ML040690129

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Inspection Results Memoranda
ML040690129
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 03/05/2004
From: Christine Lipa
NRC/RGN-III/DRP/RPB4
To: Grobe J
NRC/RGN-III
References
Download: ML040690129 (14)


Text

March 5, 2004 MEMORANDUM TO: John A. Grobe, Chairman Davis-Besse Oversight Panel FROM: Christine A. Lipa, Chief /RA/

Branch 4 Division of Reactor Projects

SUBJECT:

DAVIS-BESSE INSPECTION RESULTS MEMORANDA The purpose of this memorandum is to provide you four separate Inspection Results Memoranda that supported Panel discussion of several Restart Checklist items. Since several Inspection Reports are still under development, the Panel requested team members to document their conclusions in memoranda to the Panel. The conclusions contained in these memoranda will also be documented in the related Inspection Reports; however, this provides early documentation of the teams assessment and conclusions.

Attached are the following memoranda, which are associated with the Restart Checklist.

Date of Memorandum Checklist Number ADAMS ML#

February 6, 2004 Memorandum from Restart Checklist Items 5.b, ML040611081 R. Skokowski and 5.c February 18, 2004 Memorandum Restart Checklist Item 2.a ML040611099 from S. Thomas February 23, 2004 Memorandum Restart Checklist Item 2.e ML040420027 from W. Ruland February 25, 2004 Memorandum Restart Checklist Item 4.b ML040580717 from G. Wright Attachments: As Stated

DOCUMENT NAME: C:\ORPCheckout\FileNET\ML040690129.WPD To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RIII RIII RIII RIII NAME CLipa/trn DATE 03/05/04 OFFICIAL RECORD COPY

Attachment 1 February 6, 2004 MEMORANDUM TO: John A. Grobe, Chairman, Davis-Besse Oversight Panel FROM: Richard A. Skokowski, Leader, Davis-Besse Restart Readiness Assessment Team /RA/

SUBJECT:

RESTART CHECKLIST AND RESTART ACTION MATRIX ITEMS CLOSURE RECOMMENDATIONS The purpose of the Restart Readiness Assessment Team Inspection (RRATI) was to determine whether the plant is ready to enter power operations and what conclusions can be made regarding plant operations once the plant enters normal routine operations. The inspection report for the Restart Readiness Assessment Team Inspection, Report 50-346/04-04, will likely not be issued prior to the restart decision by the Oversight Panel. This memorandum serves to document the teams conclusions with respect to Restart Checklist and Restart Action Matrix (RAM) items assigned to this inspection. The basis for the teams recommendations will be documented in Report 50-346/04-04.

The team identified no issues to preclude restart of the plant.

The RAM items assigned to this RRATI were:

C SUP-32 (IP95003 02.03.b3)- Assessment of Performance in the Reactor Safety Strategic Performance Area: Key Attribute - Design: Determine if the System is operated consistent with the design and licensing documents. - Overall Acceptable C SUP-35 (IP95003 02.03.c 2.a) - Assessment of Performance in the Reactor Safety Strategic Performance Area: Key Attribute - Human Performance: Review specific problem areas and issues identified by inspections to determine if concerns exist in organizational practices such as pre-job briefings, control room team work, shift turnover, self-checking and procedural use and adherence. - Overall Acceptable C SUP-48 (IP95003 02.03.f.1) - Assessment of Performance in the Reactor Safety Strategic Performance Area: Key Attribute - Configuration Control: Assess the effectiveness of corrective actions for deficiencies involving configuration control. -

Overall Acceptable C C Complete RRATI inspection to do round-the-clock inspection of complex control room evolutions. - Complete/Overall Acceptable

The Restart Checklist Items assigned to the RRATI were:

C 5.b System Readiness for Restart - Overall Acceptable C 5.c Operations Readiness for Restart - Overall Acceptable CONTACT: Richard A. Skokowski, DRP (815) 234-5451 To receive a copy of this document, indicate in the box: C = Copy without enclosure E = Copy with enclosure N = No copy OFFICE RIII RII RIV RIII NAME GWilson JZeiler THoeg JRutkowski DATE 02/06/04 02/06/04 02/06/04 02/06/04 OFFICE RIII NAME RSkokowski DATE 02/06/04 OFFICIAL RECORD COPY

Attachment 2 February 18, 2004 MEMORANDUM TO: John A. Grobe, Chairman, Davis-Besse Oversight Panel FROM: Scott Thomas, SRI, Davis-Besse Nuclear Power Station

SUBJECT:

RESTART CHECKLIST ITEM 2.a CLOSURE RECOMMENDATION The purpose of this memorandum is to recommend the closure of Restart Checklist Item 2.a

[Reactor Pressure Vessel Head Replacement].

Several inspections were conducted to evaluate licensee activities associated with the replacement of the reactor vessel pressure head at the Davis-Besse Station. Using approved special inspection plans and Inspection Procedure 71007, Reactor Vessel Head Replacement Inspection, as guidance, the inspectors assessed licensee performance in the following areas:

design and planning/reactor vessel head inspection; reactor vessel removal and replacement; containment vessel restoration; and post installation testing. Specific inspection activities were documented in the following inspection reports: 05000346/2002007; 05000346/2002010; 05000346/2003005; 05000346/2003017; and 05000346/2003023. Based on results of these inspections, sufficient inspection activities were completed to provide reasonable assurance that Restart Checklist Item 2.a can be closed, with the exception of the observance of control rod drive insertion testing.

The inspectors observed the performance of surveillance test procedure DB-SC-03270, Control Rod Assembly Insertion Time Test, Revision 03, on February 10, 2004. The surveillance was completed successfully and all acceptance criteria were satisfied. No findings of significance were identified by the inspectors. This inspection activity will be documented in the Integrated Inspection Report 05000346/2004002.

This memorandum serves to document the recommendation for closure of Restart Checklist Item 2.a, Reactor Pressure Vessel Head Replacement. The details supporting closure of Restart Checklist Item 2.a will be documented in Integrated Inspection Report 05000346/2004002.

CONTACT: Scott Thomas, SRI, Davis-Besse /RA C. Lipa for C. Thomas via tel-con_

(419) 244-4494 Christopher S. Thomas SRI, Davis-Besse Station

ML040420027 OFFICE PM:PDIII-2 LA:PDIII-2 SC:PDIII-2 PD:PDIII NAME JHopkins PCoates AMendiola WRuland DATE 2/19/04 2/19/04 2/19/04 2/19/04 Attachment 4 February 25, 2004 MEMORANDUM TO: John A. Grobe, Chairman Davis-Besse Oversight Panel FROM: Geoffrey C. Wright, Leader, Davis-Besse Management /RA/

and Human Performance Inspection Team

SUBJECT:

RESTART CHECKLIST ITEM 4.b CLOSURE RECOMMENDATION The Management and Human Performance inspection was designed to evaluate the licensees actions in response to the degraded reactor vessel head issue. Specifically, the inspection was to evaluate the following areas: the licensees root cause assessments, the licensees corrective actions and their implementation, and the licensees tools for monitoring the effectiveness of the corrective actions. Because of concerns which developed following the root cause analyses, the inspection also included an evaluation of the licensees actions regarding safety conscious work environment (SCWE) and the employee concerns program (ECP). The inspection report for the Follow Up Management and Human Performance inspection, Report 50-346/04-03, will not be issued prior to the restart decision by the Oversight Panel. This memorandum serves to document the Teams overall conclusion with respect to Restart Checklist Item 4.b. Attachment 1 provides additional detail on the results of the Management and Human Performance inspections three phases and the Follow Up inspection into the November 2003 SCWE survey results.

The Management and Human Performance inspection was divided into three phases to look at the three areas. Phase 1 evaluated the licensees root cause analyses. Phase 1 concluded that while the initial analyses that the licensee had performed were acceptable, they had missed a number of areas and as such, the licensee needed to perform additional analyses to appropriately cover all potential areas of concern. Phase 1 results were documented in Inspection Report 50-346/2002015. Phase 2 reviewed the corrective actions associated with the root or contributing causes. The review looked at whether the actions would address the causes and the schedule for implementing the actions. Phase 2 concluded that the proposed corrective actions if properly implemented and monitored should preclude recurrence of the causes for the head degradation. Phase 2 results were documented in Inspection Report 50-346/2002018. Phase 3 evaluated the licensees tools for monitoring the effectiveness of the management and human performance corrective actions. Phase 3 also evaluated the licensees activities to improve the sites SCWE, the activities of the safety conscious work environment review team (SCWERT), and the current status of the employee concern program. Phase 3 concluded that the tools the licensee was using to monitor safety culture and SCWE were appropriate and provided valuable information in these areas. Further, Phase 3 concluded that the current ECP was appropriate and was functioning as designed.

Phase 3 results were documented in Inspection Report 50-346/20003012.

Notwithstanding the generally positive characterizations above, the Teams review of the licensees November SCWE survey, one monitoring tool that included safety culture attributes,

DOCUMENT NAME: C:\ORPCheckout\FileNET\ML040690129.WPD To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RES NRR OE NRR NAME GWright for (email) GWright for GWright for (email) GWright for (email)

JPersensky/trn (email) LJarriel DDesaulniers CGoodman DATE 02/24/04 02/24/04 02/24/04 02/24/04 OFFICE RI RIII RES NRR NAME GWright for (email) GWright for GWright for (email) GWright for (email)

HEichenholz (email) MKeefe JCai JHeller DATE 02/24/04 02/25/04 02/24/04 02/24/04 OFFICE RIII RIII RIII RIII NAME GWright for (email) MBrothers GWright JBeck unavailable DATE 02/23/04 02/ /04 02/25/04 OFFICIAL RECORD COPY

J. Grobe identified that a number of key organizations had provided more negative responses to some questions then in March 2003. Specifically operations, plant engineering, quality assurance, and to a lesser extent maintenance provided more negative responses to questions dealing with production over safety/quality, SCWE, corrective action program, and management involvement then in May 2003. For example, operations went from 6% to 23.4% negative responses to the question Management cares more about safety than cost and schedule, Plant Engineering went from 6.6% to 12% negative responses to the question I can raise nuclear safety or quality concern without fear of retaliation, and Quality Assurance went from 0% to 8.7% negative responses to the question I am aware of others who have been subjected to HIRD within the last 6 months. Additional details are provided in Attachment 2. Because the responses raised questions regarding the continuing effectiveness of the licensees actions to improve safety culture, the Team determined that additional inspection was necessary to understand the cause(s) of the additional negative responses.

The Team developed a detailed inspection methodology to evaluate and independently validate the licensees assessment of the increases in negative responses. The inspection methodology included document reviews and interviews with approximately 120 individuals, in the departments of concern, to gain insights into why there was an increase in negative responses.

The Team validated, through independent inspection, that the licensees assessment of the causes for the increase in negative responses was appropriate. The licensee had used an appropriate approach to determine the causes of the decline and interviewed an acceptable sample of staff from the affected departments. Throughout the NRC interview process, the Team noted a less positive tone by the licensees staff when responding to questions dealing with the behavior and effectiveness of their management than the NRC Team noted during interviews in May 2003. The staffs responses related in large part to work hours, schedule credibility, and management comments that appeared to be inconsistent with the licensees Leadership In Action training. The Team also noted that interviewees personally exhibited a high focus on safety and indicated that their management placed the highest priority on addressing safety concerns. While the licensee is developing additional corrective actions in response to their assessment, the Team concluded that the licensees immediate corrective actions were adequate for restart and that there were no outstanding issues that would preclude restart.

In summary, through the three phases and Follow Up inspections, the Management and Human Performance Team concluded that the licensees root cause analyses and associated corrective actions for the safety culture issues which resulted in the reactor head degradation, were appropriate. The Team also concluded that the corrective actions with the associated monitoring activities, have been sufficiently effective to provide reasonable assurance to preclude recurrence of the conditions which led to the degradation of Davis-Besses reactor vessel head. While additional actions are planned for continued improvement in the safety culture at Davis-Besse, no issues were identified that would preclude unit restart. Therefore, the Team recommended closure of restart checklist item 4.b.

Attachments: 1. Safety Culture Issues at the Davis-Besse Nuclear Power Station

2. Davis-Besse March and November 2003 SC/SCWE Survey Department Data - FENOC and Contract Employees

ATTACHMENT 1 SAFETY CULTURE ISSUES AT THE DAVIS-BESSE NUCLEAR POWER STATION DEFINITION OF THE PROBLEM On August 21, 2002, the licensee submitted its root cause analysis for the reactor pressure vessel head degradation. The licensee concluded that there was a lack of sensitivity to nuclear safety and the focus was on justifying conditions, that there was less than adequate nuclear safety focus, and that there was less than adequate implementation of the corrective action program as indicated by addressing symptoms rather than causes. To address these cultural deficiencies in its past performance, the licensee created the Management and Human Performance building block in its Return to Service Plan. The building block was designed to further identify organizational performance and cultural causal factors, and to identify and track corrective action implementation.

NRC INSPECTION AND ASSESSMENT The NRC structured its inspection in this area in three phases; (1) inspection of the root cause evaluations; (2) inspection of the corrective action development, prioritization and implementation; and (3) evaluation of the effectiveness of the corrective actions at improving organizational effectiveness and cultural.

Phase 1 - Inspection of the Root Cause Evaluations The inspections first phase was the assessment of the adequacy of the licensees root cause evaluations. This inspection was conducted by Region III, NRR and contract staff experts in inspection and assessment, root cause evaluation techniques, and human and organizational performance. The licensee used the Management Oversight and Risk Tree (MORT) analysis technique to perform their overall root cause assessment. The inspection team found that the principles of MORT were properly applied; however, the scope of the assessment was not sufficient to reveal all potential causal factors. The licensee performed additional assessments in multiple areas including engineering, operations, and corporate support, among others.

Review by the team revealed that the combined assessments resulted in sufficient breadth and depth to be confident that the causal factors were identified. During the course of these assessments, many contributors were identified, including deficiencies in the licensees safety conscious work environment, the ombudsman program, and safety culture at the facility.

Phase 2 - Inspection of the Corrective Action Development, Prioritization and Implementation The same team returned to evaluate corrective action development and implementation to ensure those actions addressed all the causal factors. The licensee developed over 125 specific corrective actions. The team concluded that each of the causal factors was addressed in the corrective actions. In addition, the team concluded that the corrective actions were properly prioritized and sampled implementation of the corrective actions concluding that the 1

actions would be implemented properly. Corrective actions ranged from corporate governance issues and executive pay structures, policy and procedural alignment in safety culture areas, replacing the ombudsman program with a structured employee concerns program, establishing a formal safety conscious work environment program and addressing a multitude of organizational and communication issues.

Phase 3 - Evaluating the Effectiveness of Corrective Actions at Improving Safety Cultural Recognizing the key role safety culture deficiencies played in the root cause of the head degradation event, the Panel determined that it was necessary to evaluate the effectiveness of the improvement in safety culture at the facility. Because the NRC has only broadly stated expectations in cultural areas, the approach the Panel employed was not to specifically assess organizational safety culture, but to ensure that the licensee had adequate tools to self-assess in the safety culture areas, that the assessments were appropriately performed and provided meaningful insights into organizational weaknesses, and that the licensee was responding to those assessment results by taking actions to ensure a continuing trend of improvement.

The Panel brought together a team of experts from Region III, NRR, RES, OE and contractors who were highly capable and credible in performing this type of assessment. The team utilized national and international guidance and standards as a foundation for its assessment. The team concluded that the combination of licensee internal management assessments, surveys, and independent assessments provided a solid foundation for understanding organizational safety performance strengths and weaknesses. The team also found that the licensee, with some exceptions, was using their corrective action program to address safety culture deficiencies. The team noted steady improvement in overall organizational performance in this area.

Recent Results of the SC/SCWE Survey In November 2003, the licensee performed their third safety culture/safety conscious work environment survey of all staff. The results of all the surveys have been presented and discussed publicly. The first survey, conducted in August 2002, revealed significant cultural problems in many areas of the organization, including a significant lack of confidence in facility managements focus on safety. The second survey, conducted in March 2003, revealed double digit percentage improvements in many areas of the organization. The November 2003 survey showed steady or slightly improving overall organizational performance; however, several critical departments including operations, system engineering and quality assurance exhibited declines in some areas.

The NRC inspection team performed surveys of plant staff in May 2003 following the March 2003 survey to validate the veracity of the survey technique and implementation.

Following the November 2003 survey results, an expanded team, including an individual from Region I, performed a follow-up inspection, to evaluate the licensees assessment of the declines. The team performed detailed document reviews and conducted a survey of selected licensee staff in January 2004. The team found that in all cases, staff understood and would fulfill their responsibility for identifying safety concerns and had confidence that management would place the proper priority on addressing safety concerns. However, when the team contrasted its interview results from May 2003 with January 2004, the team identified a less positive perspective of some staff in their confidence in managements behaviors and effectiveness in other areas. The team concluded that the licensee had identified the 2

contributing factors to this decline, including excessive work hours, inadequate work scheduling resulting in schedule adherence problems, and poor or inappropriate communication vertically in the organization on critical management decisions. The team found that licensee management had identified and implemented short term actions to address these issues. The team concluded that the short term actions were adequate for the identified issues and, while some of the actions had not been in place long enough to obtain feedback on their effectiveness, other actions had received positive response from the licensees staff. The licensee has committed to perform a follow up effectiveness evaluation, patterned after the initial evaluation, toward the end of the 2nd quarter 2004. The team considered this appropriate.

Conclusions Overall, the three phases of the inspection and the Follow Up inspection revealed adequate cause assessments, sufficient corrective actions, and effective assessment techniques for measuring organizational improvement.

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Attachment 2 Davis-Besse March and November 2003 SC/SCWE Survey Department Data - FENOC and Contract Employees All Ops Plant Maint QA Blank Engr Mar Nov Mar Nov Mar Nov Mar Nov Mar Nov Mar Nov Number of surveys 1139 780 100 77 107 75 285 167 24 23 87 14 Management care mor about safety than 15.2% 17.1% 6% 23.4% 18.7% 24.0% 21.4% 25.0% 0.0% 21.7% 18.6% 35.7%

cost & schedule Management expectations on safety and 9.9% 12.5% 9.0% 11.7% 8.8% 16.0% 12.4% 16.2% 4.3% 13.0% 9.3% 8.3%

quality are reflected in appraisals, reward, and discipline Resolution of nuclear safety and quality 10.2% 9.8% 6.0% 11.0% 16.9% 16.7% 11.2% 7.8% 4.2% 23.9% 11.2% 18.5%

issues, including Root Cause is effective in our organization CR issues are properly prioritized, 13.2% 10.9% 6.0% 15.6% 16.8% 21.3% 14.4% 9.6% 4.2% 17.4% 12.8% 21.4%

evaluated and resolved in timely manner CR process is effectively utilized by DB to 12.1% 11.4% 7.0% 14.3% 18.9% 18.7% 13.7% 7.2% 8.3% 26.1% 14.1% 21.4%

resolve quality issues in timely manner I can raise nuclear safety or quality 7.1% 6.5% 3.0% 5.2% 6.6% 12.0% 9.5% 11.4% 0.0% 0.0% 15.1% 7.1%

concern without fear of retaliation ECP will keep my identity confidential at 6.4% 9.3% 8.0% 11.8% 3.8% 12.0% 9.1% 7.2% 0.0% 13.0% 13.1% 14.3%

my request I am aware of SCWERT and its purpose 6.2% 8.5% 4.0% 11.7% 11.2% 14.7% 6.4% 10.2% 0.0% 13.0% 8.3% 14.3%

I have been subjected to HIRD within the 8.1% 3.7% 5.0% 2.6% 8.5% 8.0% 9.5% 4.2% 0.0% 4.3% 21.2% 0.0%

last 6 months I am aware of others who have been 15.3% 7.3% 8.0% 13.0% 15.1% 18.7% 22.8% 4.3% 0.0% 8.7% 28.6% 7.7%

subjected to HIRD within the last 6 months 1

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