Information Notice 1979-04, Degradation of Engineered Safety Features

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Degradation of Engineered Safety Features
ML031180118
Person / Time
Issue date: 02/16/1979
From:
NRC/IE
To:
References
IN-79-004, NUDOCS 7912120548
Download: ML031180118 (7)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

WASHINGTON, D.C. 20555 February 16, 1979 IE Information Notice No. 79-04

DEGRADATION OF ENGINEERED SAFETY FEATURES

Summary

On September 16, 1978, an unusual sequence of events occurred at Arkansas

Nuclear One, Units 1 and 2. The events involved the electrical power

sources and culminated in the spurious activation and degraded operation

of Unit 2 Engineered Safety Features (ESF). Analysis of the course of

the incident has identified three safety concerns in the electrical

distribution system operation and design.

(1) The offsite power supply for ANO Unit 1 Engineered Safety Feature

loads was deficient in that degraded voltage could have resulted

in the unavailability of ESF equipment, if it were to be needed.

(2) The design of the ANO site electrical system that provides offsite

power to Units 1 and 2 did not fully meet the Commission's Regula- tions, 10 CFR 50, Appendix A, General Design Criterion 17, because

in certain circumstances a loss of one of the two offsite power

circuits would also result in a loss of the other such circuit.

(3) Deficiencies existed in the operation of the Unit 2 inverters

that convert DC to AC power for the uninterruptable 120 volt

vital AC buses.

Description of Circumstances

Initially Unit 1 was operating at 100 percent power; Unit 2 was in hot

standby performing hot functional testing in preparation for initial

criticality and power operational) Unit 1 auxiliary electrical loads

were being supplied from the Unit 1 main generator via the unit

auxiliary transformer. Unit 2 auxiliary electrical loads were being fed

from the offsite grid through Startup Transformer No. 3. The normal

operating status was interrupted by the failure of the Unit 1 Loop "A"

Main Steam Line Isolation Valve (MSIV) air operator solenoid causing the

MSIV to close as designed. The Unit 1 Reactor Protection System sensed

conditions requiring reactor shutdown and tripped the reactor. The

1 The Unit 2 Operating License did not permit criticality of power

operation at the time of the incident.

l of 5 793208

7 903 02 0 3 8 3

IE Information Notice No. 79-04 February 16, 1979 Unit 1 turbine-generator tripped concurrently. Because the Unit l

generator could no longer supply power for the Unit 1 auxiliary loads, these loads were automatically transferred to Startup Transformer No. 1 to supply this power from offsite. The sequence of events should have

ended at this point.

The power to Startup Transformer No. 3, which was feeding Unit 2, and to

Startup Transformer No. 1, now feeding Unit 1, normally passes through a

single piece of equipment, the Bus Tie Auto-Transformer. (Figure 1 shows a simplified block diagram of the principal electrical equipment

involved.) The Auto-Transformer has the capacity to provide power for

both units, but due to an error, the protective relays were still adjusted

for the operation of Unit 1 only. As a result, when both units concur- rently drew power from the Auto-Transformer these protection relays

tripped and cut off power to Startup Transformer Nos. 1 and 3.

Startup Transformer No. 2, also shown in Figure 1, thus became the only

source of offsite power for both Units 1 and 2. The onsite switching

equipment automatically transferred the full auxiliary loads for both

units to this transformer. However, this transformer is not designed to

carry full auxiliary loads for both units. For this reason, Startup

Transformer No. 2 became overloaded and the voltage dropped on the

station distribution system for offsite power. At this time and during

most of the incident t perating personnel at both units were unaware of

the degraded voltage 2 dondition due to the overloaded Startup Trans- former No. 2.(3)

2 Two other events involving degraded voltage for ESF equipment occurred

at Millstone Unit 2 in July 1976. These events were reported as an

abnormal occurrence (No. 76-9) in NUREG-0900-5, Report to Congress on

Abnormal Occurrences, July-September 1976.

3 It was subsequently determined that the following combinations of

Unit 1 and Unit 2 operation would lead to the loss of the Bus Tie

Auto-Transformer and the subsequent overloading of Startup Transformer

No. 2:

1. Both Units in either the startup or shutdown mode, or

2. Trip of one unit while the other is in either the startup

or shutdown mode, or

3. Simultaneous trip of both units.

2 of 5

IE 'Information Notice No. 79-04 February 16, 1979 At Unit 2, eight seconds after the switch to Startup Transformer No. 2, the relays (4) which operate to protect Engineered Safety Feature (ESF)

equipment from low (degraded) voltage disconnected and therefore

deenergized both Unit 2 ESF buses as designed. At the same time, the

Unit 2 Core Protection Calculator (CPC) instrumentation registered trips

which indicated a loss of AC power to the circuits (5) that supply at

least two instrument channels.

The loss of power on two 120 volt vital AC Instrument buses caused, as

designed, an actuation of all Unit 2 Engineered Safety Features. Thus, when the two Unit 2 emergency diesel generators started and provided

power to the previously deenergized ESF buses, the Engineered Safety

Features equipment began to operate. However, due to inverter failures, premature actuation of the Recirculation Actuation System (RAS)

occurred. This actuation momentarily opened a flow path directly

between the Refueling Water Tank (RWT) and the containment sump. ESF

operation and premature RAS operation combined to transfer approximately

60,000 gallons of borated refueling water to the containment sump in

about 90 seconds.

4 These relays are the second level of undervoltage protection required

as a result of the NRC staff review of the 1976 Millstone 2 degraded

voltage event. Corrective design changes (i.e., undervoltage relays

and load sequencing to offsite power) had been implemented on Unit 2 for degraded voltage protection. These design changes had not been

implemented on Unit 1 at the time of the event.

5 Each one of the four CPC instrumentation circuits receives power from

a vital AC bus which in turn receives power from a battery through an

inverter that converts DC power to AC power. Each inverter normally

provides power through a circuit with access to both an ESF bus and

the station batteries. Each inverter also has an automatic switch

that can cut off this normal supply circuit and shift the loads to

an alternate supply circuit, which includes just the ESF bus. (See -

insert on Figure 1.) With both Unit 2 ESF buses momentarily deenergized

the only source of instrument power was from the station batteries

through the normal switch position. However, although the exact cause

is unknown, all four inverter automatic switches were found in the

alternate position. Three of four inverters had improper settings on

time delay relays and one inverter had the undervoltage trip setting

too high, which may have In part been the cause. IE Circular No. 79-02, Failure of 120 Volt Vital AC Power Supplies, dated January 16, 1979, provided details of the inverter problems and recommended items to be

reviewed to avoid similar problems.

3 of 5

IE Information Notice No. 79-04 February 16, 1979 The normal design sequence calls for the RAS to automatically change the

valve lineup when signals from the level instruments on the Refueling

Water Tank (RWT) indicate that the tank is nearly empty, which is

expected to occur approximately 30 minutes after the LOCA. During this

incident, the RAS acted immediately in response to the failure of the

inverters and made the change in lineup while the RWT was nearly full.

The loss of power from the inverters caused a false low water level

indication in the RWT. This false indication provided the signals for

the automatic actuation of the RAS.

Had the Emergency Core Cooling System and/or the Containment Spray

System been needed in the event of a design basis loss of coolant

accident, it would not have performed as designed because of the pre- mature RAS valve actuation. ESF degradation on Unit 2 did not involve a

threat to the health and safety of the public because Unit 2 was pre- operational and had no radioactive fission product inventory in the

core. However, there was no assurance that the inverter deficiencies

which caused the premature operation of the RAS valves would have been

corrected prior to Unit 2 power operation.

In the event of a LOCA with a fission product inventory, if the RAS were

to initiate at the beginning of the accident, as it did in this incident, the low pressure and high pressure coolant injection subsystems (LPCI

and HPCI) of Emergency Core Cooling (ECC) and the Containment Spray

System might not function properly. Actuation of RAS causes isolation

of the water in the RWT, which is the source of short term cooling water

for Emergency Core Cooling and Containment Spray. The premature actua- tion of RAS also causes these pump suction lines to be connected to the

containment sump when there may not be sufficient water available.

Initially, the sequence of events on September 16 did not Indicate any

problem with the electrical distribution system of Unit 1. However, subsequent analysis indicated that in the event of a LOCA at Unit 1 during which Startup Transformer No. 1 received both the auxiliary

electrical loads and starting loads of the Engineered Safety Features a

voltage reduction would result. The safety loads might not initially

transfer to the Unit 1 diesel generators but could remain on the startup

transformer with reduced (degraded) voltage. Although there is margin

in the sizing of emergency equipment and the conditions of operation of

such equipment, this situation could cause fuses to blow in Engineered

Safety Feature circuits which could result in disabling the safety

equipment.

4 of 5

IE Information Notice No. 79-04 February 16, 1979 Cause or Causes The immediate causes of the unusual event at Arkansas

Nuclear One were: (1) loss of the Bus Tie Auto-Transformer which

resulted in degraded power operation through Startup Transformer No. 2, and (2) multiple Unit 2 inverter failures.

The loss of the Bus Tie Auto-Transformer was caused by inappropriate

setpoints for its protective relays. The Bus Tie Auto-Transformer loss

had not been adequately reviewed prior to this event in that the over- loading of the shared Startup Transformer No. 2 had not been identified

during the design and review process.

The primary cause of the failure of the inverters to perform as a

reliable power supply was the lack of adequate preoperational test

procedures, inadequate knowledge of inverter operation and lack of

maintenance control (maintenance has been performed on the inverters

several times prior to this event).

This Information Notice provides details of a significant occurrence

that is still under review by the NRC staff. After completion of the

staff review, this Information Notice will be followed with specific

actions to be taken by licensees.

No written response is required. If you desire additional information

regarding this matter, contact the Director of the appropriate NRC

Regional Office.

Attachment:

Figure 1, Simplified

Block Diagram, Electrical

Distribution

5 of 5

IE Information Notice Nlo. 79-04 INlVERTER l yVR1

[

AUTOMATIC

SWITCH IN

str1 -v

j

NORMAL

POSITION

I VITAL VIT)

IAC AC

I BUS ,BU

AC OUT I

INVERTER UNIT ANO-UNIT 2 (TYPICAL OF FOUR) (ONE OF TWO ESF

TRAINS SHOWW.)

SIiMPLIFIED BLOCK VIAGRAfl - ELECTRIC DISTRIBUTION

FIGURE 1 Attachnent

IE Information Notice No. 79-04 February 16, 1979 LISTING OF IE INFORMATION NOTICES

ISSUED IN 1979 Information Subject Date Issued To

Notice No. Issued

79-01 Bergen-Paterson Hydraulic 2/2/79 All power reactor

Shock and Sway Arrestor facilities with an

OL or a CP

79-02 Attempted Extortion - 2/2/79 All Fuel Facilities

Low Enriched Uranium

79-03 Limitorque Valve Geared 2/9/79 All power reactor

Limit Switch Lubricant facilities with an

OL or a CP