IR 05000282/2002002

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IR 05000282/2002-002; IR 05000306/2002-002, Nuclear Management Company, Prairie Island Nuclear Generating Plant, Units 1 and 2, Resident Inspector Report. No Violations Identified
ML021090403
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 04/19/2002
From: Lanksbury R
Division Reactor Projects III
To: Nazar M
Nuclear Management Co
References
IR-02-002
Download: ML021090403 (25)


Text

April 19, 2002

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT NRC INSPECTION REPORT 50-282/02-02; 50-306/02-02

Dear Mr. Nazar:

On March 31, 2002, the NRC completed an inspection at your Prairie Island Nuclear Generating Plant. The enclosed report documents the inspection findings which were discussed on March 28, 2002, with you and members of your staff.

This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

No findings of significance were identified.

In accordance with 10 CFR 2.790 of the NRC's Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Roger D. Lanksbury, Chief Branch 5 Division of Reactor Projects Docket Nos. 50-282; 50-306 License Nos. DPR-42; DPR-60

Enclosure:

Inspection Report 50-282/02-02; 50-306/02-02 See Attached Distribution

DOCUMENT NAME: G:\\PRAI\\PRA2002002DRP.WPD To receive a copy of this document, indicate in the box "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RIII RIII RIII NAME MCastanedo:dtp Mkunowski RLanksbury DATE 04/19/02 04/19/02 04/19/02 OFFICIAL RECORD COPY

REGION III==

Docket Nos:

50-282; 50-306 License Nos:

DPR-42; DPR-60 Report No:

50-282/02-02; 50-306/02-02 Licensee:

Nuclear Management Company, LLC Facility:

Prairie Island Nuclear Generating Plant Location:

1717 Wakonade Drive East Welch, MN 55089 Dates:

February 15 through March 31, 2002 Inspectors:

S. Ray, Senior Resident Inspector D. Karjala, Resident Inspector Z. Dunham, Resident Inspector, Kewaunee M. Kunowski, Project Engineer J. Adams, Resident Inspector, Quad Cities Approved by:

Roger D. Lanksbury, Chief Branch 5 Division of Reactor Projects

SUMMARY OF FINDINGS IR 05000282-02-02; IR 05000306-02-02, on 2/15-3/31/2002; Nuclear Management Company, Prairie Island Nuclear Generating Plant, Units 1 & 2, Resident Inspector Report.

This report covers a 6-week routine resident inspection. The inspection was conducted by resident inspectors and a regional project engineer. No findings of significance were identified.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described at its Reactor Oversight Process website at http://www.nrc.gov/NRR/OVERSIGHT/ASSESS/index.html. Findings for which the SDP does not apply are indicated by No Color or by the severity level of the applicable violation.

A.

Inspector-Identified Findings No findings of significance were identified.

B.

Licensee-Identified Findings No findings of significance were identified.

Report Details Summary of Plant Status Unit 1 was operated at or near full power for the entire inspection period. Unit 2 was in a refueling outage until the reactor was brought critical on March 1, 2002. The Unit 2 generator was placed online on March 2 and reached full power on March 4, 2002. Unit 2 operated at or near full power for the remainder of the inspection period.

1.

REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01)

a.

Inspection Scope The inspectors observed operator actions and plant response during icing conditions that caused instabilities on the transmission grid. The inspection was conducted because the adverse weather conditions created the potential for a loss of offsite power and/or a reactor trip transient. Circuit breakers 8H7 and 8H8 opened in response to transmission line icing conditions, which isolated a Red Rock transmission line from the Prairie Island switchyard. The inspectors observed control room activities to verify that equipment responded as expected and that operator actions addressed the alarms and conditions in accordance with the procedures listed at the end of this report.

b.

Findings No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1 Train Walkdown a.

Inspection Scope The inspectors performed a partial walkdown of the D1 diesel generator while the D2 diesel generator was unavailable because of surveillance testing. The inspectors utilized the valve and electrical breaker status checklists listed at the end of the report to verify that components were properly positioned and that support systems were lined up to support diesel generator operation. The inspectors also examined the material condition of diesel generator components and valves and evaluated the general housekeeping of the D1 diesel generator room. The inspectors reviewed outstanding work orders (WOs) and condition reports (CRs) associated with the diesel to verify that these documents did not reveal issues that could affect train function. The inspectors used the information in the sections of the Updated Safety Analysis Report (USAR) and Technical Specifications (TSs) listed at the end of this report to determine the functional requirements of the system.

b.

Findings No findings of significance were identified.

.2 System Walkdown a.

Inspection Scope The inspectors walked down the accessible portions of the cooling water system in the turbine and auxiliary buildings. The inspectors utilized the system checklists and flow diagrams listed at the end of the report to verify that components were properly positioned. The inspectors also examined the material condition of the components.

The inspectors reviewed outstanding WOs and CRs associated with the system to verify that these documents did not reveal issues that could affect system function. The inspectors used the information in the sections of the USAR and TSs listed at the end of this report to determine the functional requirements of the system. The inspectors reviewed licensee records to verify that minor deficiencies identified during this inspection were entered into the corrective action system.

b.

Findings No findings of significance were identified.

1R05 Fire Protection (71111.05)

a.

Inspection Scope The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events (IPEEE), their potential to impact equipment which could initiate a plant transient, or their impact on the plants ability to respond to a security event. The inspectors used the documents listed at the end of this report to verify that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The following areas were inspected:



Fire Area 41A, Screenhouse Safeguards Area;



Fire Area 41B, Screenhouse Basement;



Fire Area 58, Auxiliary Building 695-foot elevation, Unit 1; and



Fire Area 73, Auxiliary Building 695-foot elevation, Unit 2.

b.

Findings No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a.

Inspection Scope The inspectors observed an operating crew during an as found requalification examination on the simulator. The inspectors evaluated crew performance in the areas of:



clarity and formality of communications;



ability to take timely actions in the safe direction;



prioritization, interpretation, and verification of alarms;



procedure use;



control board manipulations;



oversight and direction from supervisors; and



group dynamics.

Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the operations section work instructions (SWIs) listed at the end of this report and to the critical tasks listed in the exercise guide at the end of this report. The inspectors also compared simulator configurations with actual control room board configurations. For any weaknesses identified, the inspectors observed the licensee evaluators to verify that they also noted the issues and discussed them in the critique at the end of the session. For this examination, the licensee evaluators determined that the crew had failed because they did not properly perform one of the critical tasks, so the inspectors interviewed personnel and reviewed records to verify that actions were initiated to remediate the crew before they returned to duty.

b.

Findings No findings of significance were identified.

1R12 Maintenance Rule Implementation (71111.12)

a.

Inspection Scope The inspectors reviewed systems to verify that the licensee properly implemented the maintenance rule for structures, systems, or components (SSCs) with performance problems. This evaluation included the following aspects:



whether the SSC was scoped in accordance with 10 CFR 50.65;



whether the performance problems constituted maintenance rule functional failures;



the proper safety significance classification;



the proper 10 CFR 50.65(a)(1) or (a)(2) classification for the SSC; and



the appropriateness of the performance criteria for SSCs classified as (a)(2) or the appropriateness of goals and corrective actions for SSCs classified as (a)(1).

The above aspects were evaluated by using the maintenance rule scoping and report documents listed at the end of this report. For each SSC reviewed, the inspectors also reviewed significant WOs and CRs listed at the end of this report to verify that failures were properly identified, classified, and corrected and that unavailable time had been properly calculated. The inspectors reviewed documents to verify that minor discrepancies in the licensees maintenance rule reports were corrected.

The inspectors reviewed the licensees implementation of the maintenance rule requirements for the following SSCs:



Unit 2 auxiliary feedwater (AFW) system;



Unit 1 and Unit 2 cooling water system; and



Unit 2 condenser air removal system.

b.

Findings No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope The inspectors reviewed the licensees management of plant risk during emergent maintenance activities or during activities where more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety significant equipment. The inspection was conducted to verify that evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate. The licensees daily configuration risk assessment records, observations of shift turnover meetings, observations of daily plant status meetings, observations of shiftly outage meetings, and the documents listed at the end of this report were used by the inspectors to verify that the equipment configurations had been properly listed, that protected equipment had been identified and was being controlled where appropriate, and that significant aspects of plant risk were being communicated to the necessary personnel.

The inspectors reviewed the following emergent maintenance activities:



failure of the 22 containment spray (CS) pump breaker to close during the integrated safety injection test;



reduced seal return flow on the 22 reactor coolant pump (RCP); and



steam leak on high pressure turbine drain piping on Unit 2.

b.

Findings No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a.

Inspection Scope The inspectors evaluated plant conditions, selected CRs, and corrective action process (CAP) documents for risk significant components and systems in which operability issues were questioned. These conditions were evaluated to determine whether the operability of the components and systems was justified. The inspectors compared the operability and design criteria in the appropriate sections of the TS and USAR to the licensees evaluations presented in the CRs and documents listed at the end of this report to verify that the components or systems were operable. Where compensatory measures were necessary to maintain operability, the inspectors reviewed the documents listed at the end of the report to verify that the measures were in place, would work as intended, and were properly controlled.

The conditions evaluated were:



the licensees evaluation of steam generator level setpoint issues identified by Westinghouse Nuclear Safety Advisory Letters (NSALs); and



whether the liquid radwaste discharge monitor, R-18, could be considered operable when its ability to discriminate low level signals was questionable.

b.

Findings No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

a.

Inspection Scope The inspectors reviewed post-maintenance testing activities associated with maintenance on important mitigating, barrier integrity, and support systems to ensure that the testing adequately verified system operability and functional capability with consideration of the actual maintenance performed. The inspectors used the appropriate sections of the TSs and the USAR, as well as the documents listed at the end of this report, to evaluate the scope of the maintenance and to verify that the post-maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. In addition, the inspectors reviewed CAPs to verify that minor deficiencies identified during these inspections were entered into the licensees corrective action system.

Testing subsequent to the following activities was observed and evaluated:



the 12 diesel cooling water pump annual inspection;



decontamination of the sample chamber of the liquid radwaste discharge monitor R-18; and



draining and refilling the D5 diesel generator fuel oil day tank.

b.

Findings No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20)

a.

Inspection Scope The inspectors reviewed and/or observed activities associated with a Unit 2 refueling outage. The inspectors reviewed the outage plan and schedule to verify that risk had been appropriately considered, and evaluated how emergent work and changing plant conditions were handled from a risk control perspective. Among the significant outage activities the inspectors observed were the reactor coolant system (RCS) draindown to reduced inventory conditions for removal of the steam generator nozzle dams; and preparation for, and accomplishment of, mode changes from refueling through power operation; including heatup, securing of residual heat removal (RHR) cooling, reactor startup preparations, physics testing, and power ascension. Documents and procedures used in these reviews are listed at the end of this report. For each mode change, the inspectors reviewed the completed prerequisite checklists to ensure that TS requirements were met. The inspectors also conducted a containment cleanliness inspection near the end of the outage with emphasis on ensuring that no material was left in containment that could affect the flow to the containment recirculation sump. The inspectors also observed and/or reviewed several other miscellaneous outage activities.

The inspectors regularly reviewed the licensees shutdown risk assessment classification and its control of protected equipment when defense-in-depth equipment was unavailable, especially electrical power sources.

b.

Findings No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope The inspectors witnessed selected surveillance testing and/or reviewed test data to verify that the equipment tested using the surveillance procedures (SPs) met the TSs, the USAR, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in verifying mitigating systems capability and barrier integrity.

The inspectors used the documents listed at the end of this report to verify that the

testing met the TS frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded.

The following tests were observed and evaluated:



SP 2083, Unit 2 Integrated SI [safety injection] Test With a Simulated Loss of Offsite Power;



SP 2750, Post Outage Containment Close-Out Inspection; and



SP 2093, D5 Diesel Generator Monthly Slow Start Test and Coincident Opacity Testing.

b.

Findings No findings of significance were identified.

1R23 Temporary Modifications (71111.23)

a.

Inspection Scope The inspectors reviewed a temporary modification to remove one of the overspeed trip mechanisms on the D5 diesel generator. The inspectors reviewed the temporary modification description and the 10 CFR 50.59 screening form listed at the end of the report to ensure they were completed in accordance with the licensee administrative work instruction (AWI) guidance listed at the end of the report. In addition, the inspectors reviewed the listed section of the USAR and TSs to verify that the installation did not affect the specified design function or operability of the system. The inspectors also reviewed the installation and removal work orders listed at the end of the report and walked down the installation to insure the temporary equipment was installed in accordance with the plan. The inspectors also reviewed the control room transitional drawing file to ensure that the appropriate drawing had been updated to show the temporary modification.

b.

Findings No findings of significance were identified.

4.

OTHER ACTIVITIES 4OA1 Performance Indicator (PI) Verification (71151)

a.

Inspection Scope The inspectors reviewed the PI data submitted by the licensee for completeness and accuracy of the Safety System Unavailability PI for the RHR System in the Mitigating Systems Cornerstone. The inspectors compared the data reported by the licensee to the definitions and guidance contained in the Nuclear Energy Institute (NEI) guidance

listed at the end of this report. The inspectors reviewed electronic control room logs and limiting condition for operations logs for the first through fourth quarters of 2001 to verify the reported unavailable times. The inspectors also reviewed the CRs and WOs listed at the end of this report to identify any unavailability times that the licensee might have missed.

b.

Findings No findings of significance were identified.

4OA3 Event Followup (71153)

Inadvertent Train B SI Actuation on Unit 2 a.

Inspection Scope The inspectors observed control room personnel respond to an inadvertent Train B SI actuation on February 26, 2002, on Unit 2. Unit 2 was in the process of heatup and startup, and was at approximately 340 degrees Fahrenheit at the end of its refueling outage when the actuation occurred. The inspectors responded to the control room and conducted control panel walkdowns to verify that all Train B engineered safeguards equipment had responded as expected. The inspectors also observed operator response actions to diagnose the event, stabilize the plant, and recover. The event resulted in the operators tripping the only operating decay heat removal system. There was no RCS heatup, at the time, due to the injection of relatively cool water by the 22 SI pump. The operators terminated the injection before the pressurizer was filled so pressure control was never lost. Because the event did not result in any adverse reactor conditions and all mitigating equipment responded as expected, this event was considered to be of minor safety significance.

Several issues were raised by both the inspectors and licensee personnel regarding TS interpretation and compliance, the adequacy of the emergency procedures for the unusual plant conditions, and reporting requirements. Each of the issues was entered into the licensees corrective action system using the CRs listed at the end of this report.

The licensee concluded that the actuation was invalid and was caused by an electrical maintenance technician accidently shorting two contacts with a test equipment lead.

The inspectors reviewed the electrical drawings listed at the end of the report with licensee engineering personnel to verify that the licensees conclusions regarding the cause of the actuation were reasonable and would have led to the plant response experienced. The licensee intended to report the event as either a written Licensee Event Report (LER) or optional 60-day telephone report to the NRC.

b.

Findings No findings of significance were identified.

4OA6 Meeting(s)

Exit Meeting The resident inspectors presented the inspection results to Mr. and other members of licensee management at the conclusion of the inspection on March 28, 2002. The licensee acknowledged the findings presented. No proprietary information was identified.

KEY POINTS OF CONTACT Licensee T. Breene, Manager Nuclear Performance Assessment B. Jefferson, Director Site Operations A. Johnson, General Superintendent Radiation Protection and Chemistry R. Lingle, Operations Manager J. Maki, Production Planning Manager L. Meyer, General Superintendent Plant Maintenance M. Nazar, Site Vice President J. Waddell, Superintendent Security M. Werner, Plant Manager L. Williams, Director of Engineering LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened None Closed None Discussed None

LIST OF ACRONYMS USES ADAMS Agencywide Documents Access and Management System AFW Auxiliary Feedwater ARP Alarm Response Procedure AWI Administrative Work Instruction CAP Corrective Action Process CFR Code of Federal Regulations CR Condition Report CS Containment Spray IMC Inspection Manual Chapter IPEEE Individual Plant Examination of External Events IR

Inspection Report

KV

Kilovolt

LER

Licensee Event Report

NEI

Nuclear Energy Institute

NRC

Nuclear Regulatory Commission

NSAL

Nuclear Safety Advisory Letter

NSSS

Nuclear Steam Supply System

PARS

Publicly Available Records

PI

Performance Indicator

PM

Preventive Maintenance

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RHR

Residual Heat Removal

SDP

Significance Determination Process

SI

Safety Injection

SP

Surveillance Procedure

SSC

Structure, System, or Component

SWI

Section Work Instruction

TS

Technical Specification

USAR

Updated Safety Analysis Report

WO

Work Order

LIST OF DOCUMENTS REVIEWED

1R01

Adverse Weather Protection

CR 200202426

Received Undervoltage Alarms on Bus 11 &

Bus 12

Alarm Response

Procedure (ARP) C47005-

0201

Bus 11 4.16KV [kilovolts] Undervoltage

Revision 11

ARP C47005-0202

Bus 12 4.16KV Undervoltage

Revision 11

ARP C47022-0610

Fire Detection Panel FP121 Trouble Alarm

Revision 29

ARP C47023-0601

Substation Local Alarm

Revision 31

ARP C47024-0704

Bus 16 Sequencer Channel Alert

Revision 34

ARP C47507-0303

Hydrogen and Seal Oil Local Alarm

Revision 20

ARP C47508-0509

NSSS [Nuclear Steam Supply System]

Annunciator System Power Failure

Revision 22

ARP C47524-0701

Bus 25 Sequencer Channel Alert

Revision 34

ARP C47524-0704

Bus 26 Load Sequencer Channel Alert

Revision 34

1R04

Equipment Alignment

D1 Diesel Generator

Integrated Checklist

C1.1.20.7-1

D1 Diesel Generator Valve Status

Revision 17W

Integrated Checklist

C1.1.20.7-2

D1 Diesel Generator Auxiliaries and Room

Cooling Local Panels

Revision 8W

Integrated Checklist

C1.1.20.7-3

Diesel Generator D1 Main Control Room

Switch and Indicating Light Status

Revision 13

Integrated Checklist

C1.1.20.7-4

D1 Diesel Generator Circuit Breakers and

Panel Switches

Revision 11

USAR Section 8.4

Plant Standby Diesel Generator Systems

Revision 23

TS 3.7

Auxiliary Electrical System

Revision 160

TS 4.6

Periodic Testing of Emergency Power

System

Revision 147

Cooling Water System

CR 20005789

Flow Element FE-27024 Was Removed

Prior to Design Change Approval

CR 20015676

Obtain Approval for Design Change and

Implement Modification

WO 9701104

Remove Flow Element and Plug Fitting

WO 0007825

Valve Is Hard To Operate

USAR Section 10.4.1

Cooling Water System

Revision 22

TS 3.3.D

Cooling Water System

Revision 131

Abnormal Operating

Procedure C35 AOP4

Cooling Water Leakage in Containment

Revision 8

Integrated Checklist

C1.1.35-1

Cooling Water System Unit One

Revision 8

Integrated Checklist

C1.1.35-2

Cooling Water System Unit 2

Revision 8

Drawing NF-39216-1

Flow Diagram Unit 1 & 2 Cooling Water -

Screenhouse

Revision AD

Drawing NF-39216-2

Flow Diagram Unit 1 Cooling Water -

Turbine Building

Revision X

Drawing NF-39216-3

Flow Diagram - Unit 1 Cooling Water -

Auxiliary Building

Revision R

Drawing NF-39216-4

Flow Diagram Unit 1 Cooling Water -

Containment

Revision F

Drawing NF-39217-1

Flow Diagram Unit 2 Cooling Water -

Turbine Building

Revision X

Drawing NF-39217-2

Flow Diagram Unit 2 Cooling Water -

Auxiliary Building

Revision S

Drawing NF-39217-3

Flow Diagram Unit 2 Cooling Water -

Containment

Revision C

Drawing NF-39255-1

Diesel Generators D1 & D2 Units 1 and 2

Flow Diagram

Revision Z

CAP000090

Work Request Sticker Was Not Removed

When Work Order 0110644 Was Canceled

1R05

Fire Protection

Plant Safety Procedure F5

Fire Fighting

Revision 27

Plant Safety Procedure F5

Appendix F

Fire Hazard Analysis

Revision 12

Plant Safety Procedure F5

Appendix D

Impact of Fire Outside Control/Relay Room

Revision 8

Plant Safety Procedure F5

Appendix A

Fire Strategies

Revision 7

IPEEE NSPLMI-96001

Appendix B

Internal Fires Analysis

Revision 2

1R011 Licensed Operator Requalification Program

Lesson Plan P9160S-001

Simulator Cycle Quiz #35

Revision 1

SWI O-0

Conduct of Operations

Revision 1

SWI O-2

Shift Organization, Operations, and

Turnover

Revision 46

SWI O-10

Operation Manual Usage

Revision 41

SWI O-25

Periodic Data Acquisition and Logkeeping

Revision 29

1R12

Maintenance Rule Implementation

General

2000 Equipment Performance Annual

Report

April 20, 2001

Maintenance Rule System Basis Document,

Volume 1A

Revision 3

Maintenance Rule System Basis Document,

Volume 1B, Cooling Water Section

Revision 3

Quarterly Equipment Performance Report -

4th Quarter 2001 (draft)

February 2002

NUMARC 93-01

Nuclear Energy Institute Industry Guideline

for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants

Revision 2

Regulatory Guide 1.160

Monitoring the Effectiveness of Maintenance

at Nuclear Power Plants

Revision 2

Unit 2 AFW System

CR 20014863

Control Valve CV-31419 Did Not Open

Within Reference Range

CR 20017083

Entered Unplanned Limiting Condition for

Operation Action Due to 22 Turbine-Driven

AFW Pump Recirculation Control Valve CV-

31419 Failure to Open During SP-2102

CR 20017776

Replace AFW Pump

Recirulation/Lubricating Oil Solenoid Valves

With Models Having Elastomers Rated for

Higher Temperature

CR 20017971

Modify AFW Systems to Remove the

Recirulation/Lubricating Oil Cooling Control

Valves

CR 200186464

Implement Periodic Inspection and/or

Replacement of AFW Recirculation

Solenoid Valve Elastomeric Seats

CR 200200675

Develop an Action Plan for Returning the

AFW System to Maintenance Rule a(2)

Status

WO 0110640

Solenoid Valve SV-33493 Did Not Vent

Completely Off

WO 0111809

Fail Open AFW Recirculation Control Valve

CV-31418

WO 0111811

Fail Open AFW Recirculation Control Valve

CV-31419

Unit 1 and Unit 2 Cooling Water

CR 20004776

Cooling Water Vertical Cooling Water Pump

Bearing Lubricating Supply Downgrade to

Non Quality

CR 200186350

Re-examine the Revised Root Cause

Evaluation for the Cooling Water White

Finding

CR 200200677

Develop Action Plan to Return the Cooling

Water System to a(2)

Unit 2 Air Removal System

CR 20014153

At 24 Megawatts During Performance of

2C1.3, Unit 2 Turbine Was Manually

Tripped Due to High Condenser Differential

Pressure of 2.5 Inches With Vacuum

Decreasing

CR 200185657

Manual Reactor Trip Due to Condenser

Vacuum Differential Greater Than 2.5

Inches

LER 2-01-04

Manual Turbine Trip/Reactor Trip Due to

High Differential Condenser Backpressure

Original

LER 2-01-05

Manual Reactor Trip on Unit 2, Initiated in

Response to a High Differential Pressure

Between the Turbine Steam Condensers,

Caused by an Inadvertent Venting of One

Condenser While Isolating a Steam Leak

Original

1R13

Maintenance Risk Assessments and Emergent Work Control

CS Breaker Issue

WO 0104847

Perform PM [Preventive Maintenance] on

Breaker 26-9 CS Pump

WO 0201793

Troubleshoot Cause of 22 CS Pump Not

Starting

CR 200201895

During Preparations for SP 2083 Breaker

26-9 22 CS Pump Failed to Close from

Relay 2CS-20X and from CS-46561

Electrical Maintenance

Procedure PE 0007

5HK250/350 Breaker Testing Maintenance

& Repair - Minor

Revision 1

22 RCP Seal Issue

CR 200202073

22 RCP Number 1 Seal Leak-Off Flow Rate

Decreased Below 0.8 Gallons Per Minute

During Startup on 2/27/02 - Evaluate Low

Leak-Off Flow Rate

WO 0201940

Start 22 RCP With Enhanced Monitoring

WO 0201921

Provide a 2nd Balance Shot for 22 RCP

WO 0201937

Start/Stop the 22 RCP Oil Lift Pump

WO 0201966

22 RCP Seal Replacement Per D15.1 [this

WO was written as a contingency]

Abnormal Operating

Procedure 2C3 AOP3

Failure of a Reactor Coolant Pump Seal

Revision 8

Temporary Change Notice

2002-0901 to 2C3 AOP3

Failure of a Reactor Coolant Pump Seal

Project Plan

22 Reactor Coolant Pump Seal Leak-Off

Issues

March 1, 2002

P. Huffman Memorandum

Low Leak-Off RCP Seal Concern

March 5, 2002

High Pressure Steam Leak Issue

D. Herling Memorandum

Contingency Actions for Unit 2 High

Pressure Steam Leak

March 4, 2002

P. Huffman Memorandum

Unit 2 Turbine Drain Steam Leak

March 4, 2002

J. Loesch Memorandum

Steam Leak Safety Requirements

March 4, 2002

Temporary Modification

02T122

Furmanite Repair on Turbine CV-3 Drain

Loop

WO 0202013

Install Furmanite Box on Turbine CV-3 Drain

Loop

Maintenance Procedure

D93

On-Line Leak Sealing

Revision 9

1R15

Operability Evaluations

Steam Generator Level Issues

CR 200201616

NSAL 02-3 Steam Generator Narrow Range

Level Offset Due to Mid-Deck Plate

Pressure Loss

CR 200201692

Steam Generator Mid-Deck Plate Pressure

Loss Issue

CR 200201822

Maximum Reliable Indicated Steam

Generator Water Level

CR 200201823

Steam Generator Water Level Control

System Uncertainty Issue

Westinghouse NSAL-02-3

Steam Generator Mid-Deck Plate Pressure

Loss Issue

February 18, 2002

Westinghouse NSAL-02-4

Maximum Reliable Indicated Steam

Generator Water Level

February 19, 2002

Westinghouse NSAL-2-5

Steam Generator Water Level Control

System Uncertainty Issue

February 19, 2002

SP 1002A

Analog Protection System Calibration

Revision 26

TS 2.3

Limiting Safety System Setting, Protective

Instrumentation

Revision 91

USAR Section 7.4.1

Reactor Protection System

Revision 23

R-18 Radiation Monitor

CAP000026

Evaluate Low End Bug Point Check for R-18

USAR Section 7.5.2.12

Waste Disposal System Liquid Effluent

Monitor (R-18)

Revision 23

Operating Procedure C11

Radiation Monitoring System

Revision 20

Operations Manual B11

Radiation Monitoring System

Revision 5

H Procedures H4

Offsite Dose Calculation Manual, Section

2.0, Liquid Effluents

Revision 16

USAR Section 9.2

Liquid Radwaste System

Revision 23

TS 6.5.D

Radioactive Effluent Controls Program

Revision 147

1R19

Post Maintenance Testing

TS 3.3.D.

Cooling Water System

Revision 131

USAR Section 10.4.1

Cooling Water System

Revision 22

PM 3002-2-12

12 Diesel Cooling Water Pump Annual

Inspection

Revision 19

SP 1106A

12 Diesel Cooling Water Pump Monthly Test Revision 59

WO 0112416

R-18 Sample Chamber Decontamination

PM 3155-3

R-18 Sample Chamber Decontamination

Revision 4W

USAR Section 7.5.2.12

Waste Disposal System Liquid Effluent

Monitor (R-18)

Revision 23

USAR Section 9.2

Liquid Radwaste System

Revision 23

TS 6.5.D

Radioactive Effluent Controls Program

Revision 147

SP 2093

D5 Diesel Generator Monthly Slow Start

Test

Revision 69

WO 0202003

Perform D5 Opacity Test

5AWI 15.4.0

Minor Maintenance Program

Revision 0

Maintenance Procedure

D18

Equipment Lubrication

Revision 54

TS 3.7

Auxiliary Electrical Systems

Revision 160

TS 4.6

Periodic Testing of Emergency Power

Systems

Revision 147

USAR Section 8.4

Plant Standby Diesel Generator Systems

Revision 23

CAP000100

Level in D5 Turbocharger Lowered Without

Proper Documentation or Work Control

1R20

Refueling and Other Outage Activities

Operating Procedure

2C1.6

Shutdown Operations - Unit 2

Revision 13

Operating Procedure

2C4.2

RCS Inventory Control - Post Refueling

Revision 13

Operating Procedure

2C1.4

Unit 2 Power Operation

Revision 27

Operating Procedure

2C1.2

Unit 2 Startup Procedure

Revision 25

Special Operating

Procedure 2D2

RCS Reduced Inventory Operation

Revision 13

PM 3132-1-22

22 Turbine-Driven Aux Feed Pump

Refueling Inspection

Revision 33

SP 2102

22 Turbine-Driven AFW Pump Monthly Test

Revision 68

SP 2330

22 Turbine-Driven AFW Turbine/Pump

Bearing Temperature Test

Revision 7

Maintenance Procedure

D30

Post Refueling Startup Testing

Revision 34

Maintenance Procedure

D32

Temperature Coefficient Measurement at

Hot Zero Power

Revision 10

Maintenance Procedure

D34

Boron Endpoint Measurement

Revision 8

1R22

Surveillance Testing

SP 2083

Unit 2 Integrated SI Test With a Simulated

Loss of Offsite Power

Revision 24

WO 0201775

Test SP 2083 Exceptions 22 Fan Cooler

Unit and Containment Cooling System

Valves

WO 0201805

Test SP 2083 Exceptions 22 Fan Cooler

Unit Load Reject/Restore

TS 4.5.A

Engineered Safety Features System Tests

Revision 161

SP 2750

Post Outage Containment Close-Out

Inspection

Revision 22

SP 2093

D5 Diesel Generator Monthly Slow Start

Test

Revision 69

WO 0201925

Add Fuel Additive for Opacity Testing on D5

Safety Evaluation

Screening 1164

WO #0201925 to Perform Additive Test

Revision 0

TS 4.6

Periodic Testing of Emergency Power

Systems

Revision 147

1R23

Temporary Modifications

5AWI 6.5.0

Temporary Modifications

Revision 11

Temporary Modification

02T113

Bypass and Isolate the Function of a Failed

Field Flash Speed Switch or a Failed

Overspeed Switch

WO 0201073

Isolate Overspeed Trip Device or Field

Flash Speed Switch

WO 0201074

Remove Overspeed Trip Device or Field

Flash Speed Switch Temporary Modification

Controlled Transitional

File Drawing NE 118250

Flow Diagram Unit 2 Starting Air Diesel

Generator D5

Revision B

USAR Section 8.4

Plant Standby Diesel Generator Systems

Revision 23

TS 3.7

Auxiliary Electrical Systems

Revision 160

TS 4.6

Periodic Testing of Emergency Power

Systems

Revision 147

USAR Section 8.4

Plant Standby Diesel Generator Systems

Revision 23

4OA1 Performance Indicator Verification

NEI 99-02

Regulatory Assessment Performance

Indicator Guideline

Revision 2

Electronic Control Room Logs

1/1/2001-

12/31/2001

Electronic Limiting Conditions for

Operations Logs

1/1/2001-

12/31/2001

WO 0107626

Replace 22 RHR Pump Seal - Inspect and

Replace Studs and Nuts

CR 20014785

22 RHR Pump Seal Leaking

4OA3 Event Followup

USAR Section 6

Engineered Safety Features

Revision 23

CR 200202010

Manual Trip of 21 RCP Due to Loss of Seal

Water Return Following Train B SI Signal

While 22 RCP Isolated

CR 200202013

During SP 2373 Reactor Trip and Bypass

Breaker Contacts Inadvertent SI Occurred

During Step 7.6.1 - Worker Brushed Wrong

Contacts

CR 20020216

Review Application of TS 3.1.A.1.c on

2/26/02 With 21 RCP On, 22 RCP Out of

Service, and RHR Aligned for Injection

CR 20020217

TS 3.1.A.1.c Is Not Clear Regarding

Required Actions When One RCP Is

Stopped (Operable) With One RCP

Inoperable

CR 200202015

Operators Deviated from E-0 and ES-0.2

Following Inadvertent SI Due to Plant

Conditions Not Meeting SI Termination

Criteria

Emergency Operating

Procedure 2E-0

Reactor Trip or Safety Injection

Revision 19

Emergency Subprocedure

2ES-0.2

SI Termination

Revision 18

TS 3.1

Reactor Coolant System

Drawing X-HIAW-1001-

885-10

Feedwater Isolation Safeguards System

Unit 1 & 2

Revision E

Drawing X-HIAW-1001-

885-7

Safety Injection Scheme

Revision J

Drawing X-HIAW-1001-

885-16

Safeguards Logic Cabinets

Revision B

Drawing X-HIAW-1-242

Safeguards Actuation Signals Logic

Diagrams

Revision E