caused the cooling tower screens to foul relatively quickly and required

prompt action to ensure the functionality of the cooling tower was retained.

  • On December 14, 2005, with the plant operating at 100 percent power, the 1-1

EDG load sequencer for design basis loads failed causing the actuation of

components which would start on the loss of offsite power with a design

accident. The failure simultaneously started the associated train's high head and

low head Emergency Core Cooling Pumps and caused the running charging

pump suction to shift from the Volume Control Tank (VCT) to the Boric Acid

Storage Tank. The charging pump injected about 200 gallons of concentrated

boric acid before being realigned to the VCT. The negative reactivity resulted in

a reduction of Power, Temperature (average), and reactor coolant system

pressure. A 10 degree F Temperature (reference) to Temperature (average)

deviation occurred, reactor coolant pressure dropped from 2060 to 1967 psig,

and power dipped from 100 to 81 percent following the boron injection and

actions taken to restore Temperature (average) and Temperature (reference).

Operators restored pressure, power, and temperature, and declared the 1-1

EDG inoperable. The inspectors observed the recovery from the transient and

the problem solving activities associated with it. All equipment responded as

expected due to the Load Sequencer Failure.

b. Findings

Introduction: The inspectors identified one finding of very low safety significance and an

associated non-cited violation when plant personnel performed activities outside the

scope of the work package used to inspect the spent fuel pool crane.

Description: On October 11, 2005, while raising a dry fuel storage cask from the spent

fuel pool following loading of the cask, the emergency brake on the crane engaged.

The engaged emergency brake stopped movement of the load resulting in suspension

of the load partially out of the pool. The licensee stopped DFS activities and developed

work instructions to inspect the crane and determine the cause for the brake

engagement.

The licensee developed a work package to inspect the crane and determine the cause

of the brake engagement. The work package developed for this activity did not include

manipulation of crane components. Status meetings held earlier in the day emphasized

that no crane component manipulations were currently planned. However, the workers,

after consultation with vendor representatives, moved the brake release to verify the

brake was set. Since early discussions regarding the scope of work clearly stated crane

components would not be manipulated, the inspectors discussed the activity with plant

management. Plant management was unaware of the manipulation prior to its

8 Enclosure

occurrence and subsequently determined the workers had exceeded the bounds of the

authorized work.

After evaluating the available data, the licensee developed and implemented a work

package to lower the cask to the floor of the spent fuel pool. Further troubleshooting by

the licensee determined the emergency brake had engaged due to an improperly set

torque limiter that engaged the brake prematurely. This torque limiter had been

adjusted using incorrect techniques in August, in part due to a failure to use a procedure

for resetting the torque limiter.

This finding also affected the cross cutting area of human performance. Specifically,

this finding addressees a failure to follow procedures.

Analysis: The inspectors concluded that working outside the bounds of a work package

on a crane with a suspended load that if dropped would damage the spent fuel pool

warranted a safety significance determination in accordance with IMC 0612. The

inspectors discussed the effects of a drop of the load with licensee personnel. Had the

load dropped, the spent fuel pool could have sustained severe damage. The inspectors

were also aware that the individuals involved in the work activity were not fully

knowledgeable of the crane's design, operation, and failure modes at the time the work

occurred. In order to compensate for the gap in knowledge, the licensee obtained

telephonic support from the crane vendor. Therefore, the inspectors concluded working

outside the bounds of the approved work package and manipulating the brake release

represented an increase in the risk of a load drop. This increase in risk is directly

associated with the reactor safety cornerstone objective of the spent fuel cooling system

as a radiological barrier.

The finding was not suitable for evaluation under the SDP. However, because the

actions by the worker did not result in any load motion and both crane brakes remained

set, NRC management determined the finding to be of very low safety significance

(Green).

Enforcement: License Amendment No. 215 approved modifications to the facility

license to increase the spent fuel pool crane capacity to 110 tons and reflect the single

failure proof design of the crane. The associated amendment request identified

NUREG-0612, Control of Heavy Loads at Nuclear Power Plants, as a regulatory

requirement. NUREG-0612 requires licensees to have procedures in place for load

handling operations over or in the proximity to irradiated fuel. Contrary to this

requirement, the licensee performed work on the spent fuel pool crane by manipulating

its components without written procedures in place authorizing the particular task.

Because the finding was of very low safety significance and the finding was entered

into the licensee's corrective action program (CAP 01000753) this violation is being

treated as an NCV consistent with Section VI.A.1 fo the NRC enforcement Policy

(NCV 05000255/2005012-01).

9 Enclosure

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

For the three operability evaluations described in the Operability Recommendations

(OPRs) listed below, the inspectors evaluated the technical adequacy of the evaluations

to ensure that TS operability was properly justified and the subject component or system

remained available such that no unrecognized increase in risk occurred. The inspectors

reviewed the UFSAR to verify that the system or component remained available to

perform its intended function. In addition, the inspectors reviewed compensatory

measures implemented to verify that the compensatory measures worked as stated and

the measures were adequately controlled. In addition, the inspectors verified that the

condition reports generated for equipment operability issues were entered into the

licensees corrective action program with the appropriate significance characterization.

Documents reviewed are listed in the attachment.

  • OPR 01000525-01, Control Room Cooler VHX-4 through-wall service water leak
  • OPR000096, Intake crib degradation
  • OPR - CAP 33264, CCW non-conformance of fluid temperatures during design

accidents

b. Findings

Introduction: An inspector-identified finding of very low significance (Green) and an

associated non-cited violation of TS 5.4, "Procedures", occurred when the licensee

failed to declare the containment air cooler, VHX-4, inoperable when a through wall leak

was discovered on a service water (SW) pipe for that cooler. The SW piping serves as

part of a closed system for the containment boundary. The ASME Class III component

should have been declared inoperable with the appropriate actions taken as required by

the sites quality procedure for operability determinations, FP-OP-OL-01.

Description: On October 9, 2005, after completion of surveillance testing which

performed cycling of the inlet and outlet valves to the control air coolers service water

(SW) side, the licensee noted that level in the containment sump was rising more rapidly

than normal (from .15 gpm to .5 gallons per minute). Based on inspection and sampling

the licensee determined that the leak was from the VHX-4 control air cooler service

water supply.

The licensee marked "N/A" for an immediate operability assessment on the associated

CAP because service water to VHX-4 was not required during an accident. Although

the piping formed part of the containment boundary as a closed loop inside containment,

the licensee had previously evaluated containment integrity in Operability Evaluation

CPAL 0101971 (May 25, 2001) for leaks up to 1 gpm. Therefore, the licensee

concluded no further operability evaluation was required.

A detailed inspection on October 11, 2005 indicated the leak was coming from two

locations on a single 5/8" diameter brazed joint. Since this had occurred in the past and

was inside of the 1 gallon per minute rate of the previous evaluation the licensee

10 Enclosure

believed there was no question of operability. The inspectors questioned this

assessment since the potential impact to containment integrity was not evaluated if the

crack propagated. The inspectors questioned whether with the SW system no longer

closed, if containment pressure in an accident could act to move containment activity

through the penetration and into the SW system discharge (which discharges to mixing

basin and the lake). Although the leak was not large at the time, since it was through

wall, the licensee could not assume the flaw would not propagate. The piping is ASME

Code Class III.

The inspector reviewed the current guidance issued on September 26, 2005 in

RIS 2005-05: Revision to Guidance Formerly Contained in Generic Letter 91-18,

"Information to Licensees Regarding Two NRC Inspection Manual Sections on

Degraded and Non-conforming Conditions and on Operability" and the previous

guidance in GL 91-18 and the Part 9900 guidance: "Operable/Operability: Ensuring the

Functional Capability of a System or Component". RIS 2005-05 stated: "If the flaw is

through wall or does not meet the limits established in the Code, the component and

part of the system containing the flaw is inoperable." The previous GL 91-18 provided

similar guidance. The guidance permitted a flaw evaluation to determine if the piping

can be placed back in service. The licensee has implemented NMCs Corporate Office

Quality Procedure for Operability Determinations, FP-OP-OL-01, which states for Code

components, that the Shift manager SHALL declare a component whose pressure

boundary has leakage inoperable. For Class 3 piping, the system containing the

through wall flaw may be considered operable after it has been evaluated and found to

meet the acceptance criteria in Generic Letter 90-05. Since the licensee had not

completed a flaw evaluation, had not isolated the component and had not declared the

affected component inoperable, the inspectors concluded the licensee was not

complying with applicable requirements.

The inspectors shared the information regarding the GL 91-18 guidance with plant

management on October 13, 2005 who had been unaware of the information. The

licensee accelerated the repair of the VHX-4 cooler and completed it the same day

(October 13, 2005).

Analysis: The failure to declare the VHX-4 cooler SW piping inoperable and take action

in accordance with licensee procedures when the through wall leak existed was a

performance deficiency which warranted a significance determination. The inspectors

determined that the issue was more than minor in accordance with IMC 0612,

Appendix B because the issue impacted the barrier integrity cornerstone attributes for

containment barrier performance. The deficiency affected the barrier integrity objective

of providing reasonable assurance that physical design barriers for the containment

protect the public from radio nuclide releases because part of the boundary to a closed

system for a containment penetration was breached.

Using IMC 0609, Appendix A, "SDP Phase 1 Screening Worksheet for IE [Initiating

Events], MS [Mitigating Systems] and B [Barrier Integrity] Cornerstones" the inspectors

determined the finding impacted the barrier integrity cornerstone. Although a large

amount of water leakage could impact the flood plane and thus plant mitigation

equipment in the containment, the licensee demonstrated that the functionality of

mitigating systems was not lost. Since the finding did represent an actual open pathway

11 Enclosure

in the physical integrity of reactor containment on a designed closed system, IMC 0612,

Appendix H was used. Using Table 4.1, Containment-Related SSCs Considered for

Large Early Release Requency (LERF) Implications, due to the small size of pipe (even

if completely failed) which is less than 1-2" diameter, there is no or little impact to LERF.

Therefore this issue screens as Green. Although a complete failure of the pipe could

potentially exceed the TSs for allowed containment leakage, an additional evaluation by

the licensee indicated the impact on offsite dose would have been negligible.

This finding also affected the cross cutting area of human performance. Specifically,

this finding addressees a failure to follow procedures as well as a lack of knowledge of

procedural requirements, which, in accordance with IMC 0612, affects the cross-cutting

area of human performance.

Enforcement: Technical Specification 5.4 requires that procedures be established,

implemented, and maintained as recommended in Regulatory Guide 1.33, Revision 2.

Regulatory Guide 1.33, Appendix A, Section 1c indicated procedures should be

implemented on equipment control for safety-related equipment. The plant procedure

for implementing equipment control, Administrative Procedure 4.02, requires the Fleet

Operations Procedure, FP-OP-OL-01 "Operability Determination," be followed for

assessing the operability of plant safety related SSCs when operability is in question

(Section 9.1.2 of "Equipment Status"). Contrary to this requirement, procedure FP-OP-

OL-01 "Operability Determination" was not properly implemented in that the procedure

required the Shift Manager to declare components inoperable which had pressure

boundary component leakage (Class I, II or III). This action was not completed for the

VHX-4 cooler through wall leak, and no action was taken to evaluate the Class III

component flaw consistent with industry standards or remove the component from

service. Because this violation was associated with a finding of very low safety

significance and because the finding was entered into the licensees corrective action

program (CAP 01000525), this violation is being treated as an NCV, consistent with

Section VI.A.1 of the NRC Enforcement Policy (NCV 05000255/2005012-02). The

corrective actions included repairing the leaking component using an acceptable

procedure.

1R16 Operator Work Arounds (71111.16)

a. Inspection Scope

The inspectors completed one inspection sample regarding operator work arounds.

This was the semiannual review which evaluates workarounds for the cumulative impact

to operators in response to transients and accidents. The inspectors reviewed the

cumulative effects of deficiencies that constituted operator workarounds to determine

whether or not they could affect the reliability, availability, and potential for mis-operation

of a mitigating system; affect multiple mitigating systems; or affect the ability of

operators to respond in a correct and timely manner to plant transients and accidents.

The inspectors also assessed whether operator workarounds were being identified and

entered into the licensees corrective action program at an appropriate threshold.

Documents reviewed are listed in the attachment.

12 Enclosure

b. Findings

No findings of significance identified.

1R19 Post Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the three post-maintenance tests listed below to verify that

procedures and test activities ensured system operability and functional capability. The

inspectors reviewed the licensees test procedure to verify that the procedure

adequately tested the safety functions that may have been affected by the maintenance

activity, that the acceptance criteria in the procedure were consistent with information in

the applicable licensing basis and/or design basis documents, and that the procedure

had been properly reviewed and approved. The inspectors also witnessed the test or

reviewed the test data, to verify that test results adequately demonstrated restoration of

the affected safety function(s). Further, the inspectors reviewed condition reports to

verify that post maintenance testing problems were entered into the corrective action

program with the appropriate significance characterization. For select condition reports,

the inspectors verified that the corrective actions were appropriate and implemented as

scheduled. Documents reviewed are listed in the attachment.

C Auxiliary feedwater actuation system retest following channel repair

C VHX-4 containment air cooler service water leak repairs

C EDG 1-1 design basis accident sequencer retest

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20)

a. Inspection Scope

On December 30, 2005, the plant implemented a scheduled outage to repair the Control

Rod Drive seals on three leaking seals. The inspectors observed control room activities

during shutdown. The inspectors also completed a walkdown of accessible portions of

containment with site personnel. The inspectors evaluated these activities to ensure

licensee personnel were performing activities within TS requirements, plant procedures,

and other applicable requirements. This activity extended into the first quarter of 2006;

therefore, the remainder of the inspection will be included in NRC Inspection Report 05000255/2006-02. The inspectors completed one inspection sample.

b. Findings

No findings of significance were identified.

13 Enclosure

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors witnessed two surveillance tests and/or reviewed test data of selected

risk-significant SSCs, listed below, to assess, as appropriate, whether the SSCs met

the requirements of the TS; the UFSAR; Palisades Administrative Procedure 9.20,

TS Surveillance and Special Testing Program; Engineering Manual EM-09-02 and

EM-09-04, Inservice Testing of Plant Valves and Inservice Testing of Selected Safety

Related Pumps. The inspectors also determined whether the testing effectively

demonstrated that the SSCs were operationally ready and capable of performing their

intended safety functions. Further, the inspectors reviewed selected condition reports

regarding surveillance testing activities. The inspectors verified that the identified

problems were entered into the licensees corrective action program with the appropriate

significance characterization and that the planned and completed corrective actions

were appropriate. Additional documents reviewed are listed in the attachment.

C QO-19, Inservice Test Procedure on P66B, High Pressure Safety Injection Pump

C DWO-1, TS Surveillance Procedure: Operator Daily/Weekly Items for plant heat

balance and calculation of the calorimetric power

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspectors performed a screening review of Revisions 11 and 12 of the Palisades

Nuclear Plant Site Emergency Plan to determine whether the changes made in

Revisions 11 and 12 decreased the effectiveness of the licensees emergency planning

program. The screening review of these revisions did not constitute an approval of the

changes and, as such, the changes are subject to future NRC inspection to ensure that

the emergency plan continues to meet NRC regulations.

These activities completed one inspection sample.

b. Findings

No findings of significance were identified.

14 Enclosure

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Job-In-Progress Reviews

a. Inspection Scope

The inspectors selected two jobs being performed in radiation areas, potential airborne

radioactivity areas, and high radiation areas (HRAs) for observation of work activities

that presented the greatest radiological risk to workers and included areas where

radiological gradients could be present. This work was estimated to result in higher

collective doses and involved dry cask fuel storage welding operations and other

selected work areas.

The inspectors reviewed radiological job requirements including radiation work permit

(RWP) and work procedure requirements, and attended as low as is reasonably

achievable (ALARA) job briefings. Job performance was observed with respect to these

requirements to ascertain whether radiological conditions in the work area were

adequately communicated to workers through pre-job briefings and radiological

condition postings. This review represented one sample.

The inspectors also evaluated the adequacy of radiological controls including required

radiation, contamination and airborne surveys for system breaches and entry into HRAs.

Radiation protection job coverage, which included direct visual surveillance by radiation

protection (RP) technicians along with the remote monitoring and teledosimetry systems

and contamination control processes was reviewed to assess the effectiveness of

worker protection from radiological exposure. This review represented one sample.

Work in HRAs having significant dose rate gradients was observed to assess the

application of dosimetry to effectively monitor exposure to personnel and to evaluate the

adequacy of licensee controls. The inspectors observed RP coverage of dry cask fuel

storage welding operations which required controlling worker locations based on

radiation survey data and real time monitoring using teledosimetry in order to maintain

personnel radiological exposure ALARA. This review represented one sample.

b. Findings

No findings of significance were identified.

15 Enclosure

2OS2 As Low As Is Reasonably Achievable (ALARA) Planning And Controls (71121.02)

.1 Problem Identification and Resolution

a. Inspection Scope

The inspectors determined that the licensees self-assessment program identified and

addressed repetitive deficiencies and significant individual deficiencies that were

identified in the licensee's problem identification and resolution process. This review

represented one sample.

Corrective action reports related to the ALARA program were reviewed and staff

members were interviewed to determine if follow-up activities had been conducted in an

effective and timely manner commensurate with their importance to safety and risk

using the following criteria:

  • initial problem identification, characterization, and tracking;
  • disposition of operability/reportability issues;
  • evaluation of safety significance/risk and priority for resolution;
  • identification of repetitive problems;
  • identification of contributing causes;
  • identification and implementation of effective corrective actions;
  • resolution of NCVs tracked in the corrective action system; and
  • implementation/consideration of risk-significant operational experience feedback.

This review represented one sample.

b. Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

(71122.01)

.1 Inspection Planning

a. Inspection Scope

The inspectors reviewed the most recent Radiological Effluent Release Report for 2004,

dated March 29, 2005, along with current effluent release data to determine if the

program was implemented as described in the Radiological Environmental TS/Offsite

Dose Calculation Manual (RETS/ODCM), and the Updated Final Safety Analysis Report

(UFSAR). The effluent report was also evaluated to determine if there were any

significant changes to the ODCM or to the radioactive waste system design and

operation. There were no significant changes to the ODCM. Radioactive waste system

modifications and licensee technical reviews were evaluated to determine if those

16 Enclosure

changes would alter dose consequences to the public and if there would be any

potential impact on radiation monitor set-point calculation methodology. There were no

anomalous results in the effluent report.

The RETS/ODCM and UFSAR were reviewed to identify the effluent radiation

monitoring systems and associated flow measurement devices. Licensee records

including condition reports, self-assessments, audits, and special reports were reviewed

to determine if there were any radiological effluent performance indicator occurrences or

any unanticipated offsite releases of radioactive material for follow-up. The UFSAR

description of all radioactive waste systems was reviewed. This review represented one

sample.

b. Findings

No findings of significance were identified.

.2 Onsite Inspection

a. Inspection Scope

The inspectors walked down the major accessible components of the gaseous and

liquid release systems, including radiation and flow monitors, tanks, and vessels. This

was done to observe current system configuration with respect to the description in the

UFSAR, ongoing activities, and equipment material condition. This review represented

one sample.

The inspectors reviewed system diagrams of the radioactive liquid waste processing and

release systems to determine how liquid radwaste was processed to determine if

appropriate treatment equipment was used and that radioactive liquid waste was

processed in accordance with procedural requirements. Liquid effluent release

packages including projected doses to the public were reviewed to determine if

regulatory effluent release limits were exceeded. The inspectors reviewed system

diagrams of the radioactive gaseous effluent processing and release systems and

observed the collection and analysis of a gaseous radwaste sample to determine if

appropriate treatment equipment was used and if the radioactive gaseous effluent was

processed and released in accordance with RETS/ODCM requirements. Radioactive

gaseous effluent release data including the projected doses to members of the public

was evaluated to determine if regulatory effluent release limits were exceeded. This

review represented one sample.

The inspectors reviewed the licensees process for making releases with inoperable

effluent radiation monitors to determine if adequate compensatory sampling and

analyses were performed and to determine if an adequate defense-in-depth was

maintained against an unmonitored, unanticipated release of radioactive material to the

environment. This included projected radiological doses to members of the public.

There were no abnormal releases noted. This review represented one sample.

The ODCM was reviewed for any significant changes. Radioactive waste system

modifications including licensee technical reviews were evaluated to determine if those

17 Enclosure

changes would alter dose consequences to the public, and if there would be any

potential impact on radiation monitor set-point calculation methodology. System

modifications were reviewed to determine if they would impact the effluent monitoring or

release controls and if the changes would affect the licensees ability to maintain

effluents ALARA. The inspectors also reviewed the licensees offsite dose calculations

and discussed the process with a cognizant licensee representative. This review

represented one sample.

The inspectors reviewed a selection of monthly, quarterly, and annual dose calculations

to ensure that the licensee properly calculated the offsite dose from radiological effluent

releases and to determine if any annual RETS/ODCM (i.e., Appendix I to

10 CFR Part 50) values were exceeded. This review represented one sample.

The inspectors reviewed air cleaning system surveillance test results to determine if the

system was operating within the licensees acceptance criteria. The inspectors

reviewed surveillance test results for the vent flow rates and determined if the flow rates

were consistent with UFSAR values. This review represented one sample.

The inspectors reviewed records of instrument calibrations performed since the

last inspection for each point of discharge effluent radiation monitor and flow

measurement device. The current effluent radiation monitor alarm set point values were

reviewed for agreement with RETS/ODCM requirements. The inspectors also reviewed

calibration records of radiation measurement (i.e., counting room) instrumentation

associated with effluent monitoring and release activities. Quality control data

for the radiation measurement instruments were evaluated to determine if the

instrumentation was operating under statistical control and that any problems

observed were addressed in a timely manner. This review represented one sample.

The inspectors reviewed the results of the interlaboratory comparison program to

determine the adequacy of the quality of radioactive effluent sample analyses performed

by the licensee. The inspectors reviewed the licensees quality control evaluation of the

interlaboratory comparison test results. In addition, the inspectors reviewed the results

from the licensees quality assurance audits to determine whether the licensee met the

requirements of the RETS/ODCM. This review represented one sample.

b. Findings

No findings of significance were identified.

.3 Identification and Resolution of Problems

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, and special reports

related to the radioactive effluent treatment and monitoring program since the last

inspection to determine if identified problems were entered into the corrective action

program for resolution. The inspectors also determined whether the licensee's

self-assessment program identified and addressed repetitive deficiencies or significant

individual deficiencies that were identified in problem identification and resolution.

18 Enclosure

The inspectors also reviewed corrective action reports from the radioactive effluent

treatment and monitoring program, interviewed staff and reviewed documents to

determine if the following activities were being conducted in an effective and timely

manner commensurate with their importance to safety and risk:

  • Initial problem identification, characterization, and tracking;
  • Disposition of operability/reportability issues;
  • Evaluation of safety significance/risk and priority for resolution;
  • Identification of repetitive problems;
  • Identification of contributing causes;
  • Identification and implementation of effective corrective actions;
  • Resolution of non-cited violations tracked in the corrective action system; and
  • Implementation/consideration of risk significant operational experience feedback.

This review represented one sample.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES (OA)

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify that condition

reports were being generated and entered into the corrective action program with the

appropriate significance characterization. For select condition reports, the inspectors

also verified that identified corrective actions were appropriate and had been

implemented or were scheduled to be implemented in a timely manner commensurate

with the significance of the identified problem.

b. Findings

No findings of significance were identified.

.2 Semi-annual Trend Review

The inspectors performed a semi-annual trend review to determine that a more

significant safety issue did not exist than would be apparent in a single condition report.

The inspectors reviewed the Operations Department trend reviews and Palisades

Management Review Meeting book for October 2005. The inspectors also reviewed

condition reports to identify potential trends.

19 Enclosure

b. Findings

No findings of significance were identified.

4OA3 Event Follow-up

.1 (Closed) LER 05000-255/2005-002-01: Emergency Diesel Generator 1-2 Excessively

Loaded in Certain Postulated Post-Accident Scenarios - Condition Prohibited by TSs

and a condition that could have prevented the fulfillment of the safety function needed to

mitigate the consequences of an accident.

On February 15, 2005, the licensee identified that under certain postulated scenarios

the emergency diesel generator (EDG) 1-2 could be overloaded when the pressurizer

heaters re-energized after initially being load shed on a blackout signal. This overload,

the licensee determined, could result in an EDG 1-2 trip. The licensee determined the

cause of this event was a circuit modification which was implemented in 1986 which

removed the original plant design that blocked the heater restoration with a safety

injection signal present. Corrective actions included modifications to the circuitry to

preclude breaker closure on the pressurizer heaters with a safety injection signal

present. This finding is more than minor because it had a credible impact on safety, in

that the EDG could be tripped on overload, cause a loss of a safety related bus, and

require manual operator action to restart the EDG and manually shed the required load

during a safety injection with a loss of offsite power. The finding affects the Mitigating

System Cornerstone and was considered to have very low safety significance (Green)

using Appendix A of the IMC 0609 because the probability of events occurring which

require a safety injection with a loss of offsite power and a loss of the other EDG are

very low. This was verified using the phase 2 worksheets using the site specific risk

notebook and reviewed by a regional senior reactor risk analyst. The inspectors

validated that the higher initiating frequency events, such as a loss of offsite power

alone, would not cause the EDG 1-2 to overload. This licensee-identified finding was a

violation of TS 3.8.1 since the 1-2 EDG inoperability existed for greater than the allowed

action time and so is a condition prohibited by TSs. The enforcement aspects of the

violation are discussed in Section 4OA7. This LER is closed.

.2 (Closed) LER 50-255/2005-05-005: Reactor Protection System Actuation and Auxiliary

Feedwater Actuation

On September 1, 2005 the licensee manually tripped the reactor due to a hydrogen leak

on the main generator. Following the reactor trip, the auxiliary feedwater system

actuated to maintain steam generator level. The licensee stabilized the plant in mode

three and successfully repaired the hydrogen leak. The inspectors reviewed the LER

and no findings of significance were identified. No violation of NRC requirements

occurred. The LER is closed.

20 Enclosure

4OA5 Other (71114.04)

.1 Temporary Instruction 2515/161 - Transportation of Reactor Control Rod Drives in

Type A Packages

a. Inspection Scope

The inspectors conducted interviews with cognizant licensee personnel who conducted

record reviews to verify that: (1) the licensee had undergone refueling activities since

calender year 2002; and (2) did not ship irradiated control rod drive mechanisms in

Department of Transportation Specification 7A, Type A packages during the time frame

2002 to the present.

b. Findings

No findings of significance were identified.

.2 Emergency Action Level and Emergency Plan Changes (URI 05000255/2003008-03)

The inspectors discussed with the licensee staff the January 22, 2004, Integrated

Inspection Report which identified an unresolved item regarding previous changes to the

emergency plan which potentially resulted in the use of a non-standard emergency

action level classification scheme. The inspectors advised the licensee that this issue

will continue to be evaluated in 2006.

These activities did not constitute an inspection sample.

.3 Operation of an Independent Spent Fuel Storage Installation (ISFSI) (60855.1)

a. Inspection Scope

Loading Campaign

The inspectors reviewed the loading procedures and observed activities associated with

the loading and transfer of two NUHOMS 32 PT casks. During the lift of the first loaded

canister and transfer cask out of the Spent Fuel Pool (SFP), the mechanical brake on

the fuel building crane engaged, resulting in the cask being suspended in the SFP pit

with the top of the cask approximately 5 feet above the water surface. The inspectors

observed and evaluated the licenses response during the event. The inspectors also

reviewed the cranes annual inspection records, work orders associated with trouble

shooting activities, and the Root Cause Analysis Report associated with this event. The

inspectors evaluated the adequacy of the short and long-term corrective actions that the

licensee proposed and initiated to prevent future occurrences of similar issues.

The inspectors reviewed radiological surveys to confirm that the cask radiation and

contamination levels did not exceed requirements specified in the license. The

inspectors reviewed a number of condition reports that related to the dry fuel storage

project. The inspectors also evaluated a completed documentation package for

Horizontal Storage Module 9. Specifically, the inspectors reviewed the welding records,

21 Enclosure

the vacuum drying and helium leak testing records, as well as the visual and dye

penetrant records.

10 CFR 72.212 Evaluation and 10 CFR 72.48 Screenings

The inspectors reviewed the licensees Title 10 Code of Federal Regulations (CFR)

72.212 evaluation to verify that it addressed the NRC issuance of two new exemptions

that related to the licensees fuel selection process and 10 CFR 50.68(b) requirements.

The inspectors also reviewed a number of 10 CFR 72.48 screening documents to verify

that changes made to the dry fuel storage process or the cask components did not

adversely impact the design of the cask.

Fuel Selection

The inspectors reviewed the licensees fuel selection process to verify that the licensee

incorporated all of the physical, thermal, and radiological fuel acceptance parameters

specified in the NRC-granted exemptions into the fuel selection process. The inspectors

reviewed the fuel selection procedure, qualification records for each assembly to be

loaded in the first Dry Shielded Canister and the Loading Plan. The inspectors also

reviewed the loading procedure and the complete Fuel Move Sheets for the same

canister.

Training

The inspectors reviewed the licensees training program for the training of new welders.

The inspectors reviewed qualification records for the new welders, including on-the-job

evaluations and the final written examination records. The inspectors observed the new

welders weld the first cask. The inspectors also verified that other personnel obtained

the necessary training. The inspectors evaluated the licensees approach to train

personnel to unload a cask during an emergency.

b. Findings

No findings of significance were identified.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. P. Harden and other members of

licensee management on January 5, 2006. Licensee personnel acknowledged the

findings presented. The inspectors asked licensee personnel whether any materials

examined during the inspection should be considered proprietary. No proprietary

information was identified.

22 Enclosure

.2 Interim Exit Meetings

Interim exit meetings were conducted for:

  • The access control to radiologically significant areas program, the ALARA

planning and controls program, and the radioactive gaseous and liquid effluent

treatment and monitoring systems program under the occupational and public

radiation safety cornerstones with Mr. P. Harden on November 4, 2005.

  • Biennial Heat Sink Performance with Mr. D. Mims, Palisades Site Director and

Mr. G. Hettel, Plant General Manager, on December 2, 2005.

  • Independent Spent Fuel Storage Installation with Mr. G. Hettel, Plant General

Manager and others on December 2, 2005.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the

licensee and are violations of NRC requirements which meet the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

  • The licensee identified a design error which resulted in overloading an EDG

during certain accidents. This resulted in EDG inoperability for longer than the

7 days permitted by TS 3.8.1 Action B. This was identified in the licensees

CAP 01001432 and LER 05000-255/2005-002-01. This finding was of very low

safety significance because the accident scenarios were sufficiently infrequent

that the inoperability had a very low impact on plant risk

ATTACHMENT: SUPPLEMENTAL INFORMATION

23 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

P. Harden, Site Vice President

T. Blake, Nuclear Safety Assurance Manager

B. Brogan, Probabilistic Safety Analysis Engineer

N. Brott, Senior EP Coordinator

M. Carlson, Engineering Director

B. Dotson, Regulatory Compliance

C. Fritts, Programs and Analysis Supervisor

J. Hager, Heat Exchanger Program Engineer

R. Harvill, Program and Analysis Engineer

G. Hettel, Plant Manager

L. Lahti, Licensing Manager

D. Malone, Regulatory Affairs

C. Moeller, Radiation Protection Supervisor

B. Patrick, Radiation Protection Manager

C. Plachta, Radiation Protection Supervisor

B. Rice, Dry Fuel Storage Project Manager

R. Schmidt, HPSI System Engineer

J. Schwan, former HPSI System Engineer

K. Smith, Operations Manager

M. Sullivan, Chemistry Supervisor

M. Sweet, EP Coordinator

R. Tiffany, Site Maintenance Rule Coordinator

J. Voskuil, Engineer

K. Yeager, Assistant Operations Manager

Nuclear Regulatory Commission

M. Padovan, Project Manager, NRR

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000255/2005012-01 NCV Spent Fuel Pool Crane Manipulated Outside bounds of

Approved Procedures (Section 1R14)05000255/2005012-02 NCV Failure to Declare VHX-4 Cooler Inoperable with a

Through-wall Piping Leak (Section 1R15)

Closed

05000255/2005012-01 NCV Spent Fuel Pool Crane Manipulated Outside bounds of

Approved Procedures (Section 1R14)

1 Attachment

05000255/2005012-02 NCV Failure to Declare VHX-4 Cooler Inoperable with a

Through-wall Piping Leak (Section 1R15)

05000255/2005-002-01 LER Emergency Diesel Generator 1-2 Excessively Loaded in

Certain Postulated Post-Accident Scenarios

05000255/2005-005-00 LER Manual Reactor Trip Due to Hydrogen Leak on the Main

Generator

Discussed

05000255/2003008-03 URI Emergency Action Level and Emergency Plan Changes

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a documents on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

SOP-23 Attachment 8 CL CWCL; Cold Weather Checklist; November 29, 2005;

Revision 21

WO 00030748 01; Perform Cold Weather Checklist; October 25, 2005

AR01005931; NRC Questions Screen House Ventilation Configuration, Revision 0

CE007604; Evaluate whether MV-ES3243, SIRW TK LT ISOL, Cold Weather Protection

is Adequate; October 29, 2003

CAP03800; Intake Structure Ventilation Operation Contrary to UFSAR Described

Operation; October 8, 2003

1R04 Equipment Alignment

Palisades Nuclear Administrative Procedure 4.02; Control of Equipment; Revision 29

Risk Report for Risk Measures for In Service Items if Taken OOS; Generated

October 24, 2005

DWG M 208 1A; Piping and Instrument Diagram - Service Water System; Revision 53

DBD 1.02; Design Basis Document for Service Water System; Revision 7

DBD-2.03; Containment Spray System; Revision 7

SOP-4; Containment Spray System; Revision 22

DWG 204; Safety Injection Containment Spray and Shutdown Cooling System;

Revision 31

1R05 Fire Protection

Palisades Nuclear Plant Fire Hazards Analysis; Revision 5

USNRC SER for GL 86-10; Fire Protection; September 1, 1978

EA-APR-95-032; Evaluation Of Fire Detection and Suppression System Installed in 1-C

Switchgear Room to Satisfy Appendix R Requirements; October 7, 1995

Palisades Fire Drill Critique and Drill Guide for 18 December Fire Drill; Revision Original

IR07 Heat Sink Performance

Work Order 24011171; Rebuild P67A LPSI Pump, Replace Bearings, Mechanical Seal

and Heat Exchanger with New Design per EAR-99-238 & CPAL-99-2533; January 18,

2001

SAR00806809; Pre-NRC Biennial Ultimate Heat Sink Snapshot Self-Assessment;

November 10, 2005

Procedure No T-223: Component Cooling Water Flow Verification; October 31, 2003,

Revision 13

Letter from V. C. Hall to D. J. Olver; HPSI & LPSI Pump Cooling Spec Comments;

July 20, 1967

Letter from G. J. Parks to J. D. Alderdink; (D255/1993 and 7873/0394); October 28,

1986

3 Attachment

Letter from Durametallic to Palisades; T. E. Cook to G. Szczypka; Cooling requirements

for HPSI pumps; October 28, 1986

Letter from Durametallic to Palisades; Cooling requirements for CS pumps; T. E. Cook

to T. Peterson; September 23, 1986

PPAC SWS026A-4B; Diver Inspection of Traveling Screens & Associated Equipment;

February 14, 2005

WO 24422270-9; Diver Pumped Sand & Mussels from between Trash Racks &

Traveling Screens; February 17, 2005

PPAC SWS175A; Diver Inspection/Cleaning of Intake Bay; completed June 14, 2004

PPAC CWS086C; Diver Inspection/Cleaning of Intake Bay; completed January 12, 2005

PPAC SWS175; Diver Inspection/Cleaning of Intake Bay; completed June 21, 2005

Chemistry Operating Procedure COP-16A; CCW System Chemistry; Revision 13,

March 2, 2005

Chemistry Operating Procedure COP-3; ESS System Chemistry; Revision 25,

May 3, 2005

Procedure No. QO-16, Inservice Test Procedure - Containment Spray Pumps -

Section 5.5 performed on December 21, 2004; Revision 23

EM-09-16; Heat Exchanger Condition Assessment Program; Revision 4

Plant Industry Experience Traveler for 1993 Op Ex, RHR operation results in CCW

water hammer; April 24, 1995

NOS Observation Report 2004-004-8-024; Generic Letter 89-13 Program;

December 15, 2004

M0001GA 8001; HPSI Pump Vendor Manual; Current Compilation ONP-12, Acts of

Nature; Revision 19

OPR 110 (associated with CAP 49234); CCW temperature to ESS pumps may exceed

design after some LOCA scenarios; August 23, 2005

NMC RFQ 20315; Request for bids on CCW to ESS pumps flow requirements;

September 30, 2005

CAP006870; P-67A minor bearing fault indication found during RO-98; November 18,

1999

CAP032055; HPSI Pump P-66A Seal Cooling Heat Exchanger Missing Bolt;

November 8, 2002

CAP032245; CPAL-97-1363 didnt rigorously evaluate increased CCW Temp on ESS

pump seals during one potential scenario; November 26, 2002

CAP034799; CCW Flow to P-66A and P-67B found low during T-223; April 1, 2003

CAP049234; Post-LOCA Analyzed CCW Temperature to ESS pumps Exceeds Design

Value during two scenarios; August 16, 2005

A/R No. 01006110, A/R Type- CAP; NRC Identified Incorrect Model Number Used in

Request for Quote; originated December 2, 2005

A/R No. 01006556, A/R Type- CAP; NRC Identified FSAR HPSI cooling statement

should be addressed in CCW Rerate; originated December 6, 2005

1R11 Licensed Operator Requalification

License Operator requalification, simulator evaluation Cycle 05E, November 21, 2005

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

Risk assessment for Work Week 2540;10/2-10/8/2005 (yellow) for In service testing of

P66A (HHSI pump)

4 Attachment

Risk assessment for Work Week 2542; 10/15-10/21/2005 (yellow) for In service testing

of P66B (HHSI pump) and P-55B (charging pump) repack

Risk assessment for Work Week 2543; 10/22-10/28/2005 (yellow) for EDG 1-2 planned

90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> outage (yellow)

Risk assessment for Work Week 2547; 11/13-11/19/2005 (yellow) for In service testing

of containment spray pump P54B and P54C

Risk assessment for Work Week 2543; 11/20-10/26/2005 (yellow) for EDG 1-2

unplanned outage (yellow)

1R14 Operator Performance During Nonroutine Evolutions and Events

Palisades Challenge Board summary document; Final Actions Prior to Power

Escalation, Turbine Vibration Forced Outage; October 18, 2005

WO 00028215 01; L-3: Contingency- Dry Fuel Storage 200; October 11, 2005

RCE0100065901; Root Cause Analysis Report CAP01000659

WO 00028215 53 L-3: Contingency- Dry Fuel Storage 200; October 12, 2005

1R15 Operability Evaluations

FP-OP-OL-1; Corporate Office Quality Procedures: Operability Determination;

Revision 1

CAP 01000525; Containment Sump Fill rate increased During QO-1; November 9, 2005

OPR 01000525-01; VHX-4 Leaking Service Water to Containment Sump; October 12,

2005

OPR - CAP033264; CCW Design Temperature of 140 degrees; February 5, 2003

CAP049616; Degradation of Palisades Intake Crib; September 9, 2005

OPR000096; Palisades Intake Crib; April 19, 2005

1R16 Operator Workaround

A010 01007214; Feed Reg Valve Position Indication Not Screened as an OWA;

December 21, 2005

Procedure No 4.12; Operator Workaround Program; Revision 2

Operator Burden List; December 21, 2005

EOP-1.0; Standard Post-Trip Actions; Revision 12

1R19 Post Maintenance Testing

WO 00028548 01; Auxiliary Feedwater Actuation System; November 3, 2005

QI- 39; Auxiliary Feedwater Actuation System Logic Test; October 6, 2005

WO 00029819 01; VHX-4 Containment Air Cooler Leak Repairs; October 13, 2005

Engineering Assistance Request (EAR -2001-0367); Permanent Plugs for Containment

Air Cooler VHX-4; June 19, 2001

QO-1; Safety Injection; Revision 49; December 15, 2005

WO 00110216 01; D/G 1-1 Load Sequencer; December 14, 2005

1R22 Surveillance Testing

QO-19; Inservice Test Procedure - HPSI Pumps and ESS Check Valve Operability Test;

Revision 24, performed October 20, 2005

EA-ELEC08-0001; Engineering Analysis - Uncertainty Calculation for the Secondary

Calorimetric Heat Balance; Revision 2

DWO-1; TS Surveillance Procedure: Operator Daily/Weekly Items Modes 1,2,3 and 4;

Revision 71

5 Attachment

EA-HAR-91-10; Engineering Analysis - Heat Balance Adjustment for Moisture Content

of Steam; Revision 0

EA-BWB-96-01; Engineering Analysis - Heat Balance Calculation Using the Ultrasonic

Flowmeter Measurement Device; Revision 5

Inspection Procedure 61706; NRC Inspection Manual Core Thermal Power Evaluation;

July 14, 1986

1EP4 Emergency Action Level and Emergency Plan Changes

Palisades Nuclear Plant Site Emergency Plan; Revisions 11 and 12

2OS1 Access Control to Radiologically Significant Areas; and

2OS2 ALARA Planning And Controls

RCA Entries 100 Millirem or Greater; November 1, 2004 - November 1, 2005

Performance Indicator Data for Occupational and Public Radiation Safety; August 8,

2005

CAP049175; HRA Identified During Routine Monthly Survey; August 10, 2005

CAP049040; Worker Contaminated on Right Shoe; August 3, 2005

CAP049176; Contamination Found on Floor in 602' Miscellaneous Waste Tank Room;

August 10, 2005

CAP049351; HEPA Vacuum Inappropriately Stored; August 24, 2005

CAP049809; Neutron Dose Measurement; September 21, 2005

RWP 536; Containment Entries by Operations with Reactor Critical; October 21, 2005

RWP 537; Containment Entries by Maintenance Dept. with Reactor Critical; October 27,

2005

RWP 539; Dry Fuel Storage - Cask HSM007; Revision 2

FHS-M-39B; Fuel Loading and DSC Sealing Operations for NUHOMS 32PT Dry Fuel

Loading Operations; Revision 10

CE012085; RV-2203 Gas Header to VCT Relief Apparently Leaking By; November 30,

2004

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

2004 Annual Radioactive Effluent Release Report; March 29, 2005

Radiochemistry Cross Check Data for the 2nd, 3rd, and 4th Quarters of 2004

Operability of Main Steam Line Gross Gamma Activity Monitor; January 10, 2005

RT-85C; Fuel Handling Area Ventilation Filter Testing; Revision 7

NUCON; I-131 Removal Efficiency Determination of Adsorbent Samples; September 14,

2004

SA011366; Snapshot Report: Self-Assessment RETS; August 1, 2005

2005-003-8-022; Nuclear Oversight Observation Report; October 10, 2005

RR-9B; Radwaste Discharge Monitor Calibration; January 29, 2005

RR-9I; Waste Gas Discharge Monitor RIA-1113 Calibration; February 12, 2005

RR-84A; Iodine/Particulate Effluent Monitor RIA-2325 Calibration; August 27, 2005

RR-84B; Noble Gas Effluent Monitor RIA-2326 Calibration; October 11, 2005

RR-84C; Noble Gas Effluent Monitor RIA-2327 Calibration; June 22, 2005

DWR-10; Stack Effluent Sampling Calculations and Records, Revision 24

Gamma Spectroscopy Report; Stack Gas Iodine; November 2, 2005

CA026442; Radiation Monitoring System-Action Plan Development; January 17, 2005

ACE003633; RIA-1113 (Waste Gas Monitor) Switch Failure; September 6, 2005

6 Attachment

CAP048116; Rad Effluent Releases from the VCT Due to Leakage of RV-2203 and

CK-CVC2073; June 1, 2005

CAP048646; Record Keeping Enhancement for RETS/REMP Sampling; July 7, 2005

CAP049734; Release Rate Verification for T-91 Utility Water Tank Not Documented

Correctly; September 16, 2005

CAP049719; Offsite Dose Calculation Not Completed Within Required Time Frame;

September 15, 2005

CAP049880; RIA2327 High Range Noble Gas Stack Monitor Rad Level Spike;

September 26, 2005

Effluent Data 4th Quarter 2005; November 3, 2005

CH 4.39; Lower Limit of Detection Data, Detectors 1, 2 and 3; Revision 13

Gamma Spectroscopy Calibration Data, Detectors 1, 2 and 3

4OA2 Problem Identification and Resolution

Palisades Management Review Meeting; October 2005

Operations Department Monthly Performance Report; June and November 2005

4OA3 Event Follow-up

LER 05000-255/2005-05-005; Reactor Protection System Actuation and Auxiliary

Feedwater Actuation; October 24, 2005

LER 05000-255/2005-002-01; Emergency Diesel Generator 1-2 Excessively Loaded in

Certain Postulated Post-Accident Scenarios; September 27, 2005

4OA5 Other Activities

Loading Campaign

Condition Reports, generated between August 2005 and December 2005 for Dry Fuel

Storage Project

Procedure, FHS-M-39B; "Fuel Loading and DSC Sealing Operations for NUHOMS 32PT

Dry Fuel Loading Operations," Revision 12

Procedure, FHS-M-39C; "Dry Fuel Loading Operations Loaded NUHOMS DSC/Transfer

Cask Transfer to ISFSI"

Procedure, FHS-M-40B; "NUHOMS 32PT Unloading," Revision 1

Root Cause Analysis Report, No. CAP 01000659; "Crane operator heard loud noise

during lift with L-3 crane"

Work Order, No. 24422117; "L-3, annual inspection (NDE), Perform yearly inspection of

crane, using procedure MSM-13"

Work Order, No. 2821501; "L-3: Contingency-Dry Fuel Storage 200," October 11, 2005

Work Order, No. 2821553; "L-3: Contingency-Dry Fuel Storage 200," October 12, 2005

Work Order, No. 3087201; "Contingency-Dry Fuel Storage 200," December 1, 2005

Work Order Package, No. 2424201; "HSM-009; 2005 DFS Loading: Load DSC,"

November 23, 2005

10 CFR 72.212 Evaluation and 72.48 Screening

72.48 Screen, No. 05-0772; "Fuel Loading and DSC Sealing Operations for NUHOMS

32PT Dry Fuel Loading Operations"

72.48 Screen, No. 05-0793; "Fuel Loading and DSC Sealing Operations for NUHOMS

32PT Dry Fuel Loading Operations"

72.48 Screen, No. 05-0783; "10 CFR 72.212 and Certificate of Compliance Evaluation

Report for NUHOMS-32PT System"

7 Attachment

72.48 Screen, No. 05-0791; "Dry Fuel Loading Operations-Loaded NUHOMS

DSC/Transfer to ISFSI" 72.48 Screen, No. 05-0802; "Fuel Loading and DSC Sealing

Operations for NUHOMS 32PT Dry Fuel Loading Operations"

Report No. PNP 721004; "Palisades 10CFR 72.212 and Certificate, Compliance

Evaluation Report for NUHOMS 32PT System," Revision 2, October 7, 2005

Fuel Selection

DSC Loading Plan, DCS Serial Number PNP-32PT-K10-S125, Procedure

No. EM-04-56, Attachment 2, Revision 1

Fuel Assembly Qualifications, Procedure No. EM-04-56, Attachment 1, Revision 1

Procedure, No. EM-04-56; "Fuel Selection for Dry Fuel Storage," Revision 1

Procedure No. FHSO-17A; "MSB/DSC Loading Procedure," Fuel Move Sheets,

Attachment 1, Revision 3

Training

Training Records; "2005 Dry Fuel Storage Load Campaign"

8 Attachment

LIST OF ACRONYMS USED

ADAMS Agency-Wide Document and Management System

ALARA As Low As Is Reasonably Achievable

AR Action Request

CAP Corrective Action Program

CCW Component Cooling Water

CFR Code of Federal Regulations

CR Condition Report

CS Containment Spray

DC Direct Current

EDG emergency diesel generator

EOP Emergency Operating Procedures

ESS Engineered Safety System

HPSI High Pressure Safety Injection

HRA High Radiation Area

IMC Inspection Manual Chapter

ISFSI Independent Spent Fuel Storage Installation

LPSI Low Press Safety Injection

NCV Non-Cited Violation

NMC Nuclear Management Company

ODCM Offsite Dose Calculation Manual

PARS Publicly Available Records

PI Performance Indicator

PRA Probabilistic Risk Assessment

PSA Probabilistic Safety Assessment

REMP Radiological Environmental Monitoring Program

RETS Radiological Environmental Technical Specifications

RP Radiation Protection

RWP Radiation Work Permit

SDP Significance Determination Process

SFP Spent Fuel Pool

SSC Structures, Systems, and Components

SW Service Water

TI Temporary Instruction

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

VHRA Very High Radiation Area

9 Attachment