ML051300633

From kanterella
Jump to navigation Jump to search
IR 05000373-05-002, 05000374-05-002, on 01/01/2005 - 03/31/2005, LaSalle County Station, Units 1 & 2. Fire Protection, Maintenance Risk Assessments and Emergent Work Control, Post-Maintenance Testing, Access Control to Radiologically Signif
ML051300633
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 05/10/2005
From: Burgess B
NRC/RGN-III/DRP/RPB2
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-05-002
Download: ML051300633 (85)


See also: IR 05000374/2005002

Text

May 10, 2005

Mr. Christopher M. Crane

President and Chief Nuclear Officer

Exelon Nuclear

Exelon Generation Company, LLC

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: LASALLE COUNTY STATION, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000373/2005002;

05000374/2005002

Dear Mr. Crane:

On March 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your LaSalle County Station, Units 1 and 2. The enclosed report documents the

results of this inspection discussed on April 5, 2005, with the Site Vice President, Ms. Susan

Landahl, and other members of your staff.

The inspection examined activities conducted under your license as they related to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, four NRC-identified and three self-revealed findings of

very low safety significance were identified. All of these findings also involved violations of NRC

requirements. However, because the findings associated with these violations were of very low

safety significance and because the issues were entered into the licensees corrective action

program, the NRC is treating these issues as Non-Cited Violations in accordance with

Section VI.A.1 of the NRCs Enforcement Policy. Additionally, two licensee identified violations

are listed in Section 4OA7 of this report.

If you contest the subject or severity of any Non-Cited Violation in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission, Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352;

the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the NRC Resident Inspectors Office at the LaSalle County Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter

and its enclosures will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRC's

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Bruce L. Burgess, Chief

Branch 2

Division of Reactor Projects

Docket Nos.: 50-373; 50-374

License Nos.: NPF-11; NPF-18

Enclosure: Inspection Report 05000373/2005002; 05000374/2005002

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - LaSalle County Station

LaSalle County Station Plant Manager

Regulatory Assurance Manager - LaSalle County Station

Chief Operating Officer

Senior Vice President - Nuclear Services

Senior Vice President - Mid-West Regional

Operating Group

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing - Mid-West Regional

Operating Group

Manager Licensing - Clinton and LaSalle

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

Assistant Attorney General

Illinois Department of Nuclear Safety

State Liaison Officer

Chairman, Illinois Commerce Commission

DOCUMENT NAME: E:\Filenet\ML051300633.wpd

To receive a copy of this document, indicate in the box:"C" = Copy without enclosure "E"= Copy with enclosure"N"= No copy

OFFICE RIII N RIII RIII RIII

NAME BBurgess/sls

DATE 05/10/05 05/ /05 05/ /05 05/ /05

OFFICIAL RECORD COPY

ADAMS Distribution:

GYS

DMS6

RidsNrrDipmIipb

GEG

KGO

DEK

CAA1

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

JRK1

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-373; 50-374

License Nos: NPF-11; NPF-18

Report No: 05000373/2005002; 05000374/2005002

Licensee: Exelon Generation Company, LLC

Facility: LaSalle County Station, Units 1 and 2

Location: 2601 N. 21st Road

Marseilles, IL 61341

Dates: January 1 through March 31, 2005

Inspectors: D. Kimble, Senior Resident Inspector

D. Eskins, Resident Inspector

A. Klett, Engineering Inspector

D. Melendez-Colon, Reactor Engineer

M. Mitchell, Radiation Protection Specialist

J. Neurauter, Engineering Inspector

T. Ploski, Senior Emergency Preparedness Inspector

R. Walton, Operator Licensing Examiner

J. Yesinowski, Illinois Dept. of Emergency Management

Approved by: Bruce L. Burgess, Chief

Branch 2

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

Summary of Plant Status . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1. REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R01 Adverse Weather Protection (71111.01) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04 Equipment Alignment (71111.04) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

1R05 Fire Protection (71111.05) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R08 Inservice Inspection (ISI) Activities (71111.08) . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R11 Licensed Operator Requalification Program (71111.11) . . . . . . . . . . . . . . . . . . 8

1R12 Maintenance Effectiveness (71111.12) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13) . . 9

1R14 Operator Performance During Non-Routine Plant Evolutions and Events

(71111.14) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R15 Operability Evaluations (71111.15) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

1R16 Operator Workarounds (71111.16) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R17 Permanent Plant Modifications (71111.17) . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R19 Post Maintenance Testing (71111.19) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R20 Outage Activities (71111.20) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

1R22 Surveillance Testing (71111.22) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

1R23 Temporary Plant Modifications (71111.23) . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

1EP2 Alert and Notification System (ANS) Testing (71114.02) . . . . . . . . . . . . . . . . . 24

1EP3 Emergency Response Organization (ERO) Augmentation Testing (71114.03) 24

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

(71114.05) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

2. RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

2OS1 Access Control to Radiologically Significant Areas (71121.01) . . . . . . . . . . . . 25

2OS2 As Low As Is Reasonably Achievable Planning And Controls (ALARA)

(71121.02) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

4. OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

4OA1 Performance Indicator Verification (71151) . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

4OA2 Identification and Resolution of Problems (71152) . . . . . . . . . . . . . . . . . . . . . 35

4OA3 Event Followup (71153) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 43

4OA4 Cross-Cutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 46

4OA5 Other . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 47

4OA6 Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 48

4OA7 Licensee Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 49

ATTACHMENT: Supplemental Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

Enclosure

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

LIST OF ACRONYMS USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

Enclosure

SUMMARY OF FINDINGS

IR 05000373/2005002, 05000374/2005002; 01/01/2005 - 03/31/2005; LaSalle County Station,

Units 1 & 2; Fire Protection, Maintenance Risk Assessments and Emergent Work Control,

Post-Maintenance Testing, Access Control to Radiologically Significant Areas, and Identification

and Resolution of Problems Report.

The inspection was conducted by both resident and regional inspectors. The report covers a

3-month period of baseline resident inspection, and announced baseline inspections in

emergency preparedness, radiation protection, and of the inservice inspection program. Seven

Green findings and seven associated non-cited violations (NCVs) were identified. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using NRC

Inspection Manual Chapter (IMC) 0609 Significance Determination Process (SDP). Findings

for which the SDP does not apply may be "Green," or be assigned a severity level after NRC

management review. The NRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3,

dated July 2000.

A. Inspector-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. A finding of very low safety significance was self-revealed when sparks

from hot work associated with the cutting of a 20-inch pipe in the 2B residual

heat removal (RHR) corner room on February 16, 2005, ignited a small pile of

absorbent cleaning material in the room. An associated NCV was also identified

against Technical Specification 5.4.1(c) for failure to follow the existing plant fire

protection procedure related to hot work and ignition control.

The performance deficiency, identified during review of the event, involved two

examples where licensee personnel failed to properly implement the established

plant procedure governing hot work and ignition control. The finding was of

more than minor significance in that it had a direct impact on the cornerstone

objective. Specifically, the licensees performance deficiencies were directly

responsible for an actual Class A fire in the 2B RHR corner room on

February 16, 2005. Because the finding involved Unit 2 in a cold shutdown

condition, the inspectors determined it to be of very low safety significance

(Green) and within the licensees response band. Corrective actions completed

by the licensee include: focused coaching sessions with superintendents and

general foremen of hot work personnel; meetings between the stations Fire

Marshal and contractor supervision to discuss hot work issues; and focused

coaching sessions with fire watch personnel by contractor management

conveying the message that the fire watch is ultimately responsible for the work

location being and remaining in compliance with fire safety standards. The

finding was determined to involve the cross-cutting aspect of human

performance. (Sections 1R05.2 and 4OA4)

1 Enclosure

  • Green. The inspectors identified a finding of very low safety significance and an

associated NCV during review of corrective actions associated with a small fire in

the 2B RHR corner room on February 16, 2005. The inspectors determined that

the licensee had, during several opportunities, failed to take timely and effective

corrective actions with respect to ignition control for hot work. This failure was

determined by the inspectors to be contrary to the requirements of 10 CFR 50,

Appendix B, Criterion XVI, "Corrective Action."

In reviewing corrective actions for 2B RHR corner room fire, the inspectors

identified a performance deficiency regarding inadequate corrective actions

taken to control hot work activities. The inspectors determined that the finding

was of more than minor significance in that it had a direct impact on an objective

for the Initiating Event Cornerstone. The inspectors determined that the finding

impacted minimally on the licensees capability to reach and maintain cold

shutdown conditions. Therefore, this finding had very low safety significance

(Green) and was within the licensee's response band. Additional corrective

actions planned by the licensee include a comprehensive common cause

analysis to determine whether or not generic fire protection programmatic

weaknesses exist. (Section 4OA2.1)

  • Green. The inspectors identified a finding of very low safety significance and an

associated NCV during a review of the licensees assessment and management

of the risk affiliated with maintenance on the 1A circulating water (CW) pump.

The inspectors review revealed that the licensee had failed to recognize and

effectively manage the risk associated with a meter replacement. The meter

was in a circuit that was common to both the 1A CW pump, which was

undergoing planned maintenance, and the 1C CW pump, which was in service.

This failure to effectively assess and manage maintenance risk was determined

by the inspectors to be contrary to the requirements of 10 CFR 50.65(a)(4).

The performance deficiency with this issue was a failure on the part of the

licensee to properly assess and manage the increase in risk from a planned

maintenance evolution. The finding was of more than minor significance in that it

had a direct impact on a Initiating Event Cornerstone objective. Specifically, the

licensees failure to properly assess and manage the increase in risk resulted in

a plant transient that challenged the on-watch Operations crew. The inspectors

determined this finding to be of very low safety significance (Green) because the

finding did not contribute to both the likelihood of a transient and the likelihood

that mitigation equipment or functions would not be available. Corrective actions

completed by the licensee include: training to enhance worker proficiency at

performing maintenance risk assessments on energized equipment, assessment

of the existing production risk evaluation sheet used by work planners to

determine if additional clarifications are required, discussion of this type of task

at weekly work management meetings, reinforcement of Operations role in

reviewing work on production risk systems, and evaluation of whether or not

additional actions are required during clearance order preparations to preclude

this type of event. The finding was determined to involve the cross-cutting

aspect of human performance. (Sections 1R13.2 and 4OA4)

2 Enclosure

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a finding of very low safety significance and an

associated NCV during a review of the licensees assessment and management

of the risk affiliated with the cycling of the 1DG032 manual gate valve. The gate

valve was cycled during the performance of a scheduled 0 emergency diesel

generator (EDG) auxiliaries inservice test on December 30, 2004. The

inspectors review revealed that the licensee had failed to recognize and

effectively manage the risk associated with the operation of this valve. This

valve was part of a group of manual gate valves located in essential service

water systems that were known to be highly susceptible to disc/stem separation.

This failure to effectively assess and manage the activitys risk was determined

by the inspectors to be contrary to the requirements of 10 CFR 50.65(a)(4).

The identified performance deficiency with this finding was a failure on the part of

the licensee to have accurately assessed and properly managed the risk

associated with the cycling of the 1DG032 manual gate valve. The finding was

of more than minor significance in that it had a direct impact on an objective of

the Mitigating Systems cornerstone. Specifically, the licensees failure to

properly assess and effectively manage the risk associated with the 1DG032

valve cycling evolution resulted in the interruption of supporting cooling water

flow to Unit 1 Division 1 emergency core cooling system (ECCS) components,

rendering these components inoperable and unavailable. Because the finding

impacted only a single Division of the units ECCS; did not represent the loss of

an entire systems safety function; did not result in a Technical Specification

allowed outage time being exceeded; and the finding was not related to external

events such as fire, flooding, or adverse weather; the inspectors concluded that

the safety significance of this issue was very low (Green). Corrective actions

completed by the licensee include: hanging tags on susceptible valves to warn

personnel of the potential for stem/disc separation; validation of all essential

service water valves susceptible to stem/disc separation and providing a listing

of these components to plant operations; revision of applicable operating

procedures to include a precaution that identifies the valves that are susceptible

to stem/disc separation, and a requirement to verify the applicability of valves

prior to operation. (Section 1R13.3)

  • Green. A finding of very low safety significance was self-revealed when changes

implemented by a modification to the Unit 2 125 volt direct current (Vdc) charger

system were not appropriately incorporated into operational procedures. This

procedural deficiency resulted in an under-voltage condition during an attempt to

swap in-service chargers. An associated NCV against the requirements of

10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

was also identified.

The identified performance deficiency was the failure of the licensee to

incorporate relevant design information concerning the metering circuitry of a

newly installed battery charger into the appropriate operating procedures. The

finding was of more than minor significance in that it had a direct impact on the

3 Enclosure

MS cornerstone objective. Specifically, the procedural deficiency, and lack of

any formal training regarding the metering circuitry, contributed to a low voltage

condition on the Unit 2 Division 1 125 Vdc system. The low voltage resulted in

the Unit 2 Division 1 125 Vdc system being rendered inoperable for about 23

minutes. Because the finding involved the loss of only one train of safety related

equipment and the loss was for less than the Technical Specification allowed

outage time, the inspectors determined it to be of very low safety significance

(Green) and within the licensees response band. Corrective actions planned

and completed by the licensee include: revision of applicable operating

procedures; training for operations personnel on new charger procedures; and

planned training to enhance operator knowledge regarding the metering circuitry

and the differences between various battery chargers. (Section 1R19.2)

  • Green. A finding of very low safety significance was identified by the inspectors.

The licensee had failed during prior opportunities to fully evaluate the nature of

the problem leading to various emergency diesel generator (EDG) reverse power

trips. The most recent of these events were a reverse power trip of the 2B EDG

on August 18, 2004, for which no root cause was ever determined, and a

subsequent reverse power trip of the 2A EDG that occurred on December

7, 2004. An associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B,

Criterion XVI, "Corrective Action," was also identified by the inspectors.

The performance deficiency was determined to be a failure on the part of the

licensees staff to fully evaluate a long standing issue with EDG reverse power

trip. An evaluation in response to an event, as recent as August 18, 2004, failed

to give sufficient priority to identified corrective actions in a manner that would

preclude the latest occurrence, a reverse power trip of the 2A EDG on

December 7, 2004. The finding was of more than minor significance in that it

had a direct impact on the cornerstone objective. Specifically, the inspectors

concluded that the licensee's performance deficiency was responsible for the

reverse power trip of the 2A EDG on December 7, 2004, which caused the EDG

to be unavailable for an additional 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />. Because the finding involved the

loss of only one train of safety related equipment and the loss was for less than

the Technical Specification allowed outage time, the inspectors determined it to

be of very low safety significance (Green) and within the licensee's response

band. Corrective actions planned and completed by the licensee include:

establishment of a less restrictive EDG load limit to allow opening the EDG

output breaker when the load is less than approximately 500 kW; additional

training for licensed operators in the areas of EDG theory and operation and the

effects of reverse power conditions on diesel generators; and revision of

simulator modeling for EDGs to more accurately reflect actual plant performance

for reverse power trips. (Section 4OA2.2)

Cornerstone: Occupational Radiation Safety

  • Green. A finding of very low safety significance was self-revealed when an

electrician improperly entered a high radiation area (HRA) in the radiation

controlled area (RCA) (the Unit 2 drywell) that was posted as a HRA. This

4 Enclosure

occurrence was revealed when he exited the RCA and the electronic dosimeter

check-out was alerted that a dose rate alarm had occurred during the entry,

revealing that the individual had signed on to the wrong radiation work permit

(RWP).

The cause of the error was a failure to assure through self-checking that each

entry to the electronic RWP sign-in is made using the correct RWP. The finding,

under the Occupational Radiation Safety Cornerstone, does not involve the

application of traditional enforcement because it did not result in actual safety

consequences or potential to impact the NRCs regulatory function, and was not

the result of any willful actions. The finding was more than minor as it involves

the failure of the licensee to adhere to procedures to monitor and control

radiation exposure, a key attribute under the objective of the radiation safety

cornerstone to ensure adequate protection of worker health and safety from

exposure to radiation. The finding is of very low safety significance because the

individual was using an electronic dosimeter that alarms to warn workers of

higher than expected dose rates or accumulated dose. The issue constituted a

Non-Cited Violation of Technical Specification 5.7.1, which requires that access

to, and activities in, each HRA with dose rates not exceeding 1.0 rem per hour at

30 centimeters from the radiation source be controlled by means of a RWP that

includes specification of radiation dose rates in the immediate work area and

other appropriate radiation protection equipment and measures. Immediate

corrective actions included locking the individual out of the RCA and initiation of

an investigation. Additionally, all site personnel were notified of this event

through a station safety alert. The primary cause of the finding was related to

the cross-cutting area of human performance. (Sections 2OS1.4 and 4OA4)

B. Licensee-Identified Violations

Violations of very low safety significance that were identified by the licensee have been

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees corrective action program. These violations and corrective

action tracking numbers are listed in Section 4OA7 of this report.

5 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1

The unit began the inspection period operating at full power. On February 5, 2005, power was

reduced to approximately 65 percent to permit a control rod sequence exchange and control

rod surveillance testing. The unit returned to operation at full power on February 6, 2005, and

continued operating at or near full power for the remainder of the inspection period.

Unit 2

The unit began the inspection period operating at full power. On January 8, 2005, power was

reduced to approximately 62 percent for a control rod pattern adjustment. Operation at full

power was resumed on January 10, 2005. On February 7, 2005, the unit shut down for

refueling outage L2R10. Unit 2 Cycle 11 achieved initial criticality following L2R10 on

March 15, 2005, with full power being attained on March 18, 2005. On March 22, 2005, power

was reduced briefly to approximately 65 percent to permit a control rod sequence exchange

and control rod surveillance testing. The unit returned to full power operation later that same

day, and continued operating at or near full power for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather (71111.01)

Review of Site Specific Weather Condition - Tornado Warning

a. Inspection Scope

The inspectors performed an assessment of the licensees preparations for adverse

weather, including conditions that could lead to loss of off-site power and other

conditions that could result from high winds or tornado-generated missiles. The

licensees procedures and preparations during a tornado warning in LaSalle County on

March 30, 2005, were reviewed by the inspectors and were verified to be adequate.

During the inspection, the inspectors focused on plant specific design features and the

licensees procedures used to respond to specified adverse weather conditions.

Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR)

and performance requirements for systems selected for inspection, and verified that

operator actions were appropriate as specified by plant specific procedures.

This review constituted a single inspection sample.

1 Enclosure

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1 Semiannual Complete System Alignment Verification

a. Inspection Scope

Due to the systems risk significance, the inspectors selected the Unit 1 core standby

cooling system (CSCS) for a complete system alignment verification. The inspectors

walked down the system to verify mechanical and electrical equipment lineups,

component labeling, component lubrication, component and equipment cooling, hangers

and supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation.

The inspectors review of CSCS alignment constituted a single inspection sample.

b. Findings

No findings of significance were identified.

.2 Quarterly Partial System Alignment Verifications

a. Inspection Scope

The inspectors performed partial alignment verifications on the following equipment

trains to verify operability and proper equipment lineup. These systems were selected

based upon risk significance, plant configuration, system work or testing, or inoperable

or degraded conditions.

  • Unit 2 fuel pool cooling system while unit fuel pools were cross connected

The inspectors verified the position of critical redundant equipment and looked for any

discrepancies between the existing equipment lineups and the required lineups.

These partial equipment alignment verifications constituted three inspection samples.

b. Findings

No findings of significance were identified.

2 Enclosure

1R05 Fire Protection (71111.05)

.1 Quarterly Fire Protection Zone Inspections

a. Inspection Scope

To identify potential fire protection issues, the inspectors conducted field observations in

the following risk significant areas. These areas were selected because of the systems,

structures, or components designated as important to reactor safety that were located

therein.

  • Fire Zone 4E1, Unit 1 auxiliary equipment room
  • Fire Zone 4E3, Unit 1 Division 2 essential switchgear room
  • Fire Zone 4F1, Unit 1 Division 1 essential switchgear room
  • Fire Zone 4F2, Unit 2 Division 1 electrical switchgear room

room

room

The inspectors reviewed the control of transient combustibles and ignition sources, fire

detection equipment, manual suppression capabilities, passive suppression capabilities,

automatic suppression capabilities, barriers to fire propagation, and any contingency fire

watches that were in effect.

These quarterly fire protection inspections constituted nine inspection samples.

b. Findings

No findings of significance were identified.

.2 2B Residual Heat Removal (RHR) Corner Room Fire

a. Inspection Scope

The inspectors followed up on a small Class A fire that occurred in the 2B RHR corner

room as a result of hot work on February 16, 2005. The inspectors reviewed the control

of transient combustibles and ignition sources, fire detection equipment, manual

suppression capabilities, passive suppression capabilities, automatic suppression

capabilities, barriers to fire propagation, and any contingency fire watches that were in

effect. In addition, the inspectors reviewed the licensees apparent cause evaluation

(ACE) for the event.

This review constituted a single inspection sample.

3 Enclosure

b. Findings

Introduction

A finding of very low safety significance (Green) was self-revealed when sparks from hot

work associated with the cutting of a 20-inch pipe in the 2B RHR corner room ignited a

small pile of absorbent cleaning material in the room. A Non-Cited Violation (NCV) of

Technical Specification 5.4.1(c) for failure to follow the existing plant fire protection

procedure related to hot work and ignition control was also identified.

A second finding and NCV associated with this event are described in Section 4OA2.1

of this report.

Description

On February 16, 2005, at approximately 2:30 p.m., work was in progress in the 2B RHR

corner room to demolish a section of pipe that was slated for removal as part of an

approved permanent plant modification. The work involved cutting a vertical run of

20-inch diameter pipe into sections that were approximately 1 foot in length to facilitate

ease of removal. A single fire watch was assigned to the area where the cutting was

taking place. Fire blanketing was placed in the area of the hot work, with additional

material surrounding the floor piping penetration to prevent sparks from falling through

the penetration. This fire blanket extended outward for approximately 8 feet from the

work. During the course of the work, some of the sparks generated by the pipe cutting

activities were thrown past the fire blanket and fell through open floor grating to the

694' elevation below.

At some point following lunch, cleaning material was staged on the 694' elevation below

the area where the hot work was in progress. When interviewed as part of the

licensees ACE, the fire watch stated that he was not aware of the introduction of this

combustible material to this area. Sparks that fell from the hot work above ignited a

small Class A fire in this material. A laborer in the area detected the fire and attempted

to extinguish it by stepping on the flames. When this was not successful, a mop was

used in an attempt to smother the flames. When this action, too, proved ineffective, the

laborer notified the fire watch on the level above, who extinguished the fire with a dry

chemical fire extinguisher. The control room was notified of the fire by the personnel

involved in the 2B RHR corner room.

Unrelated to the actual fire itself, a problem was encountered with the dry chemical fire

extinguisher used by the fire watch to combat the fire. In addition to being discharged

from the nozzle as expected, dry chemical extinguishing agent was observed to emit

from underneath the cap of the extinguisher. As noted above, despite this malfunction,

the fire watch was able to use the extinguisher to successfully combat the fire. An

investigation by the licensee subsequently determined that the malfunction was the

result of a missing gasket normally installed under the fire extinguisher cap.

4 Enclosure

Analysis

The inspectors determined that there was a licensee performance deficiency associated

with the fire blanket coverage provided for the job. Specifically, the coverage was

inadequate in that it did not fully contain all the sparks being generated from the cutting

activity, and was not in compliance with the licensees established procedure governing

hot work ignition controls. Procedure OP-MW-201-004, Fire Prevention for Hot Work,

Section 4.2, Fire Prevention Precautions, required fire blanket coverage out to 35 feet

from the work location. In this event, the fire blanket coverage went out a mere 8 feet.

This lack of adequate fire blanket coverage was, in part, responsible for the sparks from

the hot work reaching the open floor grating and falling to the 694' elevation below.

In addition, a second performance deficiency associated with the duties of the fire watch

was identified. Procedure OP-MW-201-004, Section 3.4.2, discussed the duties of the

fire watch, and required that each fire watch was responsible for stopping the hot work

in the event of any safety problems, such as sparks coming in contact with combustible

material, etc. At the time of the fire, the hot work in the 2B RHR corner room had been

in progress for three shifts. The fire watches assigned to the job had ample opportunity

to self-identify the spark hazard caused by the hot work and were required by procedure

to do so.

The objective of the Initiating Events Cornerstone of Reactor Safety is to limit the

likelihood of those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. In accordance with NRC Inspection

Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, the inspectors determined that the finding was of more than minor

significance in that it had a direct impact on this cornerstone objective. Specifically, one

of the key attributes associated with this cornerstone objective is protection against fires,

and the inspectors determined that the licensees performance deficiencies were directly

responsible for an actual Class A fire in the 2B RHR corner room.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, and conducted a

Phase 1 characterization and initial screening. Because the finding was associated with

fire protection, this was accomplished using IMC 0609, Appendix F, Attachment 1, Fire

Protection SDP Phase 1 Worksheet. Based on the size and location of the fire, the

inspectors concluded it could only plausibly affect Unit 2, which was in cold shutdown.

As a result, the inspectors determined that the finding only pertained to the ability to

reach and maintain cold shutdown conditions, and was, therefore, of very low safety

significance (Green) and within the licensees response band. Because the finding

involved the cross-cutting aspect of human performance, it is also noted in

Section 4OA4, Cross-Cutting Aspects of Findings, in this report.

Enforcement

Technical Specification 5.4.1(c) requires that written procedures for the stations fire

protection program be established, implemented, and maintained. Contrary to this

requirement, on February 16, 2005, licensee personnel conducting hot work in the 2B

5 Enclosure

RHR corner room failed to implement the following provisions of OP-MW-201-004, Fire

Prevention for Hot Work, as specified:

  • Section 4.2.1.4, Openings or cracks in walls, floors, or ducts within 35 feet of

the site shall be tightly covered to prevent the passage of sparks to adjacent

areas;

  • Section 3.4.2, The Fire Watch is responsible for stopping the hot work in the

event of a safety problem (i.e., sparks coming in contact with combustible

material, faulty equipment, etc.).

The licensee had entered this fire into their corrective action program (CAP) as Issue

Report (IR) 302209. Similarly, the malfunction of the dry chemical fire extinguisher was

entered into the CAP as IR 302447. Corrective actions completed by the licensee

include: focused coaching sessions with superintendents and general foremen of

personnel performing hot work; meetings between the stations Fire Marshal and

contractor supervision to discuss hot work issues; and focused coaching sessions with

fire watch personnel by contractor management conveying the message that the fire

watch is ultimately responsible for the work location being and remaining in compliance

with fire safety standards. Because the licensee has entered the issue into their

corrective action program and the finding is of very low safety significance, this violation

of Technical Specification 5.4.1(c) is being treated as an NCV, consistent with

Section VI.A of the NRC Enforcement Policy. (NCV 05000374/2005002-01)

1R08 Inservice Inspection (ISI) Activities (71111.08)

Piping Systems ISI

a. Inspection Scope

From February 7 to February 9, 2005, and from February 28 to March 1, 2005,

inspectors conducted a review of the implementation of the licensees ISI program for

monitoring degradation of the reactor coolant system boundary and the risk significant

piping system boundaries for Unit 2. The inspectors selected the American Society of

Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Section XI required

examinations and code components in order of risk priority as identified in

Section 71111.08-03 of NRC inspection procedure (IP) 71111.08, Inservice Inspection

Activities, based upon the ISI activities available for review during the onsite inspection

period.

(02.01.a and 02.01.b)

The inspectors conducted an on-site review of the following types of nondestructive

examination activities to evaluate compliance with the ASME Code Section XI and

Section V requirements and to verify that indications and defects (if present) were

dispositioned in accordance with the ASME Code Section XI requirements. Specifically,

the inspectors observed the following examination:

2RH40CB-16-inch restraint RH40-2877X lug welds. Two recordable indications

6 Enclosure

were identified and dispositioned in accordance with the ASME Code Section XI

requirements.

The inspectors performed a record review for the following examination:

No recordable indications were identified.

(02.01.c)

The inspectors reviewed examinations completed during the previous outage with

relevant/recordable conditions/indications that were accepted for continued service to

verify that the licensees acceptance was in accordance with Section XI of the ASME

Code. Specifically, the inspectors reviewed the following records:

  • Five recordable indications found during ultrasonic examination of reactor

pressure vessel weld LCS-2-BH;

  • Ten recordable indications found during ultrasonic examination of reactor

pressure vessel nozzle to shell weld LCS-2-N4D.

(02.01.d)

The inspectors reviewed pressure boundary welds for Code Class 1 or 2 systems which

were completed during the previous refueling outage, to verify that the welding

acceptance and preservice examinations (e.g., pressure testing and dye penetrant

tests) were performed in accordance with the ASME Code Sections III, V, IX, and XI

requirements. Specifically, the inspectors reviewed welds associated with the following

work activity:

  • Penetrant examination of welds for replacement of double block valves

2E12-F325B/326B with single block valves.

(02.05)

The inspectors performed a review of piping system ISI related problems that were

identified by the licensee and entered into the CAP. The inspectors reviewed these

CAP documents to confirm that the licensee had appropriately described the scope of

the problems. Additionally, the inspectors review included confirmation that the

licensee had an appropriate threshold for identifying issues and had implemented

effective corrective actions. The inspectors evaluated the threshold for identifying

issues through interviews with licensee staff and review of licensee actions to

incorporate lessons learned from industry issues related to the ISI program. The

inspectors performed these reviews to ensure compliance with 10 CFR 50, Appendix B,

Criterion XVI, Corrective Action, requirements. The corrective action documents

reviewed by the inspectors are listed in the attachment to this report.

All the reviews discussed above constituted a single inspection sample.

7 Enclosure

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

The inspectors observed a training crew during an evaluated simulator scenario and

reviewed licensed operator performance in mitigating the consequences of events. The

scenario included a scram condition that resulted from a loss of coolant accident

(LOCA). The training crews response to this casualty was complicated by a simulated

stuck open turbine bypass valve. Areas observed by the inspectors included: clarity

and formality of communications, timeliness of actions, prioritization of activities,

procedural adequacy and implementation, control board manipulations, managerial

oversight, emergency plan execution, and group dynamics. Additionally, the inspectors

observed the instructors critique and evaluation of the training crews performance.

This quarterly training observation constituted a single inspection sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the licensee's handling of performance issues and the

associated implementation of the Maintenance Rule (10 CFR 50.65) to evaluate

maintenance effectiveness for the Unit 1 and Unit 2 standby liquid control (SBLC)

systems. The systems were selected based on being designated as risk significant

under the Maintenance Rule and due to inspector-identified issues that potentially could

impact system work practices, reliability, or common cause failures.

The inspectors review included verification of the licensee's categorization of specific

issues, including evaluation of the performance criteria, appropriate work practices,

identification of common cause errors, extent of condition, and trending of key

parameters. Additionally, the inspectors reviewed the licensee's implementation of the

Maintenance Rule requirements, including a review of scoping, goal-setting,

performance monitoring, short-term and long-term corrective actions, functional failure

determinations associated with the condition reports reviewed, and current equipment

performance status.

This maintenance effectiveness review constituted a single inspection sample.

8 Enclosure

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Routine Quarterly Inspections

a. Inspection Scope

The inspectors reviewed and observed emergent work, preventive maintenance, or

planning for risk significant maintenance activities. The inspectors observed

maintenance or planning for the following activities or risk significant systems

undergoing scheduled or emergent maintenance:

ventilation control panels;

  • Unit 1 drywell floor drain sump alternate fill up rate monitor failure upscale

troubleshooting and repair;

  • Unit 1 and Unit 2 Division 1 and 2 safeguards 4,160 Vac buses single point

vulnerability.

The inspectors also reviewed the licensee's evaluation of plant risk, risk management,

scheduling, and configuration control for these activities in coordination with other

scheduled risk significant work. The inspectors verified that the licensee's control of

activities considered assessment of baseline and cumulative risk, management of plant

configuration, control of maintenance, and external impacts on risk. In-plant activities

were reviewed to ensure that the risk assessment of maintenance or emergent work

was complete and adequate, and that the assessment included an evaluation of external

factors. Additionally, the inspectors verified that the licensee entered the appropriate

risk category for the evolutions.

These reviews constituted four inspection samples.

b. Findings

No findings of significance were identified.

.2 1C Circulating Water (CW) Pump Trip During Maintenance

a. Inspection Scope

The inspectors reviewed the licensees planning for work during a scheduled 1A CW

pump maintenance period. Among the items reviewed were the licensee's evaluation of

plant risk, risk management, scheduling, and configuration control for the scheduled

activities, and coordination with other scheduled risk significant work. The inspectors

verified that the licensees control of activities considered assessment of baseline and

cumulative risk, management of plant configuration, control of maintenance, and

9 Enclosure

external impacts on risk. Additionally, the inspectors verified that the licensee entered

the appropriate risk category for the planned maintenance tasks.

This review constituted a single inspection sample.

b. Findings

Introduction

The inspectors identified a finding of very low safety significance (Green) and an

associated Non-Cited Violation (NCV) during a review of the licensees assessment and

management of the risk affiliated with maintenance on the 1A circulating water (CW)

pump. The inspectors review revealed that the licensee had failed to recognize and

effectively manage the risk associated with a meter replacement in a circuit that was

common to both the 1A CW pump, which was undergoing planned maintenance, and

the in service 1C CW pump. This failure to effectively assess and manage maintenance

activity risk was determined by the inspectors to be contrary to the requirements of

10 CFR 50.65(a)(4).

Description

On January 4, 2005, at approximately 1:05 p.m., the 1C CW pump tripped. A planned

maintenance window for the 1A CW pump was in progress to allow plant electricians to

replace the 1A CW pumps elapsed run time meter. An investigation by the licensee

revealed that an actuation of the 1C CW pumps slip guard relay caused the trip. An

electrical short generated during the 1A CW pumps elapsed run time meter

replacement had caused the 1C CW pumps slip guard relay to actuate.

A licensee root cause review (RCR) of this event identified several human performance

issues. First, the work planner for the meter replacement task incorrectly evaluated

production risk when completing the stations production risk evaluation form for the

work package. Second, the electrical maintenance first-line supervisor did not correctly

perform the maintenance risk assessment for the task prior to executing the work. Third,

the craft electricians actually performing the meter replacement task caused an

electrical short that was the initiating event for the transient. Central to all of these

errors was the fact that an unidentified common metering circuitry existed between the

1A and 1C CW pumps. This unidentified circuit caused a short circuit during the 1A CW

pumps meter replacement to affect the running 1C CW pump. This common circuitry

had not been identified by the work planner or by the electrical maintenance first-line

supervisor during their respective risk assessments.

The trip of the 1C CW pump resulted in a slow loss of condenser vacuum, which

translated into an approximate 30 Mwe loss in generation. Ultimately, the licensee

reduced Unit 1 reactor power by approximately six percent in order to allow the

operating crew to more easily deal with the event and the recovery from it.

10 Enclosure

Analysis

The inspector-identified performance deficiency with this issue was the failure on the

part of various licensee staff members to accurately assess and properly manage the

risk associated with replacement of the 1A CW pumps elapsed run time meter. Upon

review of the event, the inspectors determined that sufficient information was available

to identify the common circuitry between the 1A and 1C CW pumps. Consequently, the

licensee should have had sufficient information to properly assess and manage the risk

associated with 1A CW pumps elapsed run time meter replacement. In interviews with

senior licensee staff members, the inspectors identified that had the vulnerability to the

running 1C CW pump been better understood, managers probably would not have

allowed the meter replacement to be performed with the unit on line, or, at a minimum,

would have ensured that more controls and oversight were in place during the evolution.

The objective of the Initiating Events Cornerstone of Reactor Safety is to limit the

likelihood of those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. In accordance with NRC Inspection

Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, the inspectors determined that the finding was of more than minor

significance in that it had a direct impact on this cornerstone objective. Specifically, the

licensees failure to properly assess and effectively manage the risk associated with the

1A CW pumps elapsed run time meter replacement resulted in a transient to the unit

that upset its stability and constituted an unwarranted operating challenge to the

on-watch control room crew.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, and conducted a

Phase 1 characterization and initial screening. Because the finding did not contribute to

both the likelihood of a transient and the likelihood that mitigation equipment or

functions would not be available, the inspectors determined it to be of very low safety

significance (Green) and within the licensees response band. Because the finding

involves the cross-cutting aspect of human performance, it is also noted in Section

4OA4, Cross-Cutting Aspects of Findings, in this report.

Enforcement

As described in the SDP station-specific notebooks for LaSalle Units 1 and 2 and the

licensees Maintenance Rule Program, the CW pumps are risk-significant components.

Section (a)(4) of 10 CFR 50.65 states that before performing maintenance activities

(including but not limited to surveillance, post-maintenance testing, and corrective and

preventive maintenance), the licensee shall assess and manage the increase in risk that

may result from the proposed maintenance activities. Contrary to this requirement, the

licensee failed to properly assess and effectively manage the increase in risk associated

with the replacement of the 1A CW pumps elapsed run time meter.

The licensee had entered this issue into their corrective action program as IR 287541.

Corrective actions completed by the licensee included: administration of training to

enhance worker knowledge and proficiency at performing maintenance risk

assessments on energized equipment; assessment of the existing production risk

11 Enclosure

evaluation sheet used by work planners to determine if additional questions and

clarifications are required; discussion of this type of task at weekly work management

meetings; and reinforcement of the Operations role in reviewing work on production risk

systems. Because the licensee has entered the issue into their corrective action

program and the finding is of very low safety significance, this violation of

10 CFR 50.65(a)(4) is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy. (NCV 05000373/2005002-02)

.3 Valve 1DG032 Disc/Stem Separation During Operation

a. Inspection Scope

The inspectors reviewed the planning associated with a scheduled 0 emergency diesel

generator (EDG) auxiliaries inservice test (IST) on December 30, 2004. Among the

items reviewed were the licensee's evaluation of plant risk, risk management,

scheduling, and configuration control for the activities performed,; and coordination with

other scheduled risk significant work. The inspectors verified that the licensees control

of activities considered assessment of baseline and cumulative risk, management of

plant configuration, control of maintenance, and external impacts on risk. Additionally,

the inspectors verified that the licensee entered the appropriate risk category for the

work performed.

This review constituted a single inspection sample.

b. Findings

Introduction

The inspectors identified a finding of very low safety significance (Green) and an

associated Non-Cited Violation (NCV) during a review of the licensees assessment and

management of the risk affiliated with the cycling of the 1DG032 manual gate valve

during the performance of a scheduled 0 EDG auxiliaries inservice test on

December 30, 2004. The inspectors review revealed that the licensee had failed to

recognize and effectively manage the risk associated with the operation of this valve.

This valve was part of a group of manual gate valves located in the plants essential

service water systems that were known to be highly susceptible to disc/stem separation.

This failure to effectively assess and manage the activitys risk was determined by the

inspectors to be contrary to the requirements of 10 CFR 50.65(a)(4).

Description

On December 30th, 2004, plant operators performed procedure LOS-DG-Q1, 0 Diesel

Generator Auxiliaries Inservice Test, Attachment A5, 0 Diesel Generator Cooling

Water Pump ASME Section XI Test. A pre-evolution briefing, held with two

non-licensed operators (NLOs) included direction that if indicated cooling water flows

were not within specification to return to the control room. The control room operators

would then provide additional briefings to the NLOs on actions contained in the

procedure intended to correct cooling water flow abnormalities.

12 Enclosure

Initial Unit 1 Division 1 cooling water flow rates were identified to be high and outside of

the procedures specified acceptance criteria. The on-watch Shift Manager was notified

of the condition and engineering contacted for assistance. Based on discussions

between engineering and operations personnel, it was determined that operators should

continue in accordance with LOS-DG-Q1, Attachment A5, in an attempt to correct the

out of specification cooling water flow. An additional NLO was assigned to assist with

these activities. A second pre-evolution briefing was held with the three NLOs, followed

by a briefing for the Unit 1 and Unit 2 operations control room crews. Items discussed

during these briefings included applicable Technical Specification Required Actions

(RAs) to be entered when specific valves were to be manipulated, the potential for

stem/disc separation, and the potential for EDG cooling water flow to be high, above

acceptable limits. Although operations personnel were not aware that the 1DG032 valve

was specifically susceptible to stem/disc separation, it was well known within the

licensees organization that similar type valves in this system have had a history of such

failures.

Valve 1DG032 controls flow through the northwest emergency core cooling system

(ECCS) corner room area cooler, the northeast ECCS corner room area cooler, and the

low pressure core spray (LPCS) motor cooler. Procedure LOS-DG-Q1 directed the

NLOs to cycle this valve as part of a sequence of steps intended to perform a flush of

system components in an attempt to restore cooling water flow rates to normal. The

procedure contained no warnings or cautions against cycling the valve. Once in the

field, the NLOs noted no signs or placards on the valve advising of any potential for

stem/disc separation. Because of the lack of any specific guidance to the contrary, the

operators concluded that it was acceptable to continue with the 1DG032 valve cycling

evolution.

In accordance with the approved LOS-DG-Q1 procedure steps, the NLOs cycled the

1DG032 valve. Cooling water flow decreased from approximately 475 gpm to 0 gpm,

and flow noises subsided. However, upon reopening the valve neither cooling water

flow indication nor increased flow noise were noted. After on-watch shift supervisors

were notified and a second attempt to cycle the valve was executed, operations

personnel concluded that the 1DG032 valve had probably suffered a stem/disc

separation.

The 1DG032 valve failure and interruption in cooling water flow resulted in the 1A RHR,

LPCS, and reactor core isolation cooling (RCIC) systems being rendered inoperable. A

subsequent licensee investigation identified that the 1DG032 valve is part of a group of

components with known tendencies for stem/disc separation. Some of these valves

have been replaced or repaired, some have failed and been abandoned (i.e., blank

flanged, etc.), and some, such as was the case with the 1DG032 valve, had not been

operated for years and their exact condition was not known. This information was

contained within the licensees computer database used to generate clearances/tagouts,

as well as on engineering prints specifically created to highlight the susceptible

components. Many members of the licensees staff, such as cycle planners, system

engineers, and work week managers, were aware of these susceptible components, but

the specific information was not provided to plant operators or properly captured in

procedures or other controlled reference documents.

13 Enclosure

Analysis

The inspector-identified performance deficiency with this issue was a failure on the part

of the licensee to accurately assess and properly manage the risk associated with the

cycling of the 1DG032 manual gate valve. Upon review of the event, the inspectors

determined that sufficient written information was available to the licensees organization

that should have alerted plant operators to the risk involved with cycling 1DG032. In

interviews with plant operators and other personnel, the inspectors identified that had

the susceptibility for 1DG032 stem/disc separation been better understood, on-watch

operations supervisors probably would not have allowed the evolution to have gone

forward, or, at a minimum, would have ensured that more controls and oversight were in

place during the evolution.

The objective of the Mitigating Systems Cornerstone of Reactor Safety is to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). In accordance with NRC

Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports,

Appendix B, Issue Screening, the inspectors determined that the finding was of more

than minor significance in that it had a direct impact on this cornerstone objective.

Specifically, the licensees failure to properly assess and effectively manage the risk

associated with the 1DG032 valve cycling evolution resulted in the interruption of

supporting cooling water flow to Unit 1 Division 1 ECCS components, rendering these

components inoperable and unavailable.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, and conducted a

Phase 1 characterization and initial screening. Because the finding only impacted a

single Division of ECCS and did not represent the loss of any entire systems safety

function, and because no Technical Specification allowed outage times were exceeded

and the finding was not related to external events such as fire, flooding, or adverse

weather, the inspectors determined it to be of very low safety significance (Green) and

within the licensees response band.

Enforcement

Section (a)(4) of 10 CFR 50.65 states that before performing maintenance activities

(including but not limited to surveillance, post-maintenance testing, and corrective and

preventive maintenance), the licensee shall assess and manage the increase in risk that

may result from the proposed maintenance activities. Contrary to this requirement, the

licensee failed to properly assess and effectively manage the increase in risk associated

with cycling the 1DG032 manual gate valve. Specifically, this type of valve was known

to be susceptible to stem/disc separation, posing the potential for increased risk when

cycling the valve.

The licensee had entered this issue into their corrective action program as IR 286665.

Corrective actions completed by the licensee include: hanging tags on susceptible

valves to warn personnel of the potential for stem/disc separation; validation of all

essential service water valves susceptible to stem/disc separation and providing a listing

of these components to plant operations; revision of applicable operating procedures to

14 Enclosure

include a precaution that identifies the valves that are susceptible to stem/disc

separation and a requirement to verify the applicability of valves prior to operation; and

review of the issue as a potential operator challenge/workaround. Because the licensee

has entered the issue into their corrective action program and the finding is of very low

safety significance, this violation of 10 CFR 50.65(a)(4) is being treated as an NCV,

consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000373/2005002-03)

1R14 Operator Performance During Non-Routine Evolutions and Events (71111.14)

.1 Operator Response to 1C Circulating Water Pump Trip on January 4, 2005

a. Inspection Scope

The inspectors performed several hours of continuous control room observation to

evaluate operator performance in coping with an unexpected trip of the 1C circulating

water (CW) pump during a planned maintenance window for the 1A CW pump. The

inspectors reviewed operator logs and plant computer data to determine how the unit

responded and to verify that operator actions were appropriate, and consistent with

operator training and plant procedures. The licensees planned recovery actions,

procedures, reactivity manipulation briefings, and contingency plans were also reviewed

by the inspectors to identify any personnel performance issues. In addition, the

inspectors verified that any problems encountered during the non-routine evolution were

identified by the licensee, and appropriately entered into the corrective action program.

The observation of this non-routine evolution by the inspectors constituted a single

inspection sample.

b. Findings

No findings of significance were identified.

.2 Operator Response to the Losses of Unit 2 Shutdown Cooling on February 7, 2005

a. Inspection Scope

The inspectors performed several hours of control room observation to evaluate

operator performance in coping with two unplanned interruptions of shutdown cooling

flow. The first occurred at 7:56 a.m. due to valve isolations resulting from a trip of the

A reactor protection system (RPS) power supply. The second occurred at 10:55 a.m.

due to the failure of the reactor recirculation (RR) system B loop discharge stop valve,

F067B, to close after shutdown of the B RR pump. The inspectors reviewed operator

logs, vessel temperature traces, and plant computer data to determine unit conditions

and to verify that operator actions were appropriate, and consistent with operator

training and plant procedures. The licensees planned recovery actions, procedures,

reactivity manipulation briefings, and contingency plans were also reviewed by the

inspectors to identify any personnel performance issues. In addition, the inspectors

verified that any problems encountered during the non-routine evolution were identified

by the licensee, and appropriately entered into the corrective action program.

15 Enclosure

The observation of this non-routine evolution by the inspectors constituted a single

inspection sample.

b. Findings

No findings of significance were identified.

.3 Operator Response to the Identification of a Single Point Vulnerability Affecting

Division 1 and Division 2 4,160 Vac Safety Related Power

a. Inspection Scope

The inspectors evaluated operator performance during the identification of a single point

vulnerability affecting the 4,160 Vac safety related switchgear on both Division 1 and

Division 2 on both LaSalle units. The inspectors reviewed operator logs, clearance

orders, equipment status tags, and plant computer data to determine unit conditions and

to verify that operator actions were appropriate, and consistent with operator training

and plant procedures. The licensees planned recovery actions, procedures, reactivity

manipulation briefings, and contingency plans were also reviewed by the inspectors to

identify any personnel performance issues. In addition, the inspectors verified that any

problems encountered during the non-routine evolution were identified by the licensee,

and appropriately entered into the corrective action program.

The observation of this non-routine evolution by the inspectors constituted a single

inspection sample.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the technical adequacy of the following operability evaluations

to determine the impact on Technical Specifications, the significance of the evaluations,

and to ensure that adequate justifications were documented:

  • Degradation of Lisega snubber operating oil due to radiation exposure in the

Unit 1 and Unit 2 drywells (OE 04-008);

following water intrusion into control panels;

isolation valves (CIVs) from the 10 CFR 50, Appendix J, Type C local leak rate

testing (LLRT) program (EC 332208);

  • Degraded cooling fans on Transformer 236Y (OE 04-007);
  • L2R10 lost parts evaluations for the reactor vessel and connected primary

systems (EC 354196 and EC 354344).

16 Enclosure

Operability evaluations were selected based upon the relationship of the safety-related

system, structure, or component to risk.

These reviews constituted five inspection samples.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds (71111.16)

a. Inspection Scope

The inspectors reviewed an operator workaround involving the manual control of reactor

building ventilation control dampers. The inspectors reviewed the workarounds

potential to impact the operators ability to maintain reactor building differential pressure

below the Technical Specification limit and detect potential changes in secondary

containment integrity.

This review represented a single inspection sample.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17)

a. Inspection Scope

The inspectors reviewed the following modifications to verify that the design basis,

licensing basis, and performance capability of risk significant systems were not

degraded by the installation of the modifications. The inspectors also verified that the

modifications did not place the plant in an unsafe configuration.

elimination (EC 342975) and stainless steel valve replacements (EC 343542)

  • Unit 2 steam dryer lifting lug upper support removal (EC 353949)

The inspectors considered the design adequacy of the modification by performing a

review, or partial review, of the modifications impact on plant electrical requirements,

material requirements and replacement components, response time, control signals,

equipment protection, operation, failure modes, and other related process requirements.

These reviews constituted three inspection samples.

b. Findings

No findings of significance were identified.

17 Enclosure

1R19 Post-Maintenance Testing (71111.19)

.1 Miscellaneous Post-Maintenance Testing Reviews

a. Inspection Scope

The inspectors selected the following post-maintenance activities for review. Activities

were selected based upon the structure, system, or component's ability to impact risk.

  • Unit 1 drywell floor drain sump alternate fill up rate monitor post repair testing

and calibration

  • Unit 1 rod position indication system testing following probe data receiver card

replacement

  • Unit 2 A RPS motor generator set testing following voltage regulator repairs

The inspectors verified by witnessing the test or reviewing the test data that

post-maintenance testing activities were adequate for the above maintenance or repair

activities. The inspectors reviews included, but were not limited to, integration of testing

activities, applicability of acceptance criteria, test equipment calibration and control,

procedural use and compliance, control of temporary modifications or jumpers required

for test performance, documentation of test data, Technical Specification applicability,

system restoration, and evaluation of test data. Also, the inspectors verified that

maintenance and post-maintenance testing activities adequately ensured that the

equipment met the licensing basis, Technical Specifications, and Updated Final Safety

Analysis Report (UFSAR) design requirements.

These reviews constituted three inspection samples.

b. Findings

No findings of significance were identified.

.2 Unit 2 Division 1 125 V Battery Charger Return to Service Following Maintenance

a. Inspection Scope

The inspectors reviewed the post maintenance testing and the return to service of the

Unit 2 Division 1 125 Vdc battery charger, 2DC09E, following maintenance activities on

January 19, 2005 and January 28, 2005. Design changes to the 125 Vdc system were

reviewed as well as maintenance and operations procedures for the 125 Vdc system.

Inspectors evaluated licensee performance and knowledge level during operation of

these chargers.

The observation of this post-maintenance test by the inspectors constituted a single

inspection sample.

18 Enclosure

b. Findings

Introduction

A finding of very low safety significance was self-revealed when a design modification to

the Unit 2 Division 1 125 Vdc charger system was not appropriately incorporated into

operational procedures. This resulted in an under-voltage condition during an attempt to

swap on-service chargers. An NCV of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, for failure to properly incorporate design

changes into procedures for the 125 Vdc system, was identified.

Description

On January 19, 2005, during the return to service of the Unit 2 Division 1 125 Vdc

charger, 2DC09E, following maintenance, a Division 1 125 Vdc bus undervoltage alarm

was received. During the swap of the on-service charger, 2DC23E, with the oncoming

charger, 2DC09E, the oncoming charger failed to pick up load. This resulted in a low

voltage condition on the Division 1 125 Vdc bus and the subsequent inoperability of that

bus. 2DC23E was restored as the on-service charger and the bus undervoltage alarms

cleared. Total inoperability time for the Division 1 125 Vdc bus was approximately

23 minutes.

Troubleshooting was commenced to determine the cause of the failure. It was

subsequently determined that a procedural problem with LOP-DC-01, Battery Charger

Startup and Shutdown, was the cause of this failure. Changes to the battery charger

system since the last design modification had not been adequately incorporated into the

procedures used to swap battery chargers, or into operator training lesson plans.

Specifically, voltage metering on the 2DC09E battery charger tapped into the DC

circuitry in a different location than similar metering on the existing 2DC23E battery

charger. The differences in voltage metering taps between the two chargers resulted in

plant operators being presented with different indications when swapping from 2DC09E

to 2DC23E, as opposed to when swapping from 2DC23E to 2DC09E.

The procedure was revised and training for operators on the procedure revision was

conducted. The 2DC09E charger was also tested with a load bank to verify it was

operating properly.

On January 28, 2005, licensee personnel again attempted to swap 2DC09E with the

on-service charger, 2DC23E. During the swap, multiple control room alarms were

received because the oncoming charger bus voltage was too high. Though this did not

result in the inoperability of the DC bus, it did result in the inoperability of several

process radiation monitors (PRMs) and the Unit 2 off gas log pretreatment monitor. The

inspectors observed the evolution and discussed the issue with plant operations

personnel. The inspectors concluded that, although the licensee had revised the

procedure for swapping chargers and trained operators on the specific revision, plant

operators performing the actual charger swap were still unaware of the differences in

voltage metering between the two battery chargers.

19 Enclosure

Analysis

The performance deficiency associated with this event was a failure on the part of

licensee personnel to have incorporated relevant design information, specifically

information regarding differences in voltage metering between 2DC09E and 2DC23E,

into LOP-DC-01, Battery Charger Startup and Shutdown.

The objective of the Mitigating Systems Cornerstone of Reactor Safety is to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). In accordance with NRC

Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports,

Appendix B, Issue Screening, the inspectors determined that the finding was of more

than minor significance in that it had a direct impact on this cornerstone objective.

Specifically, the inspectors concluded that the licensees performance deficiency was

primarily responsible for a low voltage condition on the Unit 2 Division 1 125 Vdc system

on January 19, 2005, which rendered this system inoperable for approximately

23 minutes.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, and conducted a

Phase 1 characterization and initial screening. Because the finding involved the loss of

only one train of safety related equipment and the loss was for less than the Technical

Specification allowed outage time, the inspectors determined it to be of very low safety

significance (Green) and within the licensees response band.

Enforcement

Table 3.2-1 of the licensees Updated Final Safety Analysis Report (UFSAR) indicated

that the 125 Vdc battery chargers are subject to the requirements of 10 CFR 50,

Appendix B. Criterion V, Instructions, Procedures, and Drawings, of this appendix

states, in part, that: Activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances and

shall be accomplished in accordance with these instructions, procedures, and drawings.

Contrary to this requirement, the licensee, by not incorporating relevant information

concerning battery charger voltage metering into the procedure for swapping battery

chargers, failed to properly prescribe an activity affecting quality, the swapping of battery

chargers, into the stations instructions and procedures for this task.

The licensee had entered this issue into their corrective action program as IR 287541.

Corrective actions planned and completed by the licensee include: revision of

LOP-DC-01 and training for operations personnel on new charger procedures. Because

the licensee has entered the issue into their corrective action program and the finding is

of very low safety significance, this violation of 10 CFR 50 Appendix B, Criterion V, is

being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000374/2005002-04)

20 Enclosure

.3 Unit 1 Core Standby Cooling System (CSCS) Pump Room Ventilation System Control

Cabinet Water Intrusion

a. Inspection Scope

The inspectors reviewed repairs and testing of the Unit 1 Division 1 and Division 2

CSCS pump room ventilation system after water intrusion into the conduit system

resulted in erratic behavior of the Unit 1 Division 2 temperature controller. Repairs to

the controller and conduit system were inspected, including the method and

effectiveness of sealing the conduit to prevent further water intrusion.

The observation of this post-maintenance test by the inspectors constituted a single

inspection sample.

b. Findings

No findings of significance were identified. One unresolved item (URI) was identified.

On January 3, 2005, during a rain/snow shower, the control room received a high

temperature alarm for the Unit 1 Division 2 CSCS pump room ventilation system (VY).

The room temperature controller, 1TIC-VY024, was indicating 120 degrees. Actual

room temperature was verified to be 73 degrees. The erratic behavior of this

temperature controller resulted in the potential loss of temperature control for the

Division 2 CSCS pump room and, consequently, the inoperability of the C and D

RHRSW pumps and the B spent fuel pool cooling (FC) emergency makeup pump. In

January 2003, this same temperature controller had failed and had been replaced. The

cause of this failure was never established.

Subsequent to the adverse weather on January 3, 2005, the 1TIC-VY024 controller was

replaced with a new controller, but still continued to exhibit erratic behavior. The original

controller was reinstalled and it was noted during troubleshooting that water dripping into

the control panel from an internal conductor onto a terminal strip was causing stray

currents which resulted in the erratic behavior of this controller. Further investigation

revealed water intrusion inside the conduit connected to this control panel. Corrosion

and standing water were also located in junction box 1JB301A associated with this

conduit.

On January 5, 2005, repairs were performed to clean and dry the Division 2 VY conduit

system and clean, paint, and drill weep holes in junction box 1JB301A . An

extent-of-condition walkdown by the licensee noted that the Division 1 VY conduit and

control panel also exhibited signs of water intrusion. Long term rust deposits and water

dripping within the control panel were observed. This division was not considered

inoperable due to a wiring configuration difference between the Division 1 and Division 2

control panels that directed dripping water within the panel away from the terminal strip.

This wiring practice was commonly termed as installing drip loops and was required for

cable terminations of this type per licensee maintenance procedures.

On January 9, 2005, the licensee made repairs to the Division 1 VY conduits in an

attempt to stop the water intrusion by sealing the conduit. On February 15, 2005, during

21 Enclosure

a rain shower, inspectors in the plant identified water dripping from weep holes in the

Division 1 VY junction boxes from conduit that had supposedly been sealed several

days earlier to prevent such water intrusion.

On March 25, 2005, during a rain shower, inspectors again identified water dripping

from junction boxes on both Division 1 and Division 2 VY conduits that had previously

been repaired for similar water intrusion events.

At the time of the writing of this report, the inspectors had challenged licensee

engineering and maintenance personnel with several questions related to this issue. In

response, the licensee had entered multiple items associated with this event into their

corrective action program (IRs 287742, 287334, 287987, 287351, 287694, 288823,

308000, 301768, and 317267). Among the actions the licensee has performed, or plans

to perform, to address this issue include: a complete extent-of-condition review of all

through roof conduits that may be susceptible to water intrusion; drilling of weep holes in

all susceptible junction boxes; repairs to damage caused by water intrusion; the sealing

of the leaking conduit on Unit 1 Division 1 and Division 2 VY systems; and determining

the actual cause of the water intrusion into the conduits. This issue is considered

unresolved, pending the inspectors receipt and review of the licensees corrective action

program products and the steps taken per the licensees action plan to address the

nonconforming condition. (URI 05000373/2005002-05)

1R20 Outage Activities (71111.20)

a. Inspection Scope

The inspectors evaluated outage activities for an refueling outage that began on

February 7, 2005, and ended on March 16, 2005. The inspectors reviewed activities to

ensure that the licensee considered risk in developing, planning, and implementing the

outage schedule.

The inspectors observed or reviewed the reactor shutdown and cooldown, outage

equipment configuration and risk management, electrical lineups, selected clearances,

control and monitoring of decay heat removal, control of containment activities, startup

and heatup activities, and identification and resolution of problems associated with the

outage.

The inspectors review of outage activities represented a single inspection sample.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors selected the following surveillance test activities for review. Activities

were selected based upon risk significance and the potential risk impact from an

22 Enclosure

unidentified deficiency or performance degradation that a system, structure, or

component could impose on the unit if the condition were left unresolved. These

reviews constituted nine inspection samples.

  • Unit 1 and Unit 2 drywell leak detection systems tests and calibrations

leak rate testing

leak rate test

The inspectors observed the performance of surveillance testing activities, including

reviews for preconditioning, integration of testing activities, applicability of acceptance

criteria, test equipment calibration and control, procedural use, control of temporary

modifications or jumpers required for test performance, documentation of test data,

Technical Specification applicability, impact of testing relative to performance indicator

reporting, and evaluation of test data.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors selected the following temporary modifications for review. The

inspectors reviewed the safety screening, design documents, UFSAR, and applicable

Technical Specifications to determine that the temporary modifications were consistent

with modification documents, drawings, and procedures. The inspectors also reviewed

the post-installation test results to confirm that tests were satisfactory and that the actual

impact of the temporary modification on the permanent system and interfacing systems

were adequately verified.

  • Installation of alternate method for determining Unit 1 drywell floor drain sump

flow rate (TCCP 353167)

  • Removal of 1DG032 internals and freeze seal (EC 353125)
  • Energizing both 125 Vdc division 1 or 2 battery chargers simultaneously to

support battery charger testing (EC 340584)

  • Removal of station auxiliary transformer (SAT) metering (EC 353657)

These reviews constituted four inspection samples.

23 Enclosure

b. Findings

No findings of significance were identified.

1EP2 Alert and Notification System (ANS) Testing (71114.02)

a. Inspection Scope

The inspectors discussed with corporate and station-based Emergency Preparedness

(EP) staffs the operation, maintenance, and periodic testing of the ANS in the LaSalle

County Stations plume pathway Emergency Planning Zone (EPZ) to determine whether

the ANS equipment was adequately maintained and tested in accordance with

Emergency Plan commitments and procedures. The inspectors reviewed records of

2003 and 2004 preventive and non-scheduled maintenance activities, as well as

January 2004 through December 2004 ANS operability test results.

These activities constituted a single inspection sample.

b. Findings

No findings of significance were identified.

1EP3 Emergency Response Organization (ERO) Augmentation Testing (71114.03)

a. Inspection Scope

The inspectors reviewed and discussed with station EP staff the procedures that

included the primary and alternate methods of initiating an ERO activation to augment

the on-watch ERO and the provisions for maintaining the stations ERO call-out roster.

The inspectors reviewed critiques and a sample of corrective action program records of

unannounced off-hours augmentation drills, which were conducted monthly between

April 2004 and January 2005, to determine the adequacy of the critiques and associated

corrective actions. The inspectors also reviewed the EP training records of a random

sample of 30 LaSalle County Station ERO members, who were assigned to key and

support positions, to determine whether they were currently trained for their assigned

ERO positions. The inspectors also reviewed the LaSalle County Stations ERO roster

to verify that appropriate personnel were assigned to each response position.

These activities constituted a single inspection sample.

b. Findings

No findings of significance were identified.

24 Enclosure

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a. Inspection Scope

The inspectors reviewed a sample of Nuclear Oversight staffs 2004 reviews of the

LaSalle County Stations EP program to verify that these independent assessments met

the requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports and

samples of corrective action program records associated with those reviews. The

inspectors also reviewed the licensees critique of its emergency response to an actual

seismic event, which included an Unusual Event declaration, that occurred in

June 2004. The inspectors reviewed critique reports and samples of corrective action

program records associated with the 2004 biennial exercise, as well as various EP drills

conducted between July 2003 and December 2004, in order to verify that the licensee

fulfilled its drill commitments and to evaluate the licensees efforts to identify, track, and

resolve concerns identified during these activities. The inspectors also reviewed

samples of corrective action program documents associated with other aspects of the

Stations EP program.

These activities constituted a single inspection sample.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors reviewed licensee controls and surveys in the following five radiologically

significant work areas within radiation areas, high radiation areas, and airborne

radioactivity areas in the plant and reviewed work packages which included associated

licensee controls and surveys of these areas to determine if radiological controls

including surveys, postings, and barricades were acceptable:

  • Reactor vessel disassembly and reassembly;
  • Chemical decontamination and drywell work;
  • Suppression pool diving;
  • Low pressure heater bay maintenance.

This review represented one inspection sample.

25 Enclosure

The inspectors reviewed the radiation work permits (RWPs) and work packages used to

access these five areas and other high radiation work areas to identify the work control

instructions and control barriers that had been specified. Electronic dosimeter alarm set

points for both integrated dose and dose rate were evaluated for conformity with survey

indications and plant policy. Workers were interviewed to verify that they were aware of

the actions required when their electronic dosimeters noticeably malfunctioned or

alarmed.

This review represented one inspection sample.

The inspectors walked down and surveyed (using a calibrated NRC survey meter) these

five areas to verify that the prescribed RWP, procedure, and engineering controls were

in place, that licensee surveys and postings were complete and accurate, and that air

samplers were properly located.

This review represented one inspection sample.

The inspectors reviewed RWPs for airborne radioactivity areas to verify barrier integrity

and engineering controls performance (e.g., high efficiency particulate air (HEPA)

ventilation system operation) and to determine if there was a potential for individual

worker internal exposures of greater than 50 millirem committed effective dose

equivalent. Work areas having a history of, or the potential for, airborne transuranics

were evaluated to verify that the licensee had considered the potential for transuranic

isotopes and provided appropriate worker protection. There were no airborne

radioactivity work areas identified during the course of the inspection.

This review represented one inspection sample.

The adequacy of the licensees internal dose assessment process for internal exposures

greater than 50 millirem committed effective dose equivalent was assessed. There

were no internal exposures greater than 50 millirem.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

.2 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, licensee event reports,

and special reports related to the access control program to verify that identified

problems were entered into the corrective action program for resolution.

This review represented one inspection sample.

26 Enclosure

The inspectors reviewed 15 corrective action reports related to access controls and 2

high radiation area radiological incidents when available (non-performance indicators

identified by the licensee in high radiation areas <1R/hr). Staff members were

interviewed and corrective action documents were reviewed to verify that follow-up

activities were being conducted in an effective and timely manner commensurate with

their importance to safety and risk based on the following:

  • Initial problem identification, characterization, and tracking;
  • Disposition of operability/reportability issues;
  • Evaluation of safety significance/risk and priority for resolution;
  • Identification of repetitive problems;
  • Identification of contributing causes;
  • Identification and implementation of effective corrective actions;
  • Resolution of NCVs tracked in the corrective action system;
  • Implementation/consideration of risk significant operational experience feedback.

This review represented one inspection sample.

The inspectors evaluated the licensees process for problem identification,

characterization, prioritization, and verified that problems were entered into the

corrective action program and resolved. For repetitive deficiencies and/or significant

individual deficiencies in problem identification and resolution, the inspectors verified

that the licensees self-assessment activities were capable of identifying and addressing

these deficiencies.

This review represented one inspection sample.

The inspectors reviewed licensee documentation packages for all performance indicator

(PI) events occurring since the PI events involved dose rates greater than 25 R/hr at

30 centimeters or greater than 500 R/hr at 1 meter. Barriers were evaluated for failure

and to determine if there were any barriers left to prevent personnel access. There

were no PI events occurring since the last inspection.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

.3 Job-In-Progress Reviews

a. Inspection Scope

The inspectors observed the following five jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers:

  • Drywell CRD pull/put activities;
  • Reactor vessel disassembly and reassembly;

27 Enclosure

  • Chemical decontamination and drywell work;
  • Suppression pool diving;
  • Low pressure heater bay maintenance.

The inspectors reviewed radiological job requirements for these five activities, including

RWP requirements and work procedure requirements, and attended As-Low-As-Is-

Reasonably-Achievable (ALARA) job briefings.

This review represented one inspection sample.

The above review is combined with NRC IP 71121.02, ALARA, Planning, and Controls,

and documented in Section 2OS2.2.

Job performance was observed with respect to these requirements to verify that

radiological conditions in the work area were adequately communicated to workers

through pre-job briefings and postings. The inspectors also verified the adequacy of

radiological controls including required radiation, contamination, and airborne surveys

for system breaches; radiation protection job coverage which included audio and visual

surveillance for remote job coverage; and contamination controls.

This review represented one inspection sample.

Radiological work in high radiation work areas having significant dose rate gradients

was reviewed to evaluate the application of dosimetry to effectively monitor exposure to

personnel and to verify that licensee controls were adequate. These work areas

involved areas where the dose rate gradients were severe (diving activities and the

reactor water cleanup (RWCU) heat exchanger room) which increased the necessity of

providing multiple dosimeters and/or enhanced job controls.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

.4 Radiation Worker Performance

a. Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation protection work requirements and

evaluated whether workers were aware of the significant radiological conditions in their

workplace, of the RWP controls and limits in place, and that their performance had

accounted for the level of radiological hazards present.

This review represented one inspection sample.

The inspectors reviewed radiological problem reports which found that the cause of the

event was due to radiation worker errors to determine if there was an observable pattern

28 Enclosure

traceable to a similar cause, and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. These

problems, along with planned and taken corrective actions were discussed with the

Radiation Protection Manager.

This review represented one inspection sample.

b. Findings

(1) Electrician Enters the Drywell on the Wrong RWP

Introduction

A self-revealing finding of very low safety significance (Green) and an associated NCV

were identified when an electrician logged onto a general all-buildings minor

maintenance activities RWP and entered the drywell, a posted HRA, contrary to the

licensees Technical Specifications. The finding was identified when the electricians

electronic dosimeter alarmed after he entered a 106 millirem/hour dose field in the

drywell.

Description

On February 7, 2005, an electrician was assigned to minor electrical maintenance work

in the drywell.

The workers proceeded to the RP desk to sign on to the RWP 10003998, Unit 2

Drywell (construction) Minor Maintenance Activities for L2R10. This RWP contained

proper controls for the assigned activity in a HRA. The workers proceeded to the

electronic dosimeter (ED) station where the electrician mistakenly signed onto RWP

10003938, All-Building Minor Maintenance Activities. The ED computer sign-in had

displayed screens to allow the individual to verify the RWP number, and these screens

were incorrectly answered in the affirmative. The electrician knew the dose and dose

rate limits for the correct RWP from the HRA pre-job brief. The electrician entered the

radiologically controlled area (RCA) and proceeded to the work area at approximately

1:50 a.m. and left the RCA at 5:00 p.m.

When the electrician exited the drywell and checked out of the RCA, he received a

warning on the computer screen that he had received a dose rate alarm during the

entry. He immediately notified RP staff of the warning. The RP staff investigated the

event and identified that he had signed on to the wrong RWP.

The individual received a total dose of 4 millirem, and the maximum dose rate measured

by the ED was 106 millirem/hour.

The failure to assure through self-checking that each high radiation area entry is made

using the correct RWP that includes specification of radiation dose rates in the

immediate work area and other appropriate radiation protection equipment and

measures is contrary to Technical Specification 5.7.1: (a) requiring entry controls; and

(b) requiring that an appropriate RWP be utilized by workers.

29 Enclosure

The licensees initial prompt investigation determined the cause to be a failure of human

performance error prevention techniques. Specifically, the electrician lacked

self-checking and peer-checking in entering the wrong RWP and accepting the ED

log-in screens that asked if this was the correct RWP. As immediate corrective actions,

the individual was locked out of the stations RCA, and the licensee initiated an

investigation. Additionally, all site personnel were notified of this event through a station

safety alert.

Analysis

The inspectors determined that the performance deficiency associated with this event

was failure to follow procedure, in that the individual did not electronically sign onto the

right RWP. The finding, under the Occupational Radiation Safety Cornerstone, does not

involve the application of traditional enforcement because it did not result in actual

safety consequences or potential to impact the NRCs regulatory function and was not

the result of any willful actions. The finding was more than minor as it could be

reasonably viewed as a precursor to a more significant event. The finding is associated

with one of the cornerstone attributes, specifically occupational radiation safety.

The inspectors determined that the finding was more than minor because the

occurrence involved an individual worker potential unplanned, unintended dose resulting

from actions or conditions contrary to licensee procedures and radiation work permit

which could have been significantly greater as a result of a single minor, reasonable

alteration of the circumstances. The finding was evaluated using the Significance

Determination Process (SDP) for the Occupational Radiation Safety Cornerstone and

was determined to be of very low safety significance (Green). The finding did not

involve an ALARA issue, as collective dose was not an issue. Furthermore, the

individuals radiation exposure was low relative to regulatory limits; there was not a

substantial potential for a worker overexposure; and the licensees ability to assess

worker dose was not compromised.

Because the inspectors determined that the primary cause for the finding was related to

the cross-cutting aspect of human performance, it is discussed in Section 4OA4 as well.

Enforcement

Technical Specification 5.7.1(a) and 5.7.1(b) require for HRAs, with dose rates not

exceeding 1.0 rem per hour at 30 centimeters from the radiation source, that access to

and activities in each area shall be controlled by means of a RWP that includes the

specification of radiation dose rates in the immediate work area and other appropriate

radiation protection equipment and measures. Contrary to the above, on

February 7, 2005, an electrician received a dose rate alarm when working in the drywell

during the L2R10 refueling outage. The worker entered an elevated dose rate area

above the floor, an area that was not normally surveyed, and this action was contrary to

the limits of the RWP onto which he had electronically acknowledged. Because entry

into the RCA was conducted under an all-buildings scaffold activities RWP, the entry

into the HRA was monitored by EDs. Since the finding is of very low safety significance

and had been entered into the corrective action system as IR 218052, the associated

30 Enclosure

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy (NCV 05000374/2005002-06).

(2) Venture Pipefitters Enter HRA Without RWP Brief on February 13, 2005

No findings of significance were identified. One unresolved item (URI) was identified.

On February 13, 2005, a Radiation Protection Technician (RPT) identified that a

pipefitter foreman and two pipefitters had inappropriately gone past two HRA postings

and barricades to enter the condenser pit room. Prior to the unauthorized entry, the

pipefitters discussed their work and RWP limitations (RWP 1004122, Unit 2 Minor

Maintenance-Non-HRA) with RPTs at the low pressure heater bay access point. The

RPTs thought the pipefitters were working in the adjacent amertap room, which was not

a posted HRA. The RPTs and pipefitters confirmed through a 3-way communication

that the discussion was not an HRA brief and that they were not to enter any HRAs. In

addition, all three pipefitters had attended the required radworker training that

specifically challenged the workers on HRA entry requirements.

When the pipefitters entered the condenser pit room HRA to access their assigned work

area, they identified that they needed a survey completed before accessing a scaffold.

They requested assistance from a RPT in the area for this task. The RPT asked if they

had received an HRA brief. They told the RPT they had received the required brief.

The RPT completed the survey for them, and the pipefitters completed the assigned

work in the HRA and left the area. The highest dose rate for the pipefitters was

38 millirem/hour and the highest dose was 3.7 millirem. No electronic dosimeter alarms

were activated by the entry.

When the RPT returned to the low pressure heater bay access point he questioned why

he was not made aware that the pipefitters were being sent to the condenser pit for

assigned work. At this point, it was identified that the pipefitters were not properly

briefed and were on the wrong RWP.

Because the pipefitters had potentially been directed by their supervisor to enter the

HRA, the event remains under review by the NRC pending further investigation and is

categorized as an Unresolved Item. (URI 05000374/2005002-07)

.5 Radiation Protection Technician Proficiency

a. Inspection Scope

During job performance observations, the inspectors evaluated RPT performance with

respect to radiation protection work requirements and evaluated whether they were

aware of the radiological conditions in their workplace, the RWP controls and limits in

place, and if their performance was consistent with their training and qualifications with

respect to the radiological hazards and work activities.

This review represented one inspection sample.

31 Enclosure

The inspectors reviewed radiological problem reports which found that the cause of the

event was radiation protection technician error to determine if there was an observable

pattern traceable to a similar cause and to determine if this perspective matched the

corrective action approach taken by the licensee to resolve the reported problems.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

2OS2 As Low As Is Reasonably Achievable Planning And Controls (ALARA) (71121.02)

.1 Radiological Work Planning

a. Inspection Scope

The inspectors evaluated the licensees list of work activities ranked by estimated

exposure that were in progress and reviewed the following five work activities of highest

exposure significance:

  • Drywell CRD pull/put activities;
  • Reactor vessel disassembly and reassembly;
  • Chemical decontamination and drywell work;
  • Suppression pool diving;
  • Low pressure heater bay maintenance.

This review represented one inspection sample.

For these five activities, the inspectors reviewed the ALARA work activity evaluations,

exposure estimates, and exposure mitigation requirements in order to verify that the

licensee had established procedures, and engineering and work controls that were

based on sound radiation protection principles in order to achieve occupational

exposures that were ALARA. This also involved determining that the licensee had

reasonably grouped the radiological work into work activities, based on historical

precedence, industry norms, and/or special circumstances.

This review represented one inspection sample.

The inspectors compared the results achieved including dose rate reductions and

person-rem used with the intended dose established in the licensees ALARA planning

for these five work activities. Reasons for inconsistencies between intended and actual

work activity doses were reviewed.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

32 Enclosure

.2 Job Site Inspections and ALARA Control

a. Inspection Scope

The inspectors observed the following five jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers:

  • Drywell CRD pull/put activities;
  • Reactor vessel disassembly and reassembly;
  • Chemical decontamination and drywell work;
  • Suppression pool diving;
  • Low pressure heater bay maintenance.

The licensees use of ALARA controls for these work activities was evaluated.

Specifically, the licensees use of engineering controls to achieve dose reductions was

evaluated to verify that procedures and controls were consistent with the licensees

ALARA reviews, that sufficient shielding of radiation sources was provided for, and that

the dose expended to install/remove the shielding did not exceed the dose reduction

benefits afforded by the shielding.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

.3 Source-Term Reduction and Control

a. Inspection Scope

The inspectors reviewed licensee records to determine the historical trends and current

status of tracked plant source terms and to evaluate if the licensee was making

allowances and had developed contingency plans for expected changes in the source

term due to changes in plant fuel performance issues or changes in plant primary

chemistry. Additionally, the inspectors reviewed the licensees chemical

decontamination activities and cold noble metals addition during this refueling outage.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

33 Enclosure

.4 Radiation Worker Performance

a. Inspection Scope

Radiation worker and RPT performance was observed during work activities being

performed in radiation areas, airborne radioactivity areas, and high radiation areas that

presented the greatest radiological risk to workers. The inspectors evaluated whether

workers demonstrated the ALARA philosophy in practice by being familiar with the work

activity scope and tools to be used, by utilizing ALARA low dose waiting areas and that

work activity controls were being complied with. Also, radiation worker training and skill

levels were reviewed to determine if they were sufficient relative to the radiological

hazards and the work involved.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

.5 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, and special reports

related to the ALARA program since the last inspection to determine if the licensees

overall audit programs scope and frequency for all applicable areas under the

Occupational Cornerstone met the requirements of 10 CFR 20.1101(c).

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

.1 Emergency Preparedness Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed the licensees records associated with the three EP

performance indicators (PIs) listed below. The inspectors verified that the licensee

accurately reported these indicators in accordance with relevant procedures and

Nuclear Energy Institute guidance endorsed by NRC. Specifically, the inspectors

34 Enclosure

reviewed licensee records associated with PI data reported to the NRC for the period

January 2004 through December 2004. Reviewed records included: procedural

guidance on assessing opportunities for the three PIs; assessments of PI opportunities

during pre-designated control room simulator training sessions, the 2004 biennial

exercise, and mini-drills; revisions of the roster of personnel assigned to key ERO

positions; and results of periodic alert and notification system (ANS) operability tests.

The following PIs were reviewed:

Station Common

  • ERO Drill Participation
  • Drill and Exercise Performance

These reviews represented three inspection samples.

b. Findings

No findings of significance were identified.

.2 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the 4th

Quarter 2004 performance indicators for any obvious inconsistencies prior to its public

release in accordance with IMC 0608, Performance Indicator Program.

This review did not represent an independent inspection sample.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events and Mitigating Systems

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As a part of the various inspection procedures used to accomplish Sections 1 and 2 of

this report, the inspectors verified that problems and issues associated with inspection

samples were entered into the licensees corrective action program (CAP). Additionally,

the inspectors verified that the licensee identified issues at an appropriate threshold and

that problems were properly addressed for resolution. CAP attributes reviewed

included: complete and accurate identification of the problem; that the timeliness of

problem review was commensurate with safety; that evaluation and disposition of

35 Enclosure

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrences reviews were proper and

adequate; and that classification and prioritization of corrective actions were

commensurate with safety and sufficient to prevent recurrence of the issue.

These routine reviews concerning the identification and resolution of problems were an

integral part of the inspection samples documented elsewhere in this report. As such,

they did not represent any additional inspection samples.

b. Findings

Introduction

A finding of very low safety significance (Green) was identified by the inspectors during

review of the circumstances associated with a small fire in the 2B RHR corner room on

February 16, 2005, (Section 1R05.2). The inspectors determined that the licensee had,

during several opportunities, failed to take timely and effective corrective actions with

respect to ignition control for hot work. An associated Non-Cited Violation (NCV) of

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, was also identified.

Description

On February 16, 2005, at approximately 2:30 p.m., work was in progress in the 2B RHR

corner room to demolish a section of pipe that was slated for removal as part of an

approved permanent plant modification. The work involved cutting a vertical run of

20-inch diameter pipe into sections approximately 1 foot in length to facilitate ease of

removal. A single fire watch was assigned to observe in progress hot work activities.

Fire blanketing was placed in the area of the hot work, with additional material

surrounding the floor piping penetration to prevent sparks from falling through the

penetration. A fire blanket extended outward for approximately 8 feet from the hot work

area. During the course of the hot work activities, some of the sparks generated by the

cutting were thrown past the area covered by the fire blanket. These sparks fell through

open floor grating to the 694' elevation below.

At some point following lunch, cleaning material was staged on the 694' elevation below

the area where the hot work was in progress. When interviewed as part of the licensees

ACE, the fire watch stated that he was not aware of the introduction of this combustible

material to this area. Sparks that fell from the hot work above ignited a small Class A

fire in this material. A laborer in the area detected the fire and attempted to extinguish it

by stepping on the flames. When this action was not successful, a mop was used in an

attempt to smother the flames. When this action, too, proved ineffective, the laborer

notified the fire watch on the level above, who was able to extinguish the fire with a dry

chemical fire extinguisher. The control room was notified by personnel involved in the

2B RHR corner room fire.

On February 15, 2005, the day before the fire, a region-based NRC inspector touring the

Unit 2 feedwater heater bay identified deficiencies relating to ignition control at no less

than four work locations where hot work was in progress. In each case, the inspector

observed sparks from in progress hot work activities thrown out beyond the established

36 Enclosure

fire blanket protection areas. The inspector estimated that the fire blanket coverage, at

each site he observed, extended out only 6 to 8 feet from the work location. This level of

coverage was well short of the 35 feet required by plant procedures governing hot work

ignition control. Consequently, each hot fire activity observed by the inspector had hot

sparks passing through deck grating and falling to the levels below where the actual work

was taking place. The inspector discussed his observations with the personnel

conducting the work and their assigned fire watches at each job site, however, because

the personnel did not seem to be responsive, in his opinion, to his comments, the

inspector also discussed the observations with a duty radiation protection (RP) technician

in the heater bay and the on-duty outage Heater Bay Coordinator.

Following the fire in the 2B RHR corner room on February 16, 2005, inspectors reviewed

the licensees actions in response to the NRC observations regarding hot work ignition

controls in the Unit 2 heater bay that had occurred on the preceding day. In discussions

with senior licensee managers, the inspectors identified that communication of the NRC

observations from the Unit 2 heater bay on February 15, 2005, had not gone beyond the

Heater Bay Coordinator, nor had the licensee generated an Issue Report (IR) to enter the

observations as required by their corrective action program (CAP).

On February 22, 2005, six days following the 2B RHR corner room fire, the NRC

Resident Inspector and a region-based inspector were conducting a routine plant tour

that included the 2B RHR corner room. The inspectors were surprised to find that their

passage through the lower levels of the 2B RHR corner room and up the stairs was

blocked by a shower of sparks from hot work in progress from above. When personnel

conducting the hot work noticed the NRC inspectors, they ceased grinding operations

and allowed the inspectors to climb the stairs and exit the 2B RHR corner room. This hot

work activity was for the same modification project that had caused the fire six days

earlier.

The inspectors immediately brought their observations to the attention of licensee

management personnel in the Outage Control Center. The licensee ordered work in the

2B RHR corner room stopped and conducted a follow-up inspection of the work location.

Licensee managers determined that some of the fire blanket material added to the

2B RHR corner room job site following the fire had been removed as a part of planned

housekeeping and demobilization efforts. However, three fire watches were present in

the 2B RHR corner room during the hot work and the potential for another fire was small.

The licensee generated IR 304516 to document their actions and the inspectors

observations.

Analysis

In reviewing the 2B RHR corner room fire, the inspectors evaluated the licensee

corrective actions for NRC observations concerning hot work ignition control passed to

licensee personnel both before and after the February 16, 2005 fire. Given the lack of

effective communication of this issue within the licensees organization, and the fact that

an IR had not been written for the issues discussed with the licensee on February 15, the

inspectors determined that there was a performance deficiency associated with the

corrective actions taken by the licensee. Specifically, the licencees response to

inspector observations regarding hot work ignition controls in the Unit 2 heater bay on

37 Enclosure

February 15, 2005, was narrowly focused and not properly documented or

communicated within the licensees organization, resulting in the potential for adverse

consequences to plant equipment and personnel in the vicinity of hot work. The

inspectors concluded that had the licensees corrective action response to the

February 15, 2005, observations been more thorough and robust, it is conceivable that

the 2B RHR corner room fire may not have occurred the following day. Similarly, the

inspectors observations in the 2B RHR corner room six days after the fire indicated that

the licensees corrective actions for the actual event were largely ineffective, as the same

deficient conditions in fire blanket coverage that had permitted the fire to occur in the first

place continued to exist.

The objective of the Initiating Events Cornerstone of Reactor Safety is to limit the

likelihood of those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. In accordance with NRC Inspection

Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, the inspectors determined that the finding was of more than minor

significance in that it had a direct impact on this cornerstone objective. Specifically, one

of the key attributes associated with this cornerstone objective is protection against fires,

and the inspectors determined that the licensees failure to take timely and effective

corrective actions with respect to hot work ignition control deficiencies constituted a clear

threat to fire prevention at the facility.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, and conducted a

Phase 1 initial screening. Because the finding was associated with fire protection, this

was accomplished using IMC 0609, Appendix F, Attachment 1, Fire Protection SDP

Phase 1 Worksheet. As discussed in Section 1R05.2, the inspectors determined that

the finding was associated with the licensees ability to reach and maintain cold shutdown

conditions. As a result of the phase 1 screening, this finding was determined to be of very

low safety significance (Green) and within the licensees response band.

Enforcement

Criterion XVI of 10 CFR 50, Appendix B, states, in part, that: Measures shall be

established to assure that conditions adverse to quality, such as failures, malfunctions,

deficiencies, deviations, defective material and equipment, and nonconformances are

promptly identified and corrected. Contrary to this requirement, the licensee failed to

take adequate corrective actions for procedural noncompliances relating to hot work

ignition controls in the 2B RHR corner room. Specifically, on February 16, 2005, a fire

occurred in the 2B RHR corner room caused, in part, by procedural noncompliances

related to hot work ignition control. On February 22, 2005, the inspectors identified that

some of the same hot work ignition control procedural noncompliances were still present

in the 2B RHR corner room that could have adversely impacted plant equipment or

personnel.

Following various discussions with the inspectors on this issue, the licensee entered the

issue into their CAP as issue report (IR) 319064. This IR calls for a comprehensive

common cause analysis (CCA) by the licensee, which will examine the various fire

protection issues identified to determine whether or not a generic fire protection

38 Enclosure

programmatic weakness is present. Because the licensee has entered the issue into

their corrective action program and the finding is of very low safety significance (Green),

this violation of 10 CFR 50, Appendix B, Criterion XVI, is being treated as an NCV,

consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000374/2005002-08)

.2 Selected Issue Follow-up Inspection: Corrective Actions for Emergency Diesel

Generator (EDG) Reverse Power Trips

Introduction

The inspectors selected the licensees actions in response to recurring reverse power

trips of the stations EDGs for a more in-depth review. Since 1989, the licensee has

recorded 25 reverse power trips of EDGs at the station. The focus of this inspection was

a review of the licensees root cause report (RCR) for a reverse power trip of the 2A EDG

that occurred on December 7, 2004, which was the most recent event.

The inspectors review of this issue constituted a single inspection sample.

a. Effectiveness of Problem Identification

(1) Inspection Scope

The inspectors reviewed RCR 280218, Reverse Power Trip of the 2A Diesel Generator,

to verify that the licensee's identification of the problems were complete, accurate, and

timely, and that the consideration of extent-of-condition review, generic implications,

common cause, and previous occurrences were adequate.

(2) Issues

As discussed in Section (b) that follows, the licensees ability to identify the underlying

cause for this ongoing issue has, in general, not been the reason that the issue has been

drawn out for such a long period of time. The licensees investigations following both the

June 2, 1999, reverse power trip of the 1B EDG and the February 9, 2000, reverse power

trip of the 2B EDG both readily identified problems associated with the procedural

requirement plant operators faced to drive EDG load down to less than 200 kW before

opening the EDG output breaker. The actions of evaluating the issue and ensuring that

the corrective actions taken were effective are where the licensees corrective action

processes fell short.

b. Prioritization and Evaluation of Issues

(1) Inspection Scope

In reviewing RCR 280218, Reverse Power Trip of the 2A Diesel Generator, the

inspectors considered the licensees evaluation and disposition of performance issues,

evaluation and disposition of operability issues, and application of risk insights for

prioritization of issues.

39 Enclosure

(2) Findings

Introduction

A finding of very low safety significance (Green) was identified by the inspectors. The

inspectors determined that the licensee had failed during prior opportunities to fully

evaluate the nature of the problem leading to various EDG reverse power trips. The

most recent of these events were a reverse power trip of the 2B EDG on

August 18, 2004, for which no root cause was ever determined, and a reverse power trip

of the 2A EDG that occurred on December 7, 2004, which was the topic of the licensees

root cause report (RCR). An associated Non-Cited Violation (NCV) of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action, was also identified by the inspectors.

Description

On December 7, 2004, plant operators were performing a shutdown of the 2A EDG in

accordance with approved procedures. As part of this activity, the control room crew was

reducing 2A EDG load in preparation for opening the 2A EDG output breaker. Per the

procedure, load on the 2A EDG was reduced to approximately 200 kilowatts (kW) and

approximately 200 kilovolts-amperes-reactive (kVAR).

Just before the next step in the procedure, operators noted a caution statement that

identified the fact that the EDG can become unstable and trip on reverse power if allowed

to go below 200 kVAR for more than 1.5 seconds. The control room crew was aware of

this caution and discussed the next actions for reducing load below 200 kW/200 kVAR

and then opening the EDG output breaker. While performing this next step, the control

room crew received a 2A EDG Trouble Alarm. Operators in the field reported local

alarms for EDG undervoltage, reverse power, and an EDG lockout.

As a part of the RCR, the licensee conducted interviews with the operators that shutdown

the 2A EDG. These interviews revealed that the plant operators took approximately

3 seconds to complete the opening of the EDG output breaker actions, versus the

procedurally stated caution that called for less than 1.5 seconds. The license concluded

that the requirement for the operators to act in a mere 1.5 seconds constituted a human

performance challenge.

Since 1989, there have been 25 recorded reverse power trips of EDGs at LaSalle

Station. Among the more notable events reviewed by the inspectors were:

  • On June 2, 1999, the 1B EDG tripped on reverse power. An apparent cause

evaluation (ACE) was performed for this event and identified that at low load (less

than 200 kW), the EDG is in an inherently unstable position relative to the grid.

However, there were no corrective actions associated with this investigation. The

ACE was closed based on a statement by personnel that proper guidance existed

in the EDG operating procedure and that no additional action was required.

  • On February 9, 2000, the 2B EDG tripped on reverse power. An investigation

identified the root cause as an operator skill-based human performance error in

the untimely opening of the output breaker. The operators actions to reduce

40 Enclosure

load, then perform a self-check, then request a peer-check, all prior to opening

the EDG output breaker were determined to require too much time. The reverse

power trip occurred as a result. However, based on the evaluations of the

licensees engineering staff, the 200 kW/200 kVAR caution limits in the EDG

procedures were considered appropriate and no procedural revisions took place.

  • On August 18, 2004, the 2B EDG tripped on reverse power. The licensees

investigation focused almost primarily on the equipment failures subsequent to

the reverse power trip. The investigation plan did, however, call for a review of

the previous root cause for 2B EDG trip in 2000, and an assessment of the

adequacy of the corrective actions. In addition, a review of procedural and

human performance aspects of the EDG shutdown process were also required.

Despite this, however, there was no root cause identified associated with the

reverse power trip on August 18, and no corrective actions to specifically prevent

recurrence were instituted.

Analysis

In reviewing the EDG reverse power trips at the station leading up to the most recent

reverse power trip of the 2A EDG on December 7, 2004, the inspectors determined that

there was a performance deficiency associated with the corrective actions taken by the

licensee. Specifically, in response to the prior events, one as recently as

August 18, 2004, the licensees evaluation of the issue failed to generate any corrective

actions to address the inherently unstable position into which plant operators were being

placed by the procedural requirement to drive EDG load down below 200 kW before

opening the EDG output breaker. In one case as discussed above, in 1999, the

licensees evaluation actually did determine the cause of the reverse power trips to be

due to this procedural requirement and the naturally unstable position created by it.

However, no corrective actions were taken. While following the August 18, 2004,

reverse power trip of the 2B EDG actions were created to evaluate potentially changing

the EDG operating procedures to provide less limitations on tripping the output breaker,

these evaluations were not given a high enough priority for them to have been

completed by the time the December 7, 2004, reverse power trip occurred.

Subsequently, only after the 2A EDG reverse power trip on December 7, 2004, were the

evaluations completed in rapid order and procedure changes enacted.

The objective of the Mitigating Systems Cornerstone of Reactor Safety is to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). In accordance with NRC

Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix

B, Issue Screening, the inspectors determined that the finding was of more than minor

significance in that it had a direct impact on this cornerstone objective. Specifically, the

inspectors concluded that the licensees performance deficiency was responsible for the

reverse power trip of the 2A EDG on December 7, 2004, which caused the EDG to be

unavailable for an additional 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, and conducted a

Phase 1 characterization and initial screening. Because the finding involved the loss of

41 Enclosure

only one train of safety related equipment and the loss was for less than the Technical

Specification allowed outage time, the inspectors determined it to be of very low safety

significance (Green) and within the licensees response band.

Enforcement

Criterion XVI of 10 CFR 50, Appendix B, states, in part, that: Measures shall be

established to assure that conditions adverse to quality, such as failures, malfunctions,

deficiencies, deviations, defective material and equipment, and nonconformances are

promptly identified and corrected. Contrary to this requirement, the licensee failed to

promptly identify and correct procedural deficiencies associated with the unloading and

securing of the stations EDGs. These procedural deficiencies contributed to or directly

caused 25 EDG reverse power trips since 1989. Following a subsequent reverse power

trip of the 2A EDG on December 7, 2004, the licensee entered the issue into their CAP

as IR 280218. This issue report led to a RCR, with the following corrective actions

planned or completed: establishment of a less restrictive EDG load limit to allow

opening the EDG output breaker when load is less than approximately 500 kW;

additional training for licensed operators in the areas of EDG theory and operation and

the effects of reverse power conditions on diesel generators; and revision of simulator

modeling for EDGs to more accurately reflect actual plant performance for reverse

power trips. Because the licensee has entered the issue into their corrective action

program and the finding is of very low safety significance, this violation of 10 CFR 50,

Appendix B, Criterion XVI, is being treated as an NCV, consistent with Section VI.A of

the NRC Enforcement Policy. (NCV 05000374/2005002-09)

c. Effectiveness of Corrective Actions

(1) Inspection Scope

The inspectors reviewed multiple related CAP documents relating to the 25 EDG

reverse power trips on record since 1989 at the station. The intent of this review was to

determine if the CAP actions addressed generic implications, and to verify that

corrective actions were appropriately focused to correct the problem.

(2) Issues

The inspectors determined that the licensees corrective actions for EDG reverse power

events, that actually produced corrective actions, had only marginal impact in reducing

the number and frequency of the EDG reverse power trip occurrences. However, as

discussed in the section above, there were EDG reverse power trip events that did not

generate any corrective actions. For the actions taken in the aftermath of the reverse

power trip of the 2B EDG on August 18, 2004, the inspectors concluded that the

licensees planned actions had a good probability for success, but were not prioritized

for completion in time to prevent the subsequent December 7, 2004, reverse power trip

of the 2A EDG. These corrective actions included a Corporate Engineering review of

the reverse power trip settings for all LaSalle EDGs to determine if there was additional

margin in the setpoints, and a review to determine if the unloading sequence could be

changed to permit opening the EDG output breaker at higher loads.

42 Enclosure

4OA3 Event Follow-up (71153)

Cornerstones: Initiating Events and Mitigating Systems

.1 Single Failure Vulnerability of Safety Related 4,160 Vac Division 1 and Division 2

Protective Relay Circuitry (ENS 41366)

a. Inspection Scope

On January 27, 2005, Crystal River Unit 3 (CR-3) discovered a single failure that could

prevent both EDGs and both offsite power sources from supplying power to their

respective engineered safeguards (ES) buses. This was a condition reportable under

10 CFR 50.72 (b)(3)(ii)(B), for a plant being in an unanalyzed condition that significantly

degraded plant safety (ENS 41362).

Just prior to lunch on February 1, 2005, the LaSalle Station Electrical System

Engineering Supervisor was informed of the CR-3 event and provided a copy of

ENS 41362 by the LaSalle Station NRC Senior Resident Inspector. LaSalle Station

engineers reviewed the safety related bus protective relaying circuitry to determine if a

similar vulnerability existed. In the late afternoon of the following day, plant engineers

determined that a single failure vulnerability existed for LaSalle between the current

transformer (CT) circuits of the divisional safety related buses (e.g., 141Y to 142Y,

241Y to 242Y).

Upon notification of the discovery and subsequent entry into a 12-hour Technical

Specification Required Action potentially leading to the shutdown of both LaSalle units,

inspectors responded to the plant to monitor the licensees actions. The inspectors

observed plant parameters and status; evaluated the performance of plant systems and

licensee actions; and confirmed that the licensee properly reported the event as

required by 10 CFR 50.72. The inspectors determined that all systems responded as

intended, and that no human performance errors complicated the event response.

The inspectors response to and review of this event constituted a single inspection

sample.

b. Findings

No findings of significance were identified. One URI was identified.

At approximately 3:42 p.m. on February 2, 2005, plant operators entered a 12-hour

Technical Specification Required Action for unavailability of offsite and onsite power

systems. A licensee analysis of the issue determined that the CT circuits that supply the

overcurrent relay scheme for each divisional bus were connected to a common point

that supplies control room indication for the total station auxiliary transformer (SAT) Y

winding power (kW) and current (amperes). Further, licensee engineers determined

that an open circuit condition on any of the CT phases downstream of the common point

in the circuit would have resulted in an unbalanced current condition, which would have

initiated a trip of the associated SAT feed breakers for the applicable buses (e.g., 141Y

and 142Y, 241Y and 242Y). Specifically, the current unbalance would have actuated

43 Enclosure

the ground fault relays, causing the SAT feed breaker relays to lock out both divisions.

Following a trip of the bus feed breakers, the lockout relay for the respective bus would

have initiated a trip of the other bus breakers and prevented any closure of these

breakers. The ultimate result would have been a loss of all onsite and offsite power

sources to both 4160 Vac Division 1 and Division 2 safety related buses, because no

EDG or offsite power source would have been permitted to close onto the respective

Division 1 or Division 2 safety buses.

A temporary modification was developed and installed on each unit to isolate the

common metering circuitry between the Division 1 and Division 2 buses responsible for

the single point vulnerability. These modifications were installed and Technical

Specification Required Actions exited on Unit 1 in 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, 23 minutes, and on Unit 2 in

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, 48 minutes. All actions were monitored by the inspectors. The licensee

entered the issue into their corrective action program as IR 297076, and into their

corporate corrective action program as IR 299641.

The issue is presently considered unresolved pending a more detailed NRC review of

the licensees root cause report and LER for this issue. (URI 05000373/2005002-10;

05000374/2005002-10)

.2 Inadvertent Reactor Recirculation Flow Increase Results in Unit 1 Reactor Power

Excursion to 103.17 Percent

a. Inspection Scope

On February 23, 2005, the inspectors responded to the control room following

notification from the licensee that the Unit 1 licensed reactor power limit of

3489 megawatts thermal (MWth) had been exceeded by approximately 3.17 percent for

several minutes following an unplanned and unexpected increase in reactor recirculation

flow. The inspectors observed plant parameters and status; evaluated the performance

of plant systems and licensee actions; and confirmed that the licensee properly reported

the event as required by Section 2.F(a) of Facility Operating License No. NPF-11. The

inspectors further determined that no nuclear fuel thermal limits were violated, and that

the event was bounded by the events discussed in the UFSAR.

The inspectors response to and review of this event constituted a single inspection

sample.

b. Findings

No findings of significance were identified. One URI was identified.

On February 23, 2005, at approximately 11:41 a.m., Unit 1 exceeded License

Condition 2.C (1), which limits the maximum thermal power of the unit to 3489 MWth.

Unit 1 reached a peak transient power of approximately 3599.5 MWth, or

103.17 percent of the licensed limit, for about 8 minutes.

At approximately 11:46 a.m., the Unit 1 control room supervisor (CRS), a licensed senior

reactor operator (SRO) observed that Unit 1 power had increased from 1194 megawatts

44 Enclosure

electric (MWe) to 1223 MWe, and directed the on-watch nuclear station operator (NSO),

a licensed reactor operator (RO) to lower power to 95 percent. From approximately

11:47 a.m. to 11:48 a.m., the NSO attempted to reduce reactor power using the

LOWER pushbutton on the reactor recirculation (RR) ganged (i.e., master) flow control

station. After two attempts to lower power using the RR ganged flow control station, the

NSO did not believe that power was responding as it should have, and he placed the RR

flow controllers for each RR loops flow control valve (FCV) into manual and closed them

both to approximately 80 percent at 11:49 a.m. The FCVs responded, and reactor

power was reduced to about 3471 MWth, or approximately 99.5 percent. Plant power

was subsequently stabilized at about 95 percent while the licensee began an

investigation of the event.

At approximately 5:34 p.m., the licensee contacted the NRC Region III Director of

Reactor Projects via telephone, in accordance with the reporting conditions of

Section 2.F(a) of the Unit 1 license, to discuss the event. A follow on written report was

sent on March 9, 2005.

At the time of this writing, the event is still under investigation by the licensee. FCVs on

both LaSalle units (4 valves total) were being maintained in manual control pending the

outcome of the investigation. Initial troubleshooting of the RR ganged flow controller

had not revealed any abnormalities; however, further diagnostic testing at an off site lab

was planned. The licensees investigation into potential equipment problems associated

with the RR flow controllers was entered into their CAP as IR 304613. This investigation

was scheduled for completion in April 2005.

While the event did not trigger any control board annunciator alarms (none should have

been triggered based on a review of the event by the inspectors), the licensee

investigated the on-watch crews apparent lack of response to several low-level plant

process computer alarms that were actuated on increasing plant pressure and power.

This root cause investigation was being conducted within the licensees CAP under

IR 305612, and was expected to be completed in April 2005.

In addition to maintaining FCVs in manual control, corrective actions taken by the

licensee at this point also included changing several plant process computer alarms

from low-level alarms, which annunciate only briefly and then are automatically silenced,

to higher level alarms that require operator action to silence the alarm tones. Computer

alarms included in this change were MWth, MWe, and reactor pressure.

This issue is considered unresolved pending the inspectors receipt and review of the

licensees CAP investigations regarding any potential equipment malfunctions of the RR

flow control system, and the root cause investigation into the event

(URI 05000373/2005002-11)

45 Enclosure

4OA4 Cross-Cutting Aspects of Findings

Cornerstones: Initiating Events, Barrier Integrity and Occupational Radiation

Safety

Human Performance

Several of the findings and one of the licensee-identified violations described elsewhere

in this report had human performance deficiencies as their major causal elements.

  • A Green finding and associated NCV described in Section 1R05.2 involved the

failure of plant personnel conducting hot work to follow procedural requirements

for fire blanket protection in the vicinity of the work site. The improper fire

blanket coverage and lack of attentiveness on the part of the assigned fire watch

and other licensee personnel responsible for ensuring that ignition controls in the

vicinity of hot work were being properly applied resulted in a small Class A fire

in the 2B RHR corner room.

  • A Green finding and associated NCV described in Section 1R13.2 involved the

failure of maintenance planners and maintenance first line supervisors to have

properly identified the risk associated with an electrical meter replacement for

the 1A circulating water (CW) pump. The improper assessment of risk, in

combination with an inadvertent electrical short caused during the meter

replacement itself, resulted in a trip of the 1C CW pump, which was in service at

the time of the 1A CW pump maintenance window.

  • A finding and an associated NCV described in Section 2OS1.4(1) involved the

failure of personnel to follow established plant procedures and radiological

practices with respect to HRAs. An individual signed in on a general area RWP,

and subsequently entered a HRA to conduct a work in the Unit 2 drywell,

contrary to plant Technical Specifications.

  • A licensee-identified violation discussed in Section 4OA7 involved the failure of

maintenance contractor personnel to adequately follow written work instructions

regarding the removal of a U-bolt/pipe hanger for the Unit 2 reactor recirculation

(RR) system in the Unit 2 drywell. The wrong U-bolt was removed, contrary to

written job instructions in an approved work package; the error was subsequently

discovered by the licensee and corrected several days later. While the missing

U-bolt was determined to have been of no consequence for the established plant

conditions, if left uncorrected it would have been consequential for RR pipe

qualification during operation.

These human performance deficiencies were procedure compliance and adherence

related.

46 Enclosure

4OA5 Other

Cornerstone: Mitigating Systems

.1 (Discussed) Unresolved Item 05000373/2004005-04; 05000374/2004005-04: Standby

Liquid Control (SBLC) Boron Tank Volume/Concentration Measurements

One URI from a prior inspection report was discussed. This did not represent any

inspection samples.

On November 19, 2004, the Unit 2 main control room received a SBLC tank level alarm.

Plant operators concluded that the bubbler system that provides both tank level and

alarm indications was plugged and required cleaning. After the bubbler was cleaned,

however, the SBLC tank low level alarm still was actuated. A manual measurement

conducted by operations personnel using a T-square indicated a tank volume of

4717 gallons. Since the low level alarm setpoint was at 4700 gallons, the licensee

decided to add water to the SBLC tank to increase the volume of solution.

On November 23, 2004, operations and chemistry personnel added water to the Unit 2

SBLC tank and, as required by procedure, sampled the sodium pentaborate (boron

solution) concentration afterwards. Volume was measured using the T-square at

4767 gallons and boron solution concentration was determined to be 12.99 percent.

The minimum required Technical Specification boron solution concentration for this

volume is 12.97 percent, per Technical Specification Figure 3.1.7-1. Chemistry

technicians noted that there was little margin to the Technical Specification limit, and

plans were made to perform a sodium pentaborate addition to the tank during the

following week.

Just prior to midnight on November 25, 2004, Unit 2 operators were performing their

daily Technical Specification surveillance to verify SBLC tank level within the limits of

Technical Specification Figure 3.1.7-1. Measured tank volume was 4750 gallons. This

volume was below the required Figure 3.1.7-1 limit for the current boron solution

concentration of 12.99 percent. For a volume of 4750 gallons, Figure 3.1.7-1 specified

a minimum boron solution concentration of 13.02 percent. SBLC tank volume was

subsequently measured using the T-square, and 4762 gallons was the result. This

volume was exactly at the Technical Specification Figure 3.1.7-1 limit for a boron

solution concentration of 12.99 percent. However, questions by the on-watch operations

crew raised doubt as to the accuracy of the T-square volume measurement when it was

realized that an unauthorized operator aid in the form of a placard on the side of the

SBLC tank was being used to convert inches measured with the T-square to tank

volume in gallons. The conversion method on the placard was different than the

calculation used by chemistry technicians specified in their approved plant procedures.

Using the approved calculation from a chemistry procedure, operators recalculated the

SBLC tank volume from their T-square measurement and determined it to be 4757

gallons, which was once again below the Figure 3.1.7-1 limit. Both trains of SBLC were

declared inoperable and the applicable Technical Specification 8-hour shutdown time

clock entered. Chemistry technicians were called in to sample the SBLC boron solution

tank concentration, and obtained a measured value of 13.11 percent. When compared

47 Enclosure

with the T-square volume of 4757 gallons, this concentration value was within the limits

of Technical Specification Figure 3.1.7-1 and both trains of SBLC were declared

operable.

The licensee conducted an extent-of-condition review and determined that both Unit 1

and Unit 2 SBLC tanks had routinely been maintained with little margin to the

Figure 3.1.7-1 limits for volume and boron solution concentration. The licensee has

entered multiple issues associated with this event into their corrective action program

(CRs 276755, 277113, 277439, 281247, and 281238). These condition reports have

generated several corrective action program investigations, including a root cause report

(RCR 276755) and an apparent cause evaluation (ACE 277113).

As of the publication of this inspection report, the inspectors continue to review the

licensees CAP and associated engineering documents for this issue. Initial reviews by

the inspectors have yielded several questions regarding the licensees methods for

calculating SBLC tank volume. Over the course of the inspection period, the licensees

engineering staff have developed several similar methods for calculating SBLC tank

volume, each in an attempt to demonstrate that no past violations of Technical

Specification requirements had occurred with respect to measured sodium pentaborate

concentration and volume. The issue remains unresolved pending completion of the

inspectors reviews of the licensees calculations. (URI 05000373/2004005-04;

05000374/2004005-04)

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to the Site Vice President,

Ms. S. Landahl, and other members of licensee management on April 5, 2005. The

inspectors discussed the controls associated with a single proprietary engineering

evaluation from General Electric Company that was reviewed by the inspectors. No

other proprietary information was identified.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • A refuel outage baseline radiation protection inspection with the Site Vice

President, Ms. S. Landahl, and other members of the licensees staff on

February 18, 2005.

  • A refuel outage baseline engineering inspection of ISI with the Site Vice

President, Ms. S. Landahl, and other members of the licensees staff on

March 1, 2005.

Ms. S. Landahl, and other members of the licensees staff on March 25, 2005.

48 Enclosure

4OA7 Licensee-Identified Violations

Cornerstones: Barrier Integrity and Emergency Preparedness

The following violations of very low significance were identified by the licensee and are

violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

requires that activities affecting quality be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances,

and that activities be accomplished in accordance with these instructions,

procedures, or drawings. Contrary to these requirements, on February 16, 2005,

contractor maintenance personnel removed a U-bolt from a reactor recirculation

(RR) system pipe support in the Unit 2 drywell that was not the U-bolt specified

in their approved work instructions. The error was discovered on

February 19, 2005, by the licensee and corrected.

Inspectors determined that the issue was of more than minor significance

because if left uncorrected it would have become a more significant safety

concern. Specifically, while the missing U-bolt was determined to have been of

no consequence for the established plant conditions, if left uncorrected it would

have been consequential for RR piping qualification during operation. Because

there were no actual consequences associated with the issue, the inspectors

determined it to be of very low significance and within the licensees response

band. The licensee had entered the issue into their CAP as IR 303383.

  • Part 50.47 of 10 CFR, paragraph (b)(15), requires, in part, that radiological

emergency response training be provided to those who may be called on to

assist in an emergency. Table B-1 of the licensees standardized emergency

plan required that the minimum on-shift staffing included two radiation protection

(RP) personnel for in-plant protective actions. In September 2004, EP staff

based at another of the licensees Illinois nuclear stations identified that this

emergency plan commitment was met during weekends and holidays by one

on-shift RP technician and one on-shift chemistry technician. However, the

licensee also determined that chemistry technicians training had evolved such

that the training no longer met all requirements to provide in-plant protection

actions.

In early December 2004, the licensee completed an adequate root cause

investigation of this concerns impact at each of its Illinois nuclear stations.

Timely corrective actions included assigning two RP technicians on all back

shifts, initiating revision of the standardized ERO training procedure, and

initiating an assessment of ERO position qualifications in cases where some

ERO training was being performed by other departments. Because no actual

emergency events had occurred that required in-plant protective actions and the

49 Enclosure

licensees timely corrective actions included staffing a minimum of two RP

technicians on-shift, this violation is not more than of very low significance, and is

being dispositioned as an NCV.

ATTACHMENT: SUPPLEMENTAL INFORMATION

50 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Landahl, Site Vice President

D. Enright, Plant Manager

J. Bearden, Emergency Planning Coordinator

T. Connor, Maintenance Director

L. Coyle, Operations Director

D. Czufin, Site Engineering Director

C. Dieckmann, Training Manager

A. Ferko, Nuclear Oversight Manager

F. Gogliotti, System Engineering Manager

P. Holland, Regulatory Assurance - NRC Coordinator

B. Kapellas, Radiation Protection Manager

A. Kochis, ISI Coordinator

H. Madronero, Engineering Programs Manager

C. Minor, NDE Level III

W. Riffer, Emergency Planning Manager

T. Simpkin, Regulatory Assurance Manager

C. Wilson, Station Security Manager

Nuclear Regulatory Commission

B. Burgess, Chief, Reactor Projects Branch 2

1 Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000374/2005002-01 NCV Failure to Properly Implement Procedure Requirements for

Hot Work and Ignition Control Results in a Fire in the 2B

RHR Corner Room (Sections 1R05.2 and 4OA4)05000373/2005002-02 NCV Failure to Assess and Manage Risk Associated with the 1A

Circulating Water Pump Electrical Meter Replacement

Results in the Trip of the 1C Circulating Water Pump

(Sections 1R13.2 and 4OA4)05000373/2005002-03 NCV Failure to Assess and Manage Risk Associated with the

Cycling of the 1DG032 Manual Gate Valve Results in

Inoperable and Unavailable ECCS Components

(Section 1R13.3)05000374/2005002-04 NCV Failure to Incorporate Relevant Design Information into

Battery Charger Operating Procedure Results in DC Bus

Undervoltage Condition (Section 1R19.2)05000373/2005002-05 URI Unit 1 CSCS Pump Room Ventilation System Control

Cabinet Water Intrusion (Section 1R19.3)05000374/2005002-06 NCV Electrician Enters HRA (Drywell) When Signed On To

General Area RWP (Sections 2OS1.4(1) and 4OA4)05000374/2005002-07 URI Contractor Pipefitters Enter Condenser Pit HRA Without

Required RP Briefing (Section 2OS1.4(2))05000374/2005002-08 NCV Failure to Take Timely and Effective Corrective Action for

Hot Work Ignition Control Issues (Section 4OA2.1)05000374/2005002-09 NCV Failure to Take Timely and Effective Corrective Action for

Emergency Diesel Generator (EDG) Reverse Power Trips

Results in Additional EDG Inoperability and Unavailability

(Section 4OA2.2)05000373/2005002-10 URI Single Failure Vulnerability of Safety Related 4160 Vac

05000374/2005002-10 Division 1 and Division 2 Protective Relay Circuitry

(ENS 41366) (Section 4OA3.1)05000373/2005002-11 URI Unit 1 Reactor Power Excursion to 103.18 Percent

(Section 4OA3.2)

2 Attachment

Closed

05000374/2005002-01 NCV Failure to Properly Implement Procedure Requirements for

Hot Work and Ignition Control Results in a Fire in the 2B

RHR Corner Room (Sections 1R05.2 and 4OA4)05000373/2005002-02 NCV Failure to Assess and Manage Risk Associated with the 1A

Circulating Water Pump Electrical Meter Replacement

Results in the Trip of the 1C Circulating Water Pump

(Sections 1R13.2 and 4OA4)05000373/2005002-03 NCV Failure to Assess and Manage Risk Associated with the

Cycling of the 1DG032 Manual Gate Valve Results in

Inoperable and Unavailable ECCS Components

(Section 1R13.3)05000374/2005002-04 NCV Failure to Incorporate Relevant Design Information into

Battery Charger Operating Procedure Results in DC Bus

Undervoltage Condition (Section 1R19.2)05000374/2005002-06 NCV Electrician Enters HRA (Drywell) When Signed On To

General Area RWP (Sections 2OS1.4(1) and 4OA4)05000374/2005002-08 NCV Failure to Take Timely and Effective Corrective Action for

Hot Work Ignition Control Issues (Section 4OA2.1)05000374/2005002-09 NCV Failure to Take Timely and Effective Corrective Action for

Emergency Diesel Generator (EDG) Reverse Power Trips

Results in Additional EDG Inoperability and Unavailability

(Section 4OA2.2)

Discussed

05000373/2004005-04 URI SBLC Tank Level and Boron Solution Concentration

05000374/2004005-04 Measurement Issues (Section 4OA5)

3 Attachment

LIST OF DOCUMENTS REVIEWED

1R01 Adverse Weather Protection

Procedures:

- LOA-TORN-001; High Winds/ Tornado; Revision 4

- OP-AA-108-111; Adverse Condition Monitoring and Contingency Planing; Revision 1

- OP-AA-108-111-1001; Severe Weather Guidelines; Revision 1

1R04 Equipment Alignment

Issue Reports:

- 141023; Apparent Failure of Div. II CSCS Room Temperature Controller; 1/24/2003

- 154515; Div 3 CSCS Pump Room Fans Did Not Secure Following EDG Run;

4/17/2003

- 236085; Errors in Analysis Affecting Max Anticipated CSCS Rm Temp; 7/14/2004

- 266846; Love Controller Replacement; 10/25/2004

- 283233; 1TIC-VY017 Reads Low; 12/16/2004

- 287334; Temperature Controller is Erratic, Not Giving True Readings; 1/3/2005

- 287351; Conduit Has a Leak Up at the Roofline - Causing 1TIC-VY024; 1/04/2005

- 287694; Ref. Issue Report #287351 WO # 769178-01; 1/4/2005

- 287742; Water in Local Control Panel 1PL73J; 1/5/2005

- 287987; FIN Follow-Up from Troubleshooting 1TIC-VY024 Erratic Ind; 1/5/2005

- 301768; Water Identified in Junction Boxes Feeding 1PL73J; 2/15/2005

- 302014; (NRC Identified) Discrepancy Between OPS Lesson Plan and UFSAR;

2/16/2005

- 307568; 2E12-F353C Div 2 CSCS RHR Root Valve Leaks By Excessively; 3/2/2005

- 308000; Install Drain Hole in J-Box for Damper Motor 0TZ-VD00; 3/3/2005

Operability Evaluation:

- OE 96155; Clarification of 1(2)VY05C Operability to Support DG Operations;

11/23/1996

Procedures:

- LOP-FC-02E; Unit 2 Fuel Pool Cooling Electrical Checklist; Revision 3

- LOP-FC-02M; Unit 2 Fuel Pool Cooling Mechanical Checklist; Revision 6

- LOP-DG-06E; Unit 1 A DG Cooling System Electrical Checklist; Revision 5

- LOP-DG-06M; Unit 1 A Diesel Generator Cooling System Mechanical Checklist;

Revision 12

- LOP-DG-07E; Unit 1 B Diesel Generator Cooling System Electrical Checklist;

Revision 5

- LOP-DG-07M; Unit 1 B Diesel Generator Cooling System Mechanical Checklist;

Revision 11

- LOP-DG-08E; Unit 0 Diesel Generator Cooling System Electrical Checklist; Revision 8

- LOP-DG-08M; Unit 0 Diesel Generator Cooling System Mechanical Checklist;

Revision 18

- LOP-DG-09E; Unit 2 A Diesel Generator Cooling System Electrical Checklist;

Revision 4

4 Attachment

- LOP-DG-09M; Unit 2 A Diesel Generator Cooling System Mechanical Checklist;

Revision 7

- LOP-DG-10E; Unit 2 B Diesel Generator Cooling System Electrical Checklist;

Revision 4

- LOP-DG-10M; Unit 2 B Diesel Generator Cooling System Mechanical Checklist;

Revision 9

- LOP-RH-04E; Unit 2 Residual Heat Removal System Electrical Checklist; Revision 14

- LOP-RH-2BM; Unit 2 B Residual Heat Removal System Mechanical Checklist;

Revision 0

- LOP-RH-2CM; Unit 2 C Residual Heat Removal System Mechanical Checklist;

Revision 0

- LOP-RHWS-1AM; Unit 1 A RHR Service Water System Mechanical Checklist;

Revision 1

- LOP-RHWS-1BM; Unit 1 B RHR Service Water System Mechanical Checklist;

Revision 3

- LOP-RHWS-2AM; Unit 2 A RHR Service Water System Mechanical Checklist;

Revision 1

- LOP-RHWS-2BM; Unit 2 B RHR Service Water System Mechanical Checklist;

Revision 2

- LOP-VD-01E; Unit 1 A Diesel Ventilation System Electrical Checklist; Revision 7

- LOP-VD-02E; Unit 2 A Diesel Ventilation Electrical Checklist; Revision 6

- LOP-VD-03E; Unit 1 Diesel Vent (VD) Electrical Checklist; Revision 5

- LOP-VD-04E; Unit 2 B Diesel Generator Ventilation Electrical Checklist; Revision 5

- MA-MW-726-022; Electrical Cable Termination and Inspection; Revision 0

Work Orders:

- 536202; Apparent Failure of Controller 1TIC-VY024; 1/24/2003

- 769178; Apparent Failure of Controller 1TIC-VY024; 1/04/2005

- 770108; Water in Local Control Panel 1PL73J; 1/12/2005

- 743426; Install/Remove Temp. Level Indication for LLP-2004-007; 3/6/2005

Updated Final Safety Analysis Report; Revision 15:

- Chapter 9, Auxiliary Systems

- Chapter 6, Section 6.3.2.2.4 - LPCI subsystem

1R05 Fire Protection

Procedures:

- CC-AA-201; Plant Barrier Control Program; Revision 5

- OP-MW-201-004; Fire Prevention for Hot Work; Revision 0

- OP-MW-201-007; Fire Protection System Impairment Control; Revision 3

- OP-AA-201-001; Fire Marshal Tours; Revision 2

- OP-AA-201-008; Pre-Fire Plans; Revision 1

- OP-AA-201-009; Control of Transient Combustible Material; Revision 4

- LS-AA-128; Regulatory Review of Proposed Changes to the Approved Fire Protection

Program; Revision 0

- LOS-FP-D1; Fire Protection Door Daily Surveillance; Revision 2

5 Attachment

Issue Reports:

- 302209; Small Fire in Unit 2 Reactor Building - 694 Elevation; 2/16/2005

- 302447; Near Miss - Fire Extinguisher Malfunction; 2/16/2005

- 304516; (NRC Identified) RHR Keep Fill Modification Fire Protection Awareness;

2/23/2005

Control Room Time Clock Tracking Sheet for Fire Watch Active Patrols; 2/9/2005 -

2/11/2005

Fire Protection Impairment Permits:

- 2-04-189-TRM

- 2-04-146-TRM

- 2-02-056-TRM

Plant Barrier Impairment Permits:

- DR-500.00r5

- 2B DG Access Hatch.00r5

- FP U2 DG Corridor L-21.01r5

- FP U2 DG Corridor L-21.00r5

- DR-503.00r5

Fire Watch Inspection Logs; 2/9/2005 - 2/11/2005

Pre-Fire Plans for Fire Zones 4F1, 4E1, and 4E3

La Salle County Nuclear Station Fire Protection Report Vol. 1:

- H.3.4.12 : Unit 1 Auxiliary Equipment Room - Fire Zone 4E1

- H.3.4.14 : Unit 1 Division 2 Essential Switchgear Room - Fire Zone 4E3

- H.3.4.16 : Unit 1 Division 1 Essential Switchgear Room - Fire Zone 4F1

Technical Requirements Manual :

- Vol. 4, Section 3.3p; Fire Detection Instrumentation

Updated Final Safety Analysis Report:

- Fig. 9.5-1 Fire Protection System; Sheets 17 and 22

1R08 Inservice Inspection Activities

Issue Reports:

- 303540; (NRC-Identified) Extent of Condition Review for IR 142187; 2/20/2005

- 142187; Pipe Support FW02-2875C Found Damaged; 1/31/2003

- 195554; Rejectable Indication on VT-3 Examination of FW02-1158X; 1/15/2004

- 195712; Snubber NB13-1001-S Failed on High Drag; 1/15/2004

- 195988; UT Indications in LP and HP Piping Inside the Reactor; 1/17/2004

- 196074; Additional UT Indications in LPCS Piping Inside the Reactor; 1/18/2004

- 212765; Error in LPCS Flaw Sizing Calculation; 4/1/2004

EC 341014; Evaluation of Bent FW Pipe Clamp M09-FW02-2875C; Revision 0

6 Attachment

Operating Experience:

- NRC IN 2004-08: Reactor Coolant Pressure Boundary Leakage Attributable to

Propagation of Cracking in Reactor Vessel Nozzle Welds

- G.E. RICSIL 082: Core Spray Nozzle to Safe End Weld Leak; AIR No.

373-458-97-00082.00

Nondestructive Examinations:

- Magnetic Particle Examination Data Sheet Report No. 2R10-109; Component

RH40-2877X; 2/28/2005

- UT Examination Summary Sheet No: 2R09-010, WO No: 430431; Weld

ID: LCS-2-BH; 2/3/2003

- UT Examination Summary Sheet No: 2R09-015, WO No: 430431; Weld

ID: LCS-2-N4D; 1/30/2003

- UT Examination Summary Report No. 2R10-010; Component ID: LCS-2-N2B,

Recirculation Inlet Nozzle; 2/28/2005

Work Order:

- 96094687; Replace 2E12-F325B/326B Double Block Valves with Two Single Valves;

9/24/2002

Prints and Drawings:

- ISI-RH-2009; Inservice Inspection Isometric, Residual Heat Removal System, Unit 2;

Revision B

- M09-RH40-2877X, Sheet 1; Pipe Support, Residual Heat Removal System, Unit 2;

Revision F

Procedures:

- GE-UT-705; Procedure for the Examination of Reactor Pressure Nozzle Inner Radius

and Nozzle to Vessel Welds with the GERIS 2000 OD in Accordance with Appendix VIII;

Version No. 4

- MT-EXLN-102V0; Procedure for Magnetic Particle Examination Using AC Yoke, Dry

Powder, or Wet Visible; Revision 2

1R11 Licensed Operator Requalification Program

Licensed Operator Requalification Scenario Guide:

- ESG 64; Revision 0

TQ-AA-106; Licensed Operator Requal Training Program; Revision 6

1R12 Maintenance Effectiveness

Sodium Pentaborate Sample Results for Unit 1 and Unit 2 SBLC Storage Tanks;

June 2004 - December 2004

Engineering Changes:

- 338147; SBLC Tank Level; Revision 0

- 352973; SBLC Tank Level Tee Square; Revision 0

7 Attachment

- 353491; Engineering Determination of Volume Via Gallons per Inch of Height in the

Units 1&2 SBLC Storage Tank (EPN) 1(2) C41-A001; Revisions 0 & 1

Procedures:

- CC-AA-103-2001; Set point Change Control; Revision 2

- CY-AA-130-200; Quality Control; Revision 6

- LCP-110-9; Determination of High Range Boron (Sodium Pentaborate); Revision 22

- LCP-310-09; Standby Liquid Control Tank Sampling; Revision 8

- LOP-SC-05; Changing Sodium Pentaborate Concentration in Standby Liquid Control

(SBLC) Solution Tank; Revision 18

Information Notice 86-48; Inadequate Testing of Boron Solution Concentration in the

Standby Liquid Control System; 6/13/1986

Issue Reports:

- 083484; SLC System Operability During Air Tank Sparging; 11/20/2001

- 276560; No Procedure Guidance for Sodium Pentaborate Addition Calculation;

11/24/2004

- 276755; SBLC Concentration Limits Outside TA limits; 11/25/2004

- 276839; NRC Identified Point of Discovery for SBLC Inop; 11/26/2004

- 277113; Unauthorized Operator Aid Found on Standby Liquid Control (SBLC) Solution

Tank; 11/26/2004

- 277439; NRC Identified Issue with Use of T Square for SBLC Tank Level; 11/29/2004

- 281238; Standby Liquid Control Solution Tank Volume Determination; 12/10/2004

- 281244; UFSAR Sections Not Up to Date for Standby Liquid Control to Include

Low-Level Alarm and Technical Specification 3.1.7 (Standby Liquid Control Figures);

12/10/2004

- 281247; Chemistry Procedures Not Up to Date for Technical Specification 3.1.7

(Standby Liquid Control Figures); 12/10/2004

- 283765; Sodium Pentaborate Concentration Outside Optimum Range; 12/17/2004

- 296489; SBLC Volume Resample Not Routed for Ops Review; 2/1/2005

1R13 Maintenance Risk Assessments and Emergent Work Control

Engineering Change:

- EC 353657; Isolation of Metering to Common 141Y/142Y and 241Y/242Y Safety

Related Buses; Revision 0

Issue Reports:

- 141023; Apparent Failure of Div. II CSCS Room Temperature Controller; 1/24/2003

- 154515; Div 3 CSCS Pump Room Fans Did Not Secure Following EDG Run;

4/17/2003

- 236085; Errors in Analysis Affecting Max Anticipated CSCS Rm Temp; 7/14/2004

- 266846; Love Controller Replacement; 10/25/2004

- 283104; HPCS DG Room Pressurized During DG Start; 12/16/2004

- 283233; 1TIC-VY017 Reads Low; 12/16/2004

- 286665; Stem to Disc Separation on 1DG032; 12/30/2004

- 287334; Temperature Controller is Erratic, Not Giving True Readings; 1/3/2005

- 287351; Conduit Has a Leak Up at the Roofline - Causing 1TIC-VY024; 1/4/2005

8 Attachment

- 287541; 1C Circ Water Pump Tripped; 1/4/2005

- 287694; Ref. Issue Report #287351 WO # 769178-01; 1/4/2005

- 287742; Water in Local Control Panel 1PL73J; 1/5/2005

- 287987; FIN Follow-Up from Troubleshooting 1TIC-VY024 Erratic Ind; 1/5/2005

- 290618; CSCS Valve PMs Critical Prior to L1R11 Need Deferral; 1/13/2005

- 293279; U-1 DWFD FUR 1UR-RF002 Pen 1 Ind > 1 GPM Above Alternate; 1/22/2005

- 297076; Vulnerability of Division 1 & 2 Protective Relay Circuitry; 2/4/2005

- 299188; Lack of Minimum 6-inch Physical Separation in Division 1 & 2 CTs; 2/8/2005

- 303991; DWFD Sump Flow Indication Pegged Upscale; 2/22/2005

- 304111; Possible Failed Instrument (Level Switch) 1C11-N013B; 2/22/2005

- 304853; Troubleshooting Results for Unit 1 SDV 1/2 Scram; 2/24/2005

Procedures:

- LOA-CW-101; Unit 1 Circulating Water System Abnormal; Revision 11

- LOR-1PM03-J-B406; Circulating Water Pump 1CW01P A/B/C Auto Trip; Revision 3

- LOP-CW-03; Startup and Operation of the Circulating Water System; Revision 26

- LOP-CW-09; Circulating Water System Ice Melting; Revision 13

- LOR-1PM13J-A301; Drywell Floor Drain Sump Level Hi, Hi Hi, or Pump Start Failure;

Revision 4

- LIS-PC-121; Unit 1 Drywell Floor Drain Sump Discharge Flow Calibration; Revision 1

- LOS-AA-S101; Unit 1 Shiftly Surveillence; Revision 28

- LOS-DG-Q1; 0 Diesel Generator Auxiliaries Inservice Test; Revision 38

- LSCS P.G. No. 130; Equipment to Be Worked Around the Clock; Revision 0

Corporate RCR 299641; Single Failure Vulnerability of Safety Related Division 1 & 2

Protective Relay Circuitry Root Cause Analysis; 3/8/2005

Operability Evaluation:

- OE 05-001; Minimum 6-inch Physical Separation in Division 1 & 2 CTs; Revision 0

Work Order:

- 545611-01; IM Contingency for DWFD Loop Instruments; 2/22/2005

1R14 Operator Performance During Non-Routine Plant Evolutions and Events

Issue Reports:

- 297076; Vulnerability of Division 1 & 2 Protective Relay Circuitry; 2/4/2005

- 298353; 2B-33 F067B Steam Coming From Packing Around Stem; 2/7/2005

- 298462; 2B RR PP Discharge Valve Would Not Stroke Closed; 2/7/2005

- 299188; Lack of Minimum 6-inch Physical Separation in Division 1 & 2 CTs; 2/8/2005

- 300143; 2B33-F067B Failed to Close; 2/9/2005

- 305823; SDC Not in Operation; 2/26/2005

Corporate RCR 299641; Single Failure Vulnerability of Safety Related Division 1 & 2

Protective Relay Circuitry Root Cause Analysis; 3/8/2005

9 Attachment

Engineering Change:

- EC 353657; Isolation of Metering to Common 141Y/142Y and 241Y/242Y Safety

Related Buses; Revision 0

Unit 2 Operator Logs; 2/7/2005

Operability Evaluation:

- OE 05-001; Minimum 6-inch Physical Separation in Division 1 & 2 CTs; Revision 0

Procedures:

- LOA-CW-101; Unit 1 Circulating Water System Abnormal; Revision 11

- LOP-CW-03; Startup and Operation of the Circulating Water System; Revision 26

- LOP-CW-09; Circulating Water System Ice Melting; Revision 13

- LOP-RR-09; Reactor Recirc Pump Shutdown; Revision 21

- LOR-1PM03-J-B406; Circulating Water Pump 1CW01P A/B/C Auto Trip; Revision 3

1R15 Operability Evaluations

Issue Reports:

- 288363; Results of Lisega Snubber Test Results; 1/6/2005

- 287334; Temperature Controller is Erratic, Not Giving True Readings; 1/3/2005

- 287742; Water in Local Control Panel 1PL73J; 1/5/2005

- 287987; FIN Follow-Up from Troubleshooting 1TIC-VY024 Erratic Ind; 1/5/2005

- 301768; Water Identified in Junction Boxes Feeding 1PL73J; 2/15/2005

Engineering Evaluation:

- Report No. R93-007S; Engineering Evaluation of NRC IE Notice 89-63 for LaSalle

County, Dresden, and Quad Cities Stations All Units; Revision 0

NRC Information Notice:

- 89-63; Possible Submergence of Electrical Circuits Located Above the Flood Level

Because of Water Intrusion and Lack of Drainage; 9/5/1989

Operability Evaluations:

- OE 04-008; Lisega Snubbers; Revision 3

- OE 04-007; Degraded Fans on Transformer 236Y; Revision 1

Engineering Changes:

- 332208; Evaluation of Appendix J Testing Requirements on the Standby Liquid Control

System; Revision 0

- 354196; L2R10 Lost Parts Evaluation for Items That Could Reach the Reactor Vessel;

Revision 0

- 354344; L2R10 Refuel Outage Nuclear Fuels Lost Parts Evaluation; Revision 0

1R16 Operator Workarounds

Issue Reports:

- 311171; Multiple TS 3.6.4.1 Entries Due to U2 VR System Operation; 3/10/2005

- 311529; Unexpected Change in Reactor Building Differential Pressure; 3/11/2005

10 Attachment

- 311672; Unit 1 VR Exh Flow Oscillates with Constant Signal to Damper; 3/11/2005

- 311795; L2R10 LL : VR System and RB DP Oscillations; 3/12/2005

- 312176; Sudden Increase (More Negative) in RB DP; 3/13/2005

Engineering Change:

- 352527; MR90 Review to Maintain VR DP During Troubleshooting of VR;

Revisions 0 & 1

Procedures:

- CC-AA-102; Design Input and Configuration Change Impact Screening; Revision 9

- LOP-VR-01; Reactor Building Ventiallation System Startup and Operation; Revision 31

- LS-AA-104; Exelon 50.59 Review Process; Revision 4

Work Order:

- 731302-11; Replace/ Calibrate U-2 VR Supply Instruments; 3/7/2005

1R17 Permanent Plant Modifications

Calculations:

- GEN 01-002; Generic Lead Shielding Blanket & Support Detail Qualification;

Revision 0

- L-002804; Installation of Permanent Lead Shielding Blankets Inside Unit 2 Drywell;

Revision 1

Engineering Changes:

- 342975; Unit 2 Residual Heat Removal Service Water Keep Fill Elimination; Revision 4

- 343542; Replace Carbon Steel CSCS Valves with Stainless Steel Valves ; Revision 2

- 332685; Install Permanent Lead Shielding in Unit 2 Drywell; Revision 1

- 353949; Alternate Detail for the Steam Dryer Lifting Lug Upper Support; Revision 0

Procedure:

- CC-AA-102; Design Input & Configuration Change Impact Screening; Revision 9

1R19 Post-Maintenance Testing

Issue Reports:

- 292281; Div 1 125 VDC Transient During Charger Swap; 1/19/2005

- 293279; U-1 DWFD FUR 1UR-RF002 Pen 1 Ind > 1 GPM Above Alternate; 1/22/2005

- 293389; LOP-DC-01 Revision; 1/23/2005

- 295228; Hi Voltage During U2 Division 1 Charger Swap; 1/28/2005

- 297795; Difference in 125VDC Divisional Charger Metering; 2/4/2005

- 298477; A RPS Half Scram During LOS-RP-W1 - IN Disc Rupture; 7/7/2005

- 298631; IN Rupture Disk Blew on Loss of A RPS; 2/7/2005

- 317267; NRC Identifies Water Dripping from Weep Hole in VY JB; 3/25/2005

Engineering Changes:

- 340584; Evaluate Acceptability of Energizing Both 125 VDC Division 1 or 2 Battery

Chargers Simultaneously to Support Battery Charger Testing; Revision 0

- 346528; Provide Guidance for the Use of Intermittent Loads; Revision 0

11 Attachment

Engineering Change Request:

- 368281; Battery Charger Troubleshooting as an Intermittent Load; 1/21/2005

Procedures:

- CC-AA-308; Control and Tracking of Electrical Load Changes; Revision 4

- LES-DC-103A; Division I Battery Charger Capacity Test; Revision 11

- LIS-PC-121; Unit 1 Drywell Floor Drain Sump Discharge Flow Calibration; Revision 1

- LOP-DC-01; Battery Charger Startup and Shutdown; Revisions 25 & 26

- LOR-1PM13J-A301; Drywell Floor Drain Sump Level Hi, Hi Hi, or Pump Start Failure;

Revision 4

- LOS-AA-S101; Unit 1 Shiftly Surveillence; Revision 28

Work Orders:

- 545611-01; IM Contingency for DWFD Loop Instruments; 2/22/2005

- 734945-02; Potentially Degraded RPIS Circuit Cards due to Diodes; 1/26/2005

- 774091-02; EM Replace 2A RPS Voltage Regulator; 2/15/2005

1R20 Outage Activities

Issue Reports:

- 298740; SRM D Detector Stuck Withdrawn; 2/8/2005

- 298741; IRM D Stuck Inserted; 2/8/2005

- 298322; Received B Half Scram Due to H IRM Hi=Hi; 2/7/2005

- 299196; Operator Injury During U-2 Div 3 CSCS Work; 2/8/2005

- 300701; Wrong Unit Error; 2/12/2005

- 307158; Lead Pump on the Div 2 CSCS Sump Found in the Stop Pos; 3/2/2005

- 307578; 2E12-F050A Fails High Pressure Water Leak Test; 3/2/2005

- 307589; L2R10 LL: 2B21-F032A Repair After Unacceptable LLRT Result; 3/2/2005

- 311369; Crud Burst Resulted in Increased Dose Rates on Refuel Floor; 3/11/2005

- 314018; Low Bearing Oil Pressure, Suspect Leak/ Hole in Pipe; 3/17/2005

Procedures:

- LGP-2-1; Normal Unit Shutdown; Revision 65

- LGP-1-1; Normal Unit Startup; Revision 73

- LGP1-S1; Master Startup Checklist; Revision 55

- LOA-RR-201; Unit 2 Recirculation Pump System Abnormal; Revision 13

- LIS-RR-205A; Unit 2 Recirculation Pump Trip System A Breaker Arc Suppression

Response Time Testing; Revision 7

- LES-RP-101; RPS MG Set Startup and Operation; Revision 9

- LOP-DW-02; Drywell Entry and Inspection (Shutdown, Startup or Operation);

Revision 13

- LOP-DW-01; Drywell Close Out (After Outage); Revision 38

- OP-AA-108-108-1001; Drywell/Containment Closeout; Revision 0

- LOS-DG-209; Unit 2 Integrated Division I Response Time Surveillance; Revision 1A

- LOS-DG-210; Unit 2 Integrated Division II Response Time Surveillance; Revision 1

- LOS-DG-211; Unit 2 Integrated Division III Response Time Surveillance; Revision 0

12 Attachment

L2R10 Shutdown Safety Management Program

10 CFR 50.59 Screenings and Evaluations:

- L05-73; LaSalle Unit 2 Cycle 11 Reload Package; Revision 0

- L05-74; LaSalle Unit 1 and 2 GE-14 Fuel Implementation; Revision 0

1R22 Surveillance Testing

Engineering Changes:

- 338147; SBLC Tank Level; Revision 0

- 352973; SBLC Tank Level Tee Square; Revision 0

- 353491; Engineering Determination of Volume Via Gallons per Inch of Height in the

Units 1&2 SBLC Storage Tank (EPN) 1(2) C41-A001; Revisions 0 & 1

Engineering Change Request:

- 352281; Provide Information in Eng Change or Equivalent on Delta Between V-Notch

and the Totalizer; 10/09/2001

Information Notice 86-48; Inadequate Testing of Boron Solution Concentration in the

Standby Liquid Control System; 6/13/1986

Issue Reports:

- 083484; SLC System Operability During Air Tank Sparging; 11/20/2001

- 276560; No Procedure Guidance for Sodium Pentaborate Addition Calculation;

11/24/2004

- 276755; SBLC Concentration Limits Outside TA limits; 11/25/2004

- 276839; NRC Identified Point of Discovery for SBLC Inop; 11/26/2004

- 277113; Unauthorized Operator Aid Found on Standby Liquid Control (SBLC) Solution

Tank; 11/26/2004

- 277439; NRC Identified Issue with Use of T Square for SBLC Tank Level; 11/29/2004

- 281238; Standby Liquid Control Solution Tank Volume Determination; 12/10/2004

- 281244; UFSAR Sections Not Up to Date for Standby Liquid Control to Include

Low-Level Alarm and Technical Specification 3.1.7 (Standby Liquid Control Figures);

12/10/2004

- 281247; Chemistry Procedures Not Up to Date for Technical Specification 3.1.7

(Standby Liquid Control Figures); 12/10/2004

- 283765; Sodium Pentaborate Concentration Outside Optimum Range; 12/17/2004

- 287208; DWFDS Fillup Rate High; 1/03/2005

- 290678; Noble Gas Channel Alarm Will Not Clear; 1/14/2005

- 291499; DWFDS Fillup Rate Reading 1.1 GPM; 1/18/2005

- 293279; U-1 DWFD FUR 1UR-RF002 Pen 1 Ind > 1 GPM Above Alternate;1/22/2005

- 296489; SBLC Volume Resample Not Routed for Ops Review; 2/1/2005

- 298625; MSL Drain Valves 2B21-F019/F016 Failed LLRT in LTS 100-4; 2/7/2005

- 301672; Feedwater Check Valve 2B21-F032A Failed As-Found LLRT; 2/14/2005

- 304012; Anomolies Noted During LES-SC-201 Surveillance; 2/22/2005

- 304021; Problems Encountered During the Performance of LES-SC-201; 2/22/2005

- 307210; SBLC Circuit Continuity Loss Fuse Found Blown; 3/2/2005

- 307242; Opposite Division Fuse Blown Following LOS-SC-R1; 3/2/2005

- 309172; L2R10 LL: SBLC Issues During L2R10; 3/6/2005

13 Attachment

Procedures:

- CC-AA-103-2001; Set point Change Control; Revision 2

- CY-AA-130-200; Quality Control; Revision 6

- LCP-110-9; Determination of High Range Boron (Sodium Pentaborate); Revision 22

- LCP-310-09; Standby Liquid Control Tank Sampling; Revision 8

- LOP-SC-05; Changing Sodium Pentaborate Concentration in Standby Liquid Control

(SBLC) Solution Tank; Revision 18

- LOS-DG-209; Unit 2 Integrated Division I Response Time Surveillance; Revision 1

- LOS-DG-210; Unit 2 Integrated Division II Response Time Surveillance; Revision 1

- LOS-DG-211; Unit 2 Integrated Division III ECCS Response Time Surveillance;

Revision 0

- LOS-SC-R5; SBLC Pump Full Flow/Pressure Test; Revision 2

- LOS-SC-Q1; SBLC Pump Operability/Inservice Test and Explosive Valve Continuity

Check; Revision 21

- LMP-SC-01; SBLC Explosive Valve Maintenance; Revision 14

- LTS-100-3; Main Steam Isolation Valve Local Leak Rate Test; Revision 17

- LTS-100-10; Inboard/Outboard Feedwater Check Valves and Outboard Stop Valves

Local Leak Rate Test; Revision 17

- LTS-300-5; Primary Containment Leak Rate Testing Program; Revision 35

- LTS-900-6; RHR Shutdown Cooling Return Pressure Isolation Valve Water Leak Rate

Test; Revision 19

- LTS-900-12; RHR Primary Isolation Valve Water Leak Rate Test; Revision 19

Sodium Pentaborate Sample Results for Unit 1 and Unit 2 SBLC Storage Tanks;

June 2004 - December 2004

Work Orders:

- 606950-01; OP Integrated Divisional Response Time Test IAW LOS-DG-210;

2/25/2005

- 607327-01; LOS-DG-209 Integrated Div 1 ECCS Response Time Pumps and Diesel;

2/23/2005

- 608104-01; LOS-DG-211 Integrated Div 3 ECCS Response Time Pumps and Diesel;

2/20/2005

- 759299-01; OP LOS-SC-Q1 2A SBLC Pump Quarterly Att 2A; 3/4/2005

1R23 Temporary Plant Modifications

10 CFR 50.59 Safety Evaluations:

- L01-0227; TMOD for an Alternate Means of Measuring the DW Floor Drain Sump Flow

Rate; Revision 1

Corporate RCR 299641; Single Failure Vulnerability of Safety Related Division 1 & 2

Protective Relay Circuitry Root Cause Analysis; 3/8/2005

Issue Reports:

- 286665; Stem to Disc Separation on 1DG032; 12/30/2004

- 287208; DWFDS Fillup Rate High; 1/03/2005

- 290618; CSCS Valve PMs Critical Prior to L1R11 Need Deferral; 1/13/2005

14 Attachment

- 290678; Noble Gas Channel Alarm Will Not Clear; 1/14/2005

- 291499; DWFDS Fillup Rate Reading 1.1 GPM; 1/18/2005

- 292281; Div 1 125 VDC Transient During Charger Swap; 1/19/2005

- 293279; U-1 DWFD FUR 1UR-RF002 Pen 1 Ind > 1 GPM Above Alternate; 1/22/2005

- 293389; LOP-DC-01 Revision; 1/23/2005

- 295228; Hi Voltage During U2 Division 1 Charger Swap;1/28/2005

- 297076; Vulnerability of Division 1 & 2 Protective Relay Circuitry; 2/4/2005

- 297795; Difference in 125VDC Divisional Charger Metering; 2/4/2005

- 299188; Lack of Minimum 6-inch Physical Separation in Division 1 & 2 CTs; 2/8/2005

Engineering Change Requests:

- 352281; Provide Information in Eng Change or Equivalent on Delta Between V-Notch

and the Totalizer; 10/09/2001

- 368281; Battery Charger Troubleshooting as an Intermittent Load; 1/21/2005

Engineering Changes:

- 340584; Evaluate Acceptability of Energizing Both 125 VDC Division 1 or 2 Battery

Chargers Simultaneously to Support Battery Charger Testing; Revision 0

- 346528; Provide Guidance for the Use of Intermittent Loads; Revision 0

- 353125; Removal of Disc From Valve 1DG032; Revision 0

- 353657; Isolation of Metering to Common 141Y/142Y and 241Y/242Y Safety Related

Buses; Revision 0

Operability Evaluations:

- OE 02-008; Plugging of Unit 2 Drywell Floor Drain Effects on Leak Detection

Instrumentation; Revision 0

- OE 05-001; Minimum 6-inch Physical Separation in Division 1 & 2 CTs; Revision 0

Procedures:

- CC-AA-308; Control and Tracking of Electrical Load Changes; Revision 4

- LES-DC-103A; Division I Battery Charger Capacity Test; Revision 11

- LOR-1PM13J-A301; Drywell Floor Drain Sump Level Hi, Hi Hi, or Pump Start Failure;

Revision 4

- LOS-AA-S101; Unit 1 Shiftly Surveillence; Revision 28

Temporary Configuration Change:

- 353167; Install Alternate Method of Determining DWFDS Flow Rate; 1/24/05

1EP2 Alert and Notification System (ANS) Testing

Procedures:

- EP-AA-125-1004; Emergency Response Facilities and Equipment Performance

Indicator Guidance; Revision 3

LaSalle County Station Design Study for Total EPZ Siren Coverage; January 2002

LaSalle County Station Off-Site Siren Test Plan; Revision 4; December 2002

15 Attachment

Warning System Maintenance and Operational Reports for LaSalle County Station:

- January 8, 2003 through February 28, 2003

- February 11, 2004 through March 2, 2004

Siren Operations Manual - LaSalle County; February 28, 2003

Exelon Semi-Annual Siren Reports For LaSalle County Station:

- January 1, 2003 through June 30, 2003

- July 1, 2003 through December 31, 2003

- January 1, 2004 through June 30, 2004

Issue Reports:

- 206404; Review of Semi-Annual, Non-Scheduled Maintenance Report for First Half

of 2003

- 208758; Review of Semi-Annual, Non-Scheduled Maintenance Report for Second Half

of 2003

1EP3 Emergency Response Organization (ERO) Augmentation Testing

Procedures:

- EP-AA-112-100; Control Room Operations; Revision 7

- EP-AA-112-100-F-01; Shift Emergency Director Checklist; Revision B

- EP-AA-112-100-F-06; Midwest ERO Augmentation; Revision C

- EP-AA-122-1001; Attachment 2; Conduct of Call-In Augmentation Drills; Revision 3

LaSalle County Station ERO Off-Hours, Unannounced, Off-Hours Augmentation Call-In

Drill Records; April 2004 through January 2005

LaSalle Station ERO Roster; Teams A through D and Back-ups; March 2005

Random Sample of 30 LaSalle County Station ERO Members' EP Training Records

Issue Reports:

- 217626; Paging Concerns in April 2004 Augmentation Drill

- 221122; Paging Concerns in May 2004 Augmentation Drill

- 236587; Three On-call ERO Did Not Receive Page in July 2004 Drill

- 262750; Paging Concerns in October 2004 Augmentation Drill

- 275140; Two ERO Members Did Not Receive Page in November 2004 Drill

- 282734; Four ERO Members Did Not Receive Page in December 2004 Drill

- 292460; Three ERO Members Did Not Receive Page in January 2005 Drill

- 262750; Evaluation of ERO Response Problems During Monthly Augmentation Drills

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

Procedures:

- EP-AA-122; Drills and Exercises; Revision 4

- EP-AA-122-1001; Drill Development, Conduct, and Evaluation; Revision 4

16 Attachment

Internal Memorandums:

- Mini-Drill Findings and Observation Report for Four Drills in August 2003;

September 2, 2003

- October 2003 Mini-Drill Findings and Observation Report; October 24, 2003

- LaSalle County Station 2003 Medical Drill Findings and Observation Report;

January 5, 2004

- LaSalle 2004 NRC Graded Exercise Findings and Observation Report; April 9, 2004

- May 19 and June 2, 2004 Mini-Drills Findings and Observation Report; June 3, 2004

- LaSalle County Station June 28, 2004 Unusual Event Critique Report; July 26, 2004

- July 29 and August 5, 2004 Mini-Drills Findings and Observation Report;

August 11, 2004

- December 9 and December 16, 2004 Mini-Drills Findings and Observation Report;

December 30, 2004

- LaSalle County Station 2004 Medical and Health Physics Drill Findings and

Observation Report; December 20, 2004

Nuclear Oversight Reports:

- Emergency Preparedness 50.54(t) and Meteorology Audit Report LAS-04-03;

Performed on April 12 through 16, 2004; April 22, 2004

- Objective Evidence Report LS-04-3Q; ERO Staffing and Awareness of

Fitness-for-Duty Expectations

- Objective Evidence Report LS-04-4Q; Observations of Two Mini-Drills and Medical Drill

in December 2004

Root Cause Investigation Report; Emergency Plan Radiation Protection On-Shift

Requirement Not Met Due to Lapsed Radiation Protection Qualifications of Chemistry

Technicians; December 3, 2004

Issue Reports:

- 178665; NOS Observations of December 2003 Medical Drill

- 190290; NOS Observations During February 2004 Drill and March 2004 Exercise

- 202751; February 2004 Drill Scenario Validation Concerns

- 207883; Three Concerns on Performance of In-Plant Teams' Controllers During

March 2004 Exercise

- 207887; March 2004 Exercise Scenario Development and Control Weaknesses

- 207890; Warning Onsite Personnel Objective Failed During March 2004 Exercise

- 209239; Re-assess Seismic Monitor Set Point Value in Emergency Action Level HU-4

- 214187; Slow Decision Making to Authorize Potassium Iodide to Affected On-site

Personnel During March 2004 Exercise

- 214200; Operations Support Center ERO Performance Concerns During March 2004

Exercise

- 215285; Several Emergency Plan Elements Not Tested in Five-Year Period

- 215362; Some Recreational Facilities Within the EPZ Did Not Have Posted Emergency

Information

- 216385; No Actions Planned for ERO Pagers' "Dead Zones"

- 232858; Notification Performance Improvement Opportunities from June 2004 Actual

Unusual Event Response

- 241268; Resident Inspector Noted Failure to Consider Applicability of a Heat Stress

Procedure During a July 2004 Drill

17 Attachment

- 257638; On-Shift ERO Staffing Concern - Training of Chemistry Technicians Versus

Training Of Radiation Protection Technicians

- 264105; NOS Concern on Critique When 2004 Medical Drill was Suspended

- 273813; Technical Support Center's Particulate, Iodine, and Noble Gas Monitor is Out

of Calibration and Back-up Monitor Not Adequate

Training Request 04-402; Additional Training on Notification Timeliness

NRC Event Report 40845; Unusual Event Declared Due to Earthquake Registered at

LaSalle County Station

Required Reading Packages:

- ERO Package on February 2004 Drill and March 2004 Exercise

- Shift Managers Package on Warning Onsite Personnel Concerns During March 2004

Exercise

- ERO Package on Operations Support Center Staff's Performance Concerns During

March 2004 Exercise

Corporate Action Requests:

- 5040EP; Corporate EP Staff Revise ERO Training Procedure to Increase Level of

Detail on ERO Training of Radiation Protection Versus Chemistry Technicians

- 8007EP; Corporate EP Staff Assess Process to Determine Qualification Requirements

of ERO Members Whose ERO Training Includes Accredited Training Performed by

Other Departments

2OS1 Access Control to Radiologically Significant Areas

Access Control to Radiologically Significant Areas and Occupational Exposure Control

Effective Performance Indicator; September 30, 2005

Issue Reports:

- 261792; Access Control Focused Area Self-Assessment; 10/8/2004

- 282460; TLD Run Through X-Ray Machine; 12/13/2004

- 291904; Exceeded Dose Allotted for Coil Cleaning; 1/19/2005

- 293751; Unexpected High Dose-Rate on Radwaste Container; 1/24/2005

- 294919; Venture Scaffold Carpenters Contaminated; 1/25/2005

- 297958 Venture Carpenter - Electronic Dosimeter Dose Rate Alarm; 2/4/2005

- 298702; Radworker Human Performance Issue; 2/7/2005

- 299284; Dose Rate Alarm Received While Hanging Lead in 2B RHR; 2/14/2005

- 299670; (NOS ID) Radiation Protection Improper Posting on the Turbine Deck;

2/9/2005

- 299705; Failure to Obtain Thermoluminescent Detector Prior to Working in

Radiologically Controlled Area; 2/9/2005

- 299750; Dose Rate Alarm Received During Shielding Installation; 2/9/2005

- 300861; Electronic Dosimeter Dose Rate Alarms in 678 Turbine Building Main Steam

Tunnel; 2/13/2005

- 299763; Dose Rate Alarm Received During Shielding Installation; 2/9/2005

- 301189; Unexpected Dose Rate Alarm - Venture Pipefitter; 2/19/2005

- 301225; Contaminated Area Reach-In - Venture Worker; 2/19/2005

18 Attachment

- 301798; Prompt Investigation Report of PN Services Workers Cut Vent Hose on

Refuel Floor; 2/15/2005

Procedures:

- MA-AA-716-010; Maintenance Planning; Revision 4

- MA-MW-716-010-1000; Passport Work Planning Manual; Revision 4

- RP-AA-461; Radiological Controls for Contaminated Water Diving Operations;

Revision 0

2OS2 As Low As Is Reasonably Achievable Planning And Controls (ALARA)

Issue Reports:

- 300541; RQP Hold Released By Non-Radiation Protection Person; 2/11/2005

- 300710; Work Order RQP Hold Bypassed; 2/12/2005

- 300730; LaSalle Permitting Low Standards of Work, Ineffective Corrective Actions;

2/12/2005

Procedures:

- RP-AA-376-1001; Radiological Posting, Labeling, and Marking Standard; Revision 2

- RP-AA-401; Operational ALARA Planning and Controls; Revision 4

Radiation Work Permits:

- 10004000; L2R10 Temporary Shielding in the Drywell; Revision 2

- 10004003; L2R10 Scaffold Activities in the Drywell; Revision 0

- 10004016; L2R10 CRD Pull and Put; Revision 2

- 10004057; L2R10 Unit 2 Reactor Suppression Pool Activities and Support; Revision 0

- 10004088; Unit 2 Reactor Vessel Disassembly and Reassembly; Revision 1

- 10004792; L2R10 Chemical Decon Drywell Work/Unit 2 RB 774'; Revision 0

4OA1 Performance Indicator Verification

Procedures:

- EP-AA-125-1002; ERO Performance; Revision 3

- EP-AA-125-1003; ERO Readiness; Revision 4

- EP-AA-125-1004; Emergency Response Facilities and Equipment; Revision 3

- LS-AA-2110; Monthly Data Elements for NRC ERO Drill Participation; January 2004

through December 2004; Revision 6

- LS-AA-2120; Monthly Data Elements for NRC Drill and Exercise Performance;

January 2004 through December 2004; Revision 4

- LS-AA-2130; Monthly Data Elements for NRC ANS Reliability; January 2004 through

December 2004; Revision 4

Siren Reports:

- Daily Reports; January 1, 2004 through December 31, 2004

- Monthly Operability Reports; January 2004 through December 2004

Required Reading Package; Protective Action Recommendation Development; dated

June 2004

19 Attachment

Issue Reports:

- 241955; Failure to Classify an Alert During August 2004 Drill

- 242469; Inaccurate Emergency Class on Notification Form During August Drill

- 242025; Incorrect Protective Action Recommendation Developed During a Drill

- 249574; Adverse Trend in DEP Performance Indicator in Fourth Quarter 2004

- 283475; Failure to Classify an Alert 15 Minutes During December 9, 2004, Drill

- 283601; Inaccurate Notification Form Completed During December 16, 2004, Drill

- 306946; NOS Identified Minor Error with Reported DEP PI Opportunities for Fourth

Quarter 2004

4OA2 Identification and Resolution of Problems

Procedures:

- CC-AA-201; Plant Barrier Control Program; Revision 5

- OP-MW-201-004; Fire Prevention for Hot Work; Revision 0

- OP-MW-201-007; Fire Protection System Impairment Control; Revision 3

- OP-AA-201-001; Fire Marshal Tours; Revision 2

- OP-AA-201-008; Pre-Fire Plans; Revision 1

- OP-AA-201-009; Control of Transient Combustible Material; Revision 4

Issue Reports:

- 280218; 2A Diesel Generator Trip on Reverse Power; 12/07/2005

- 302209; Small Fire in Unit 2 Reactor Building - 694 Elevation; 2/16/2005

- 302447; Near Miss - Fire Extinguisher Malfunction; 2/16/2005

- 304516; (NRC Identified) RHR Keep Fill Modification Fire Protection Awareness;

2/23/2005

4OA3 Event Follow-up

Corporate RCR 299641; Single Failure Vulnerability of Safety Related Division 1 & 2

Protective Relay Circuitry Root Cause Analysis; 3/8/2005

RA05-25; License Condition 2.F(a) Report: Exceeding License Condition 2.C(1);

3/9/2005

Issue Reports:

- 297076; Vulnerability of Division 1 & 2 Protective Relay Circuitry; 2/4/2005

- 299188; Lack of Minimum 6-inch Physical Separation in Division 1 & 2 CTs; 2/8/2005

- 304613; Controller Failed High; 2/23/2005

- 304789; Failure of 1HK-RR023 Results in Unit 1 Operation Greater Than 100 % RTP;

2/23/2005

- 305612; Evaluation of Operations Crew Performance - RR FCV Failure; 2/25/2005

- 307523; Problem with Re-Flash Function for SPDS Button on PPC; 3/2/2005

- 307654; Evaluate LOA-RR-101(102) for Possible Revision; 3/2/2005

- 307657; U1 PPC Alarm Program May Prevent Audible Alarm; 3/2/2005

- 307659; U2 PPC Alarm Program May Prevent Audible Alarm; 3/2/2005

20 Attachment

Operability Evaluation:

- OE 05-001; Minimum 6-inch Physical Separation in Division 1 & 2 CTs; Revision 0

Engineering Change:

- EC 353657; Isolation of Metering to Common 141Y/142Y and 241Y/242Y Safety

Related Buses; Revision 0

21 Attachment

LIST OF ACRONYMS USED

ACE Apparent Cause Evaluation

ALARA As-Low-As-Is-Reasonably-Achievable

ANS Alert and Notification System

APRM Average Power Range Monitor

ARM Area Radiation Monitor

ASME American Society of Mechanical Engineers

CAP Corrective Action Program

CAR Corrective Action Request

CCA Common Cause Analysis

CFR Code of Federal Regulations

CIV Containment Isolation Valves

CR Condition Report

CRD Control Rod Drive

CRS Control Room Supervisor

CSCS Core Standby Cooling System

CT Current Transformer

CW Circulating Water

CY Calendar Year

DC Direct Current

DG Diesel Generator

DGN Diesel Generators

DRP Division of Reactor Projects

DW Drywell

ECCS Emergency Core Cooling System

ED Electronic Dosimeter

EDG Emergency Diesel Generator

EP Emergency Preparedness

EPZ Emergency Preparedness Planning Zone

ERO Emergency Response Organization

ES Engineered Safeguards

FC Fuel Pool Cooling

FCV Flow Control Valve

HEPA High Efficiency Particulate Air

HRA High Radiation Area

I&C Instrumentation and Controls

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Inspection Report or Issue Report

ISI Inservice Inspection

IST Inservice Test

kV Kilovolt

kW Kilowatts

kVAR Kilovolts-Amperes-Reactive

LLRT Local Leak Rate Testing

LPCS Low Pressure Core Spray

LOCA Loss of Coolant Accident

mrem Millirem

22 Attachment

msec Millesecond

MWth Megawatts Thermal

NCV Non-Cited Violation

NEI Nuclear Energy Institute

NLO Non-Licensed Operator

NRC U.S. Nuclear Regulatory Commission

NSO Nuclear Station Operator

OWA Operator Workaround

PI Performance Indicator

PI&R Problem Identification and Resolution

PRM Process Radiation Monitors

RA Required Actions

RCA Radiologically Controlled Area

RCIC Reactor Core Isolation Cooling

RCR Root Cause Report

RCR Root Cause Review

RFO Refueling Outage

RHR Residual Heat Removal

RHRSW Residual Heat Removal Service Water

RO Reactor Operator

RP Radiation Protection

RPS Radiation Protection Specialist

RPS Reactor Protection System

RPT Radiation Protection Technician

RR Reactor Recirculation

RWCU Reactor Water Cleanup

RWP Radiation Work Permit

SAT Station Auxiliary Transformer

SBGT Standby Gas Treatment

SBLC Standby Liquid Control

SDP Significance Determination Process

SRA Senior Reactor Analyst

SRO Senior Reactor Operator

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

Vac Volts Alternating Current

Vdc Volts Direct Current

VY Ventilation System

23 Attachment