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Category:Letter type:LR
MONTHYEARLR-N23-0065, Submittal of 2023 Annual 10 CFR 50.46 Report2023-10-0202 October 2023 Submittal of 2023 Annual 10 CFR 50.46 Report LR-N23-0045, and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement2023-09-0808 September 2023 and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement LR-N23-0052, Retest Schedule for Drywell to Suppression Chamber Vacuum Breakers Per Technical Specification 4.6.2.12023-07-31031 July 2023 Retest Schedule for Drywell to Suppression Chamber Vacuum Breakers Per Technical Specification 4.6.2.1 LR-N23-0042, Spent Fuel Cask Registration2023-07-12012 July 2023 Spent Fuel Cask Registration LR-N23-0046, Emergency Plan Document Revisions Implemented June 28, 20232023-07-10010 July 2023 Emergency Plan Document Revisions Implemented June 28, 2023 LR-N23-0034, 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station2023-04-27027 April 2023 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station LR-N23-0035, 2022 Annual Radioactive Effluent Release Report (ARERR)2023-04-27027 April 2023 2022 Annual Radioactive Effluent Release Report (ARERR) LR-N23-0010, License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location2023-04-21021 April 2023 License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location LR-N23-0009, License Amendment Request (LAR) to Revise the Hope Creek Trip and Standby Auto-start Logic Associated with Safety Related Heating, Ventilation and Air Conditioning (HVAC) Trains2023-04-18018 April 2023 License Amendment Request (LAR) to Revise the Hope Creek Trip and Standby Auto-start Logic Associated with Safety Related Heating, Ventilation and Air Conditioning (HVAC) Trains LR-N23-0024, Submittal of Hope Creek Generating Station Technical Specification Bases Changes2023-03-29029 March 2023 Submittal of Hope Creek Generating Station Technical Specification Bases Changes LR-N23-0006, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-24024 March 2023 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations LR-N23-0019, and Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums2023-03-21021 March 2023 and Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums LR-N23-0016, and Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments2023-02-28028 February 2023 and Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments LR-N23-0018, Technical Specification 6.9.1.5.b - 2022 Annual Report of SRV Challenges2023-02-27027 February 2023 Technical Specification 6.9.1.5.b - 2022 Annual Report of SRV Challenges LR-N23-0012, Annual Property Insurance Status Report2023-02-24024 February 2023 Annual Property Insurance Status Report LR-N23-0014, Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.7172023-02-23023 February 2023 Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.717 LR-N23-0011, In-Service Inspection Activities - 90 Day Report: Twenty-Fourth Refueling Outage2023-01-19019 January 2023 In-Service Inspection Activities - 90 Day Report: Twenty-Fourth Refueling Outage LR-N22-0096, and Salem Generating Station, Units 1 and 2 - Request for Threshold Determination2023-01-0505 January 2023 and Salem Generating Station, Units 1 and 2 - Request for Threshold Determination LR-N22-0094, Emergency Plan Document Revisions Implemented November 21, 20222022-12-14014 December 2022 Emergency Plan Document Revisions Implemented November 21, 2022 LR-N22-0091, Independent Spent Fuel Storage Installation, Report of 10 CFR 72.48 Changes, Tests, and Experiments2022-12-0202 December 2022 Independent Spent Fuel Storage Installation, Report of 10 CFR 72.48 Changes, Tests, and Experiments LR-N22-0075, 2022 Annual 10 CFR 50.46 Report2022-09-30030 September 2022 2022 Annual 10 CFR 50.46 Report LR-N22-0074, Emergency Plan Evacuation Time Estimate2022-09-15015 September 2022 Emergency Plan Evacuation Time Estimate LR-N22-0051, License Amendment Request to Relocate Technical Specification Facility/Unit Staff Qualification Requirements to Quality Assurance Topical Report2022-06-22022 June 2022 License Amendment Request to Relocate Technical Specification Facility/Unit Staff Qualification Requirements to Quality Assurance Topical Report LR-N22-0044, Emergency Plan Document Revisions Implemented November, 20212022-05-19019 May 2022 Emergency Plan Document Revisions Implemented November, 2021 LR-N22-0041, 2021 Annual Radioactive Effluent Release Report (Rerr)2022-04-28028 April 2022 2021 Annual Radioactive Effluent Release Report (Rerr) LR-N22-0040, 2021 Annual Radiological Environmental Operating Report2022-04-28028 April 2022 2021 Annual Radiological Environmental Operating Report LR-N22-0039, Emergency Plan Document Revisions Implemented March 24, 20222022-04-21021 April 2022 Emergency Plan Document Revisions Implemented March 24, 2022 LR-N22-0023, Guarantees of Payment of Deferred Premiums2022-03-21021 March 2022 Guarantees of Payment of Deferred Premiums LR-N22-0017, Submittal of 2021 Annual Report of Fitness for Duty (FFD) Performance Data2022-02-25025 February 2022 Submittal of 2021 Annual Report of Fitness for Duty (FFD) Performance Data LR-N22-0016, Radiological Survey of Site Property to Be Used for Offshore Wind Port Facility2022-02-24024 February 2022 Radiological Survey of Site Property to Be Used for Offshore Wind Port Facility LR-N22-0019, Technical Specification 6.9.1.5.b 2021 Annual Report of SRV Challenges2022-02-24024 February 2022 Technical Specification 6.9.1.5.b 2021 Annual Report of SRV Challenges LR-N22-0011, Response to Request for Additional Information for License Amendment Request to Revise Technical Specification Limits for Ultimate Heat Sink2022-02-0101 February 2022 Response to Request for Additional Information for License Amendment Request to Revise Technical Specification Limits for Ultimate Heat Sink LR-N22-0005, Proposed Relief Request Associated with Reactor Pressure Vessel Water Level Instrumentation Partial Penetration Nozzle Repairs2022-01-0707 January 2022 Proposed Relief Request Associated with Reactor Pressure Vessel Water Level Instrumentation Partial Penetration Nozzle Repairs LR-N22-0007, Request for Exemption from Specific Requirements of 10 CFR Part 26, Fitness for Duty Programs2022-01-0505 January 2022 Request for Exemption from Specific Requirements of 10 CFR Part 26, Fitness for Duty Programs LR-N21-0087, Corrected Hope Creek 10 CFR 50.46 Reports2021-12-0202 December 2021 Corrected Hope Creek 10 CFR 50.46 Reports LR-N21-0078, Hope and Creek Generating Station, Supplement to License Amendment Request to Revise Technical Specifications (TS) to Delete Definitions Found in 10 CFR Part 20 and Delete Figures of the Site and Surrounding Areas from TS2021-11-18018 November 2021 Hope and Creek Generating Station, Supplement to License Amendment Request to Revise Technical Specifications (TS) to Delete Definitions Found in 10 CFR Part 20 and Delete Figures of the Site and Surrounding Areas from TS LR-N21-0081, Submittal of Updated Final Safety Analysis Report, Revision 25, Summary of Revised Regulatory Commitments2021-11-15015 November 2021 Submittal of Updated Final Safety Analysis Report, Revision 25, Summary of Revised Regulatory Commitments LR-N21-0056, License Amendment Request to Amend the Technical Specifications to Revise Surveillance Requirements for Electric Power Monitor Channels for the Reactor Protection System (RPS) and Power Range Neutron Monitoring System2021-11-0303 November 2021 License Amendment Request to Amend the Technical Specifications to Revise Surveillance Requirements for Electric Power Monitor Channels for the Reactor Protection System (RPS) and Power Range Neutron Monitoring System LR-N21-0079, Submittal of Hope Creek Generating Station Technical Specification Bases Changes2021-11-0303 November 2021 Submittal of Hope Creek Generating Station Technical Specification Bases Changes LR-N21-0071, 2021 Annual 10 CFR 50.46 Report2021-09-30030 September 2021 2021 Annual 10 CFR 50.46 Report LR-N21-0065, License Amendment Request - Revision of Salem and Hope Creek Generating Station Technical Specification (TS) to Delete Definitions Found in 10 CFR Part 20 and Delete Figures of the Site and Surrounding Areas from TS2021-09-29029 September 2021 License Amendment Request - Revision of Salem and Hope Creek Generating Station Technical Specification (TS) to Delete Definitions Found in 10 CFR Part 20 and Delete Figures of the Site and Surrounding Areas from TS LR-N21-0069, Emergency Plan Document Revisions Implemented August 10, 20212021-09-0909 September 2021 Emergency Plan Document Revisions Implemented August 10, 2021 LR-N21-0059, In-Service Inspection Activities - 90 Day Twenty-Third Refueling Outage2021-08-13013 August 2021 In-Service Inspection Activities - 90 Day Twenty-Third Refueling Outage LR-N21-0054, Correction to Prior Spent Fuel Cask Registration Letter2021-07-15015 July 2021 Correction to Prior Spent Fuel Cask Registration Letter LR-N21-0046, Submittal of Salem Generating Station Updated Final Safety Analysis Report, Revision 32, Summary of Revised Regulatory Commitments for Salem, 10 CFR 71.106 Review Results and 10 CFR 54.37(b) Review Results for Salem2021-06-17017 June 2021 Submittal of Salem Generating Station Updated Final Safety Analysis Report, Revision 32, Summary of Revised Regulatory Commitments for Salem, 10 CFR 71.106 Review Results and 10 CFR 54.37(b) Review Results for Salem LR-N21-0040, Response to Request for Additional Information SNSB-RAI 1 License Amendment Request to Revise Low Pressure Safety Limit to Address General Electric Part 21 Safety Communication2021-05-27027 May 2021 Response to Request for Additional Information SNSB-RAI 1 License Amendment Request to Revise Low Pressure Safety Limit to Address General Electric Part 21 Safety Communication LR-N21-0042, Core Operating Limits Report, Reload 23, Cycle 24, Revision 212021-05-24024 May 2021 Core Operating Limits Report, Reload 23, Cycle 24, Revision 21 LR-N21-0025, License Amendment Request to Revise Technical Specification Limits for Ultimate Heat Sink2021-05-0707 May 2021 License Amendment Request to Revise Technical Specification Limits for Ultimate Heat Sink LR-N21-0039, Deviation from EPRI Document 33002012244 Inspection Requirements2021-04-30030 April 2021 Deviation from EPRI Document 33002012244 Inspection Requirements LR-N21-0018, Response to Requests for Additional Information SNSB-RAI 2 and SNSB-RAI 3 License Amendment Request to Revise Low Pressure Safety Limit to Address General Electric Part 21 Safety Communication2021-04-29029 April 2021 Response to Requests for Additional Information SNSB-RAI 2 and SNSB-RAI 3 License Amendment Request to Revise Low Pressure Safety Limit to Address General Electric Part 21 Safety Communication 2023-09-08
[Table view] Category:Report
MONTHYEARML23335A1122023-12-15015 December 2023 Retest Schedule for Drywell to Suppression Chamber Vacuum Breakers ML23249A2622023-09-0606 September 2023 Attachment 1: PSEG Site Hourly Meteorological Data (2019 - 2021) LR-N21-0007, Report of Changes, Tests, and Experiments2021-01-28028 January 2021 Report of Changes, Tests, and Experiments ML20121A1332020-03-0303 March 2020 Biological Opinion 2019 Annual Incidental Take Report LR-N18-0056, Report of Full Compliance with Phase 1 and Phase 2 of June 6, 2013 Commission Order Modifying Licenses with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe Accident Conditions2018-07-25025 July 2018 Report of Full Compliance with Phase 1 and Phase 2 of June 6, 2013 Commission Order Modifying Licenses with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe Accident Conditions LR-N18-0057, Pressure and Temperature Limits Report, Revision 12018-06-0808 June 2018 Pressure and Temperature Limits Report, Revision 1 LR-N17-0163, License Amendment Request - Safety Limit Minimum Critical Power Ratio Change, Non-Proprietary2017-11-0909 November 2017 License Amendment Request - Safety Limit Minimum Critical Power Ratio Change, Non-Proprietary LR-N17-0092, Supplemental Information to License Amendment Request to Amend the Technical Specifications (TS) to Revise and Relocate the Pressure-Temperature Limit Curves to a Pressure and Temperature Limits Report2017-04-28028 April 2017 Supplemental Information to License Amendment Request to Amend the Technical Specifications (TS) to Revise and Relocate the Pressure-Temperature Limit Curves to a Pressure and Temperature Limits Report ML17188A2672017-03-31031 March 2017 Enclosure 12 to LR-N17-0044 and LAR H17-03 - Cameron Document ER-1132NP, Meter Factor Calculation and Accuracy Assessment for Hope Creek Nuclear Generating Station, Revision 2, (Non-Proprietary Version) LR-N17-0044, Enclosure 12 to LR-N17-0044 and LAR H17-03 - Cameron Document ER-1132NP, Meter Factor Calculation and Accuracy Assessment for Hope Creek Nuclear Generating Station, Revision 2, (Non-Proprietary Version)2017-03-31031 March 2017 Enclosure 12 to LR-N17-0044 and LAR H17-03 - Cameron Document ER-1132NP, Meter Factor Calculation and Accuracy Assessment for Hope Creek Nuclear Generating Station, Revision 2, (Non-Proprietary Version) LR-N17-0049, Submittal of Cycle 21 Summary of Report of Plant Startup in Accordance with the Requirements of Technical Specification 6.9.1.12017-02-0909 February 2017 Submittal of Cycle 21 Summary of Report of Plant Startup in Accordance with the Requirements of Technical Specification 6.9.1.1 LR-N17-0036, License Renewal Commitment Implementation, 90-Day Report for Refueling Outage 202017-02-0707 February 2017 License Renewal Commitment Implementation, 90-Day Report for Refueling Outage 20 ML17188A2652016-12-31031 December 2016 Enclosure 10 to LR-N17-0044 and LAR H17-03 - Cameron Document ER-1123NP, Bounding Uncertainty Analysis for Thermal Power Determination at Hope Creek, Unit 1 Nuclear Generating Station Using the LEFM System, Revision 2 (Non-Proprietary Versi LR-N17-0044, Enclosure 10 to LR-N17-0044 and LAR H17-03 - Cameron Document ER-1123NP, Bounding Uncertainty Analysis for Thermal Power Determination at Hope Creek, Unit 1 Nuclear Generating Station Using the LEFM System, Revision 2 (Non-Proprietary Ve2016-12-31031 December 2016 Enclosure 10 to LR-N17-0044 and LAR H17-03 - Cameron Document ER-1123NP, Bounding Uncertainty Analysis for Thermal Power Determination at Hope Creek, Unit 1 Nuclear Generating Station Using the LEFM System, Revision 2 (Non-Proprietary Versi LR-N16-0112, Flood Hazards Mitigating Strategies Assessment (MSA) Report Submittal2016-12-29029 December 2016 Flood Hazards Mitigating Strategies Assessment (MSA) Report Submittal ML16256A6412016-09-12012 September 2016 NUREG-0800, Appendix 18-A Assessment, Crediting Manual Operator Actions in the Diversity and Defense-in-Depth Analyses. LR-N16-0113, NUREG-0800, Appendix 18-A Assessment, Crediting Manual Operator Actions in the Diversity and Defense-in-Depth Analyses.2016-09-12012 September 2016 NUREG-0800, Appendix 18-A Assessment, Crediting Manual Operator Actions in the Diversity and Defense-in-Depth Analyses. ML16256A6422016-08-31031 August 2016 NED0-33872, Rev. 0, Hope Creek Generating Station Numac Prnm Upgrade Phase 2. ML16256A6402016-08-31031 August 2016 Hope Creek Power Range Neutron Monitoring Upgrade - Human Factors Engineering Assessment LR-N16-0113, NED0-33872, Rev. 0, Hope Creek Generating Station Numac Prnm Upgrade Phase 2.2016-08-31031 August 2016 NED0-33872, Rev. 0, Hope Creek Generating Station Numac Prnm Upgrade Phase 2. LR-N16-0113, Hope Creek Power Range Neutron Monitoring Upgrade - Human Factors Engineering Assessment2016-08-31031 August 2016 Hope Creek Power Range Neutron Monitoring Upgrade - Human Factors Engineering Assessment ML16256A6432016-07-18018 July 2016 ISG-06 Enclosure B Roadmap, Phase 2 Documents. LR-N16-0113, ISG-06 Enclosure B Roadmap, Phase 2 Documents.2016-07-18018 July 2016 ISG-06 Enclosure B Roadmap, Phase 2 Documents. LR-N16-0099, GNF-003N5734-R1-NP, Gnf Additional Information Regarding the Requested Changes to the Technical Specification SLMCPR Hope Creek Cycle 21.2016-05-31031 May 2016 GNF-003N5734-R1-NP, Gnf Additional Information Regarding the Requested Changes to the Technical Specification SLMCPR Hope Creek Cycle 21. ML16049A6092016-02-29029 February 2016 Staff Assessment of Information Provided Pursuant to Title 10 of the Code of Federal Regulations for Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-Ichi Accident and Staff Closure LR-N16-0113, NED0-33864, Rev. 0, Appendix B, Numac Systems Engineering Development Plan.2015-09-30030 September 2015 NED0-33864, Rev. 0, Appendix B, Numac Systems Engineering Development Plan. LR-N15-0178, NEDO-33864, Revision 0, Hope Creek Generating Station Numac Prnm Upgrade, (Non-Proprietary)2015-09-30030 September 2015 NEDO-33864, Revision 0, Hope Creek Generating Station Numac Prnm Upgrade, (Non-Proprietary) ML16256A6442015-09-30030 September 2015 NED0-33864, Rev. 0, Appendix B, Numac Systems Engineering Development Plan. LR-N14-0248, Response to March 12, 2012 Request for Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Re Recommendations of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident, Enclosure 5.2014-12-0909 December 2014 Response to March 12, 2012 Request for Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Re Recommendations of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident, Enclosure 5. ML15030A2942014-09-22022 September 2014 Table 03, Effluent Data Tritium Activity ML15030A2952014-09-22022 September 2014 Table 04, Groundwater Measurements and Elevations - First Quarter 2014 LR-N14-0175, CFR 71.95 Report for Packaging and Transporting a Shipping Cask (Model TN-RAM) Without Meeting a Required Condition in Certificate of Compliance 71-92332014-08-11011 August 2014 CFR 71.95 Report for Packaging and Transporting a Shipping Cask (Model TN-RAM) Without Meeting a Required Condition in Certificate of Compliance 71-9233 ML14176A9612014-06-24024 June 2014 Submittal of Non-Proprietary BWROG Technical Product, BWROGTP-11-006 - ECCS Containment Walkdown Procedure, Rev 1 (January 2011), as Formally Requested During the Public Meeting Held on April 30, 2014 LR-N14-0112, CFR 20.2206 Report - Apportion the 2013 Site Dose Between Salem and Hope Creek Station2014-04-25025 April 2014 CFR 20.2206 Report - Apportion the 2013 Site Dose Between Salem and Hope Creek Station LR-N14-0035, PSEG Nuclear Llc'S Seismic Hazard and Screening Report (CEUS Sites) Response to NRC Request for Information Pursuant to 10 CFR 50.54(f)Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima...2014-03-28028 March 2014 PSEG Nuclear Llc'S Seismic Hazard and Screening Report (CEUS Sites) Response to NRC Request for Information Pursuant to 10 CFR 50.54(f)Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima... ML13365A2532014-02-11011 February 2014 Interim Staff Evaluation Relating to Overall Integrated Plan in Response to Order EA-12-049 (Mitigation Strategies) ML14028A0742014-02-0606 February 2014 Mega-Tech Services, LLC Technical Evaluation Report Regarding the Overall Integrated Plan for Hope Creek Generating Station, TAC No. MF0867 LR-N14-0024, Report SL-011553, Revision 2, Response to the 50.54(f) Information Request Regarding Fukushima Near-Term Task Force Recommendation 2.3: Seismic2014-01-29029 January 2014 Report SL-011553, Revision 2, Response to the 50.54(f) Information Request Regarding Fukushima Near-Term Task Force Recommendation 2.3: Seismic ML13266A2972013-11-18018 November 2013 Audit Report Regarding Flooding Walkdowns to Support Implementation of Near-Term Task Force Recommendation 2.3 Related to the Fukushima Dai-Ichi Nuclear Power Plant Accident LR-N12-0366, Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Chapter 6 Through Chapter 92012-11-30030 November 2012 Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Chapter 6 Through Chapter 9 LR-N12-0366, Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Chapter 10 Through Appendix G2012-11-30030 November 2012 Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Chapter 10 Through Appendix G ML13052A6772012-11-30030 November 2012 Enclosure 1 to LR-N12-0366, Salem - Hope Creek Kld TR-499, Development of Evacuation Time Estimates, Cover Through Chapter 5 ML13052A6782012-11-30030 November 2012 Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Chapter 6 Through Chapter 9 ML13052A6792012-11-30030 November 2012 Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Chapter 10 Through Appendix G LR-N12-0366, Enclosure 1 to LR-N12-0366, Salem - Hope Creek Kld TR-499, Development of Evacuation Time Estimates, Cover Through Chapter 52012-11-30030 November 2012 Enclosure 1 to LR-N12-0366, Salem - Hope Creek Kld TR-499, Development of Evacuation Time Estimates, Cover Through Chapter 5 LR-N12-0366, Attachment to LR-N12-0366 - Study Kld TR-499, Rev 0 - 10CFR 50.54 (8) Summary2012-11-28028 November 2012 Attachment to LR-N12-0366 - Study Kld TR-499, Rev 0 - 10CFR 50.54 (8) Summary ML13052A6752012-11-28028 November 2012 Attachment to LR-N12-0366 - Study Kld TR-499, Rev 0 - 10CFR 50.54 (8) Summary ML13052A6802012-11-28028 November 2012 Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Appendix H Through Appendix J ML13052A6812012-11-28028 November 2012 Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Appendix K-1 Through K-75 ML13052A6822012-11-28028 November 2012 Kld TR-499, Revision 0, Development of Evacuation Time Estimates, Appendix K-76 Through K-149 2023-09-06
[Table view] Category:Miscellaneous
MONTHYEARML23335A1122023-12-15015 December 2023 Retest Schedule for Drywell to Suppression Chamber Vacuum Breakers LR-N21-0007, Report of Changes, Tests, and Experiments2021-01-28028 January 2021 Report of Changes, Tests, and Experiments LR-N18-0056, Report of Full Compliance with Phase 1 and Phase 2 of June 6, 2013 Commission Order Modifying Licenses with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe Accident Conditions2018-07-25025 July 2018 Report of Full Compliance with Phase 1 and Phase 2 of June 6, 2013 Commission Order Modifying Licenses with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe Accident Conditions LR-N17-0049, Submittal of Cycle 21 Summary of Report of Plant Startup in Accordance with the Requirements of Technical Specification 6.9.1.12017-02-0909 February 2017 Submittal of Cycle 21 Summary of Report of Plant Startup in Accordance with the Requirements of Technical Specification 6.9.1.1 LR-N17-0036, License Renewal Commitment Implementation, 90-Day Report for Refueling Outage 202017-02-0707 February 2017 License Renewal Commitment Implementation, 90-Day Report for Refueling Outage 20 LR-N16-0112, Flood Hazards Mitigating Strategies Assessment (MSA) Report Submittal2016-12-29029 December 2016 Flood Hazards Mitigating Strategies Assessment (MSA) Report Submittal ML16256A6412016-09-12012 September 2016 NUREG-0800, Appendix 18-A Assessment, Crediting Manual Operator Actions in the Diversity and Defense-in-Depth Analyses. LR-N16-0113, NUREG-0800, Appendix 18-A Assessment, Crediting Manual Operator Actions in the Diversity and Defense-in-Depth Analyses.2016-09-12012 September 2016 NUREG-0800, Appendix 18-A Assessment, Crediting Manual Operator Actions in the Diversity and Defense-in-Depth Analyses. ML16256A6402016-08-31031 August 2016 Hope Creek Power Range Neutron Monitoring Upgrade - Human Factors Engineering Assessment LR-N16-0113, Hope Creek Power Range Neutron Monitoring Upgrade - Human Factors Engineering Assessment2016-08-31031 August 2016 Hope Creek Power Range Neutron Monitoring Upgrade - Human Factors Engineering Assessment ML16256A6432016-07-18018 July 2016 ISG-06 Enclosure B Roadmap, Phase 2 Documents. LR-N16-0113, ISG-06 Enclosure B Roadmap, Phase 2 Documents.2016-07-18018 July 2016 ISG-06 Enclosure B Roadmap, Phase 2 Documents. LR-N16-0099, GNF-003N5734-R1-NP, Gnf Additional Information Regarding the Requested Changes to the Technical Specification SLMCPR Hope Creek Cycle 21.2016-05-31031 May 2016 GNF-003N5734-R1-NP, Gnf Additional Information Regarding the Requested Changes to the Technical Specification SLMCPR Hope Creek Cycle 21. ML16049A6092016-02-29029 February 2016 Staff Assessment of Information Provided Pursuant to Title 10 of the Code of Federal Regulations for Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-Ichi Accident and Staff Closure LR-N14-0248, Response to March 12, 2012 Request for Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Re Recommendations of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident, Enclosure 5.2014-12-0909 December 2014 Response to March 12, 2012 Request for Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Re Recommendations of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident, Enclosure 5. LR-N14-0175, CFR 71.95 Report for Packaging and Transporting a Shipping Cask (Model TN-RAM) Without Meeting a Required Condition in Certificate of Compliance 71-92332014-08-11011 August 2014 CFR 71.95 Report for Packaging and Transporting a Shipping Cask (Model TN-RAM) Without Meeting a Required Condition in Certificate of Compliance 71-9233 LR-N14-0112, CFR 20.2206 Report - Apportion the 2013 Site Dose Between Salem and Hope Creek Station2014-04-25025 April 2014 CFR 20.2206 Report - Apportion the 2013 Site Dose Between Salem and Hope Creek Station LR-N14-0035, PSEG Nuclear Llc'S Seismic Hazard and Screening Report (CEUS Sites) Response to NRC Request for Information Pursuant to 10 CFR 50.54(f)Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima...2014-03-28028 March 2014 PSEG Nuclear Llc'S Seismic Hazard and Screening Report (CEUS Sites) Response to NRC Request for Information Pursuant to 10 CFR 50.54(f)Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima... ML13266A2972013-11-18018 November 2013 Audit Report Regarding Flooding Walkdowns to Support Implementation of Near-Term Task Force Recommendation 2.3 Related to the Fukushima Dai-Ichi Nuclear Power Plant Accident ML13052A6752012-11-28028 November 2012 Attachment to LR-N12-0366 - Study Kld TR-499, Rev 0 - 10CFR 50.54 (8) Summary LR-N12-0366, Attachment to LR-N12-0366 - Study Kld TR-499, Rev 0 - 10CFR 50.54 (8) Summary2012-11-28028 November 2012 Attachment to LR-N12-0366 - Study Kld TR-499, Rev 0 - 10CFR 50.54 (8) Summary ML12220A2502012-08-10010 August 2012 Closeout of Bulletin 2011-01, Mitigating Strategies ML12159A3552012-06-0808 June 2012 Review of 60-day Response to Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 9.3 of the Near Term Task Force Review of Fukushima Dai-ichi Accident ML1127000692011-09-26026 September 2011 Enclosure 2, Mfn 10-245 R4, Description of the Evaluation and Surveillance Recommendations for BWR/2-5 Plants ML11203A0782011-07-13013 July 2011 Independent Spent Fuel Storage Installation, 10 CFR 72.212 Evaluation Report, Revision 6 LR-N11-0090, 2010 10 CFR 20.2206 Report - Apportion the 2010 Site Dose Between Salem and Hope Creek Stations2011-04-0808 April 2011 2010 10 CFR 20.2206 Report - Apportion the 2010 Site Dose Between Salem and Hope Creek Stations ML11061A0052011-03-30030 March 2011 Ncsa Hope Creek Observations Rev. 4 LR-N10-0355, Salem, EAL Technical Bases Supporting Documents2010-10-14014 October 2010 Salem, EAL Technical Bases Supporting Documents ML1100602392010-10-14014 October 2010 Salem, EAL Technical Bases Supporting Documents ML11263A0302010-09-20020 September 2010 E-mail with Attachment from B. Pham, NRR to L. Perkins, NRR, on Forward Salem/Hope Creek Chapter 5 SAMA Input ML11263A0282010-09-16016 September 2010 E-mail with Attachment from T. Ghosh, NRR, to C. Eccleston, NRR Et Al, on Reaction Hope Creek SAMA Transmittal Memo LR-N10-0306, 50.59 Review Coversheet Form for Hope Creek Unit 1 DCP 80102144, Revise Dose Analysis Calculations & Update UFSAR to Remove 120 Second Isolation Time for Pciv'S2010-08-10010 August 2010 50.59 Review Coversheet Form for Hope Creek Unit 1 DCP 80102144, Revise Dose Analysis Calculations & Update UFSAR to Remove 120 Second Isolation Time for Pciv'S LR-N09-0206, Special Report - North Plant Vent Radiation Monitoring System (Rms)2009-08-24024 August 2009 Special Report - North Plant Vent Radiation Monitoring System (Rms) LR-N08-0224, Attachments 3 and 4 - Hope Creek Extended Power Uprate Power Ascension Test Report and Affidavit2008-10-31031 October 2008 Attachments 3 and 4 - Hope Creek Extended Power Uprate Power Ascension Test Report and Affidavit ML0831008272008-10-31031 October 2008 Attachments 3 and 4 - Hope Creek Extended Power Uprate Power Ascension Test Report and Affidavit LR-N08-0247, Stations, Report of HHS-Certified Laboratory Testing Error Investigation and Corrective Action2008-10-30030 October 2008 Stations, Report of HHS-Certified Laboratory Testing Error Investigation and Corrective Action ML0826005732008-09-0202 September 2008 NFS-0255, Revision 0, Hope Creek Generating Station - Initial Implementation of WCAP-15942-P-A (Formerly CENO-287), Fuel Assembly Mechanical Design Methodology for Boiling Water Reactors Supplement to CENP-287, Evaluation of Control Blade I ML0732300962007-11-0909 November 2007 Discharge Confirmation Report - Retraction of Reported Discharge to the Delaware River HCH-2007-052, Notice of Noncompliance and Affirmative Defense of Laboratory Error2007-05-23023 May 2007 Notice of Noncompliance and Affirmative Defense of Laboratory Error LR-N07-0040, Special Report - North Plant Vent Radiation Monitoring System (Rms)2007-02-20020 February 2007 Special Report - North Plant Vent Radiation Monitoring System (Rms) LR-N06-0401, Submittal of 10CFR50.46 Report Regarding Changes in the Application of the Emergency Core Cooling System Evaluation Models2006-09-28028 September 2006 Submittal of 10CFR50.46 Report Regarding Changes in the Application of the Emergency Core Cooling System Evaluation Models ML0626900642006-09-0101 September 2006 Attachment 26, C.D.I. Report No. 06-16NP, Rev 1, Estimating High Frequency Flow Induced Vibration in the Main Stream Lines at Hope Creek Unit 1: a Subscale Four Line Investigation of Standpipe Behavior. ML0622805562006-07-27027 July 2006 Groundwater Protection - Data Collection Questionnaire LR-N06-0216, Letter to Samuel Collins, Dtd May 04, 2006, from PSEG (LR-N06-0216) Regarding Safety Conscious Work Environment Peer Assessment Report2006-05-0404 May 2006 Letter to Samuel Collins, Dtd May 04, 2006, from PSEG (LR-N06-0216) Regarding Safety Conscious Work Environment Peer Assessment Report ML0607204372006-03-0707 March 2006 Redacted Response to Request for Information Regarding Executive Review Board Commitments; PSEG ML0606703012006-02-0707 February 2006 PSEG-News Document Detailing Chris Bakken Will Succeed Anderson as President and CNO of PSEG Nuclear ML0605801622006-02-0101 February 2006 Performance Themes for Use After Inspection Exits (Regarding Poor Equipment Reliability, Corrective Action Ineffectiveness) and Organizational Issues (Regarding Engineering, Maintenance & Work Control, Operations, and Licensing/Regulatory C ML0524901582005-08-31031 August 2005 Allegation Receipt Report Regarding Facility: Hope Creek ML0526302272005-08-23023 August 2005 Communication Plan & Notification Sequence Regarding Receipt & Docketing of PSEG Assessment Reports ML0531803762005-04-30030 April 2005 NEDO-33186, Revision 1, MELLLA Tracg Divom Evaluation for Hope Creek at Cppu Conditions. 2023-12-15
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PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 0 PSEG 1Vuclear LLC FOL 2.C. (27)
LR-N17-0036 FEB 0 7**2011 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555-001 Hope Creek Generating Station Renewed Facility Operating License No. NPF-57 Docket No. 50-354
Subject:
License Renewal Commitment Implementation
References:
(1) LR-N12-0212, "License Renewal Commitment Implementation," dated July 19,2012 The Renewed Operating License No. NPF-57 for Hope Creek Generating Station (HCGS) was issued on July 20, 2011. The renewed license included several license conditions related to the ASME Section XI, Subsection IWE aging management program and, in particular, to the Hope Creek drywell air gap drains. In accordance with License Condition 2.C. (27) c, this letter transmits a report summarizing the results of the ultrasonic thickness (UT) measurements taken during Refueling Outage 20 (Attachment 1.)
There are no regulatory commitments contained in this letter.
If you have any questions or require additional information, please contact Ms. Alysse K. Ochoa at 856-339-27 42.
~
Eric Carr
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Site Vice President Hope Creek Generating Station ako : Hope Creek Generating Station License Renewal Commitment Implementation 90-Day Report for Refueling Outage 20
LR-N17-0036 Page2 cc: Mr. Daniel Dorman, Regional Administrator- NRC Region 1 Ms. Carleen Parker, Project Manager- USNRC Mr. Justin Hawkins, USNRC Senior Resident Inspector- Hope Creek Mr. Patrick Mulligan, Manager IV, NJBNE Mr. Lee Marabella, Corporate Commitment Tracking Coordinator Mr. Thomas MacEwen, Hope Creek Commitment Tracking Coordinator
LR-N17-0036 Attachment 1 Hope Creek Generating Station License Renewal Commitment Implementation 90-Day Report for Refueling Outage 20
LR-N17 -0036 Attachment 1 Page 1 of 5 Hope Creek Generating Station License Renewal Commitment Implementation 90-Day Report for Refueling Outage 20
Background:
Renewed Operating License No. NPF-57 for Hope Creek Generating Station was issued on July 20, 2011. The renewed license contains several license conditions related to License Renewal and, in particular, to the Hope Creek drywell air gap drains. Some portions of these License Conditions were included in the Refueling Outage (RF) 17 scope and were worked during the outage that began on April 13, 2012, and ended on May 9, 2012. Continued investigations and changes were included in RF18 scope and were worked during the outage that began on October 11, 2013, and ended November 10, 2013. Monitoring of air gap leakage and performance of drywell shell UT thickness measurements were included in the RF19 scope and were worked during the outage that began on April 10, 2015, and ended May 13, 2015.
Monitoring of air gap leakage and performance of drywell shell UT thickness measurements were also included in the RF20 scope and were worked during the outage that began on October 14, 2016, and ended November 11, 2016.
The relevant license conditions are contained in Section 2.C of the renewed license.
Specifically, Section 2.C.(27) delineates those activities required to be performed following the establishment of drainage capability from the drywell air gap (that is, following completion of license condition 2.C.(26)) and reads as follows:
(27) After drainage has been established from the bottom of the air gap in all four quadrants, the licensee will:
- a. Submit a report to the NRC staff in accordance with 10 CFR 50.4 describing the final drain line configuration and summarizing the testing results that demonstrate drainage has been established for all four quadrants.
- b. Monitor penetration sleeve J13 daily for water leakage when the reactor cavity is flooded up. In addition, perform a walk-down of the torus room to detect any leakage from other drywell penetrations. These actions shall continue until corrective actions are taken to prevent leakage through J13 or through the four air gap drains.
- c. Perform UT measurements of the drywell shell between elevation 86'-11" (floor of the drywell concrete) and elevation 93'-0" (bottom of penetration J13) below penetration J13 area during the next three refueling outages. In addition, UT measurements shall be performed around the full 360 degree circumference of the drywell between elevations 86'-11" and 88'-0" (underside of the torus down comer vent piping penetrations). The results of the UT measurements will be used to identify drywell surfaces requiring augmented inspections in accordance with IWE requirements for the period of extended operation, establish a corrosion rate, and demonstrate that the effects of aging will be adequately managed such that the drywell can perform its intended function until April 11, 2046. Within 90 days of completion of each refueling outage, submit a report to the NRC staff in accordance with 10 CFR 50.4 summarizing the results from the UT measurements and if appropriate, corrective action.
LR-N17-0036 Page 2 of 5 Hope Creek Generating Station License Renewal Commitment Implementation 90-Day Report for Refueling Outage 20 Summary of Commitment Implementation:
The action required by License Condition 2.C. (27) a. was completed and the results submitted to the NRC in PSEG Letter No. LR-N12-0212 dated July 19, 2012. In accordance with License Condition 2.C. (27), this report discusses the actions taken by PSEG during Hope Creek Refueling Outage 20 (RF20) to satisfy license condition 2.C. (27) b. and 2.C. (27) c., above. The specific license conditions addressed and/or resolved during RF20 are as follows:
A. Monitoring of J13 Penetration Sleeve (License Condition 2.C. (27) b.)
During RF20, the J13 penetration sleeve was monitored daily for leakage while the reactor cavity was flooded up (October 18, 2016 through November 3, 2016). Further, the penetrations adjacent to penetration J13 (J19, J14, J29, J24, and J37, specified here as the "J 13 penetration group"), and the air gap drains were monitored daily for water leakage. In addition, a full walk-down of the torus room was performed to confirm that there was no leakage from any other penetrations. While the reactor cavity was flooded, walk-downs were performed by Operations in accordance with Operating Procedure HC.OP-DL.ZZ-0026, Surveillance Log. In addition, Engineering performed independent walk-downs during this time to gather additional data points. During the walk-downs, following reactor cavity flood-up and continuing until reactor cavity drain down, water was observed leaking at the 225 degree azimuth from the J13 penetration group (specifically the J19 penetration). Unlike in the previous two refueling outages, there was zero leakage identified at the excavated access tunnel located at 250 degree azimuth (specified here as the "250 Tunnel", a credited air gap drain).
On October 19, 2016, leakage was identified from penetrations J14/J24 at a leak rate of approximately 125 drops per minute (dpm). At penetrations J13/J37 and J19/29, leakage was identified at a rate of approximately 5 dpm at each penetration respectively. No water was noted leaking from any other areas within the torus room.
The leak rate from the J14/24 penetrations increased to 332 dpm on October 20, 2016, and the leakrate on penetrations J13/J37 and J19/29 increased to approximately 125 dpm and 166 dpm, respectively. There was zero leakage identified coming out of the 250 Tunnel. On October 21, 2016, the 250 Tunnel leakage remained at zero, while the penetrations J14/24 leakage dropped to approximately 262 dpm, and the leakage on the J13/37 and J19/29 penetrations dropped to approximately 83 dpm and 21 dpm, respectively. On October 23, 2016, the leakage from the 250 Tunnel remained at zero, and the leakage from the penetrations J14/24 dropped to approximately 97 dpm and the leakage on the J13/37 and J19/29 penetrations dropped to approximately 29 dpm and zero leakage, respectively. On October 25, 2016, the leakage from the 250 Tunnel remained at zero, and the leakage from penetrations J14/24 increased to 498 dpm, and the leakage on the J13/37 and J19/29 penetrations increased to approximately 249 dpm and 24 dpm, respectively. From October 26, 2016, to October 30, 2016, leakage diminished to zero at the J14/24 penetrations and the J13/37 penetrations, but there was a slight increase in leakage on the J19/29 penetrations to 80 dpm on October 26, 2016.
The leakage at penetrations J 19/29 dropped over the next two days to approximately 28 dpm. The last leakage was recorded on October 30, 2016, from the penetration J19/29
LR-N 17-0036 Page 3 of 5 Hope Creek Generating Station License Renewal Commitment Implementation 90-Day Report for Refueling Outage 20 at a rate of approximately 28 dpm. Note that the cavity remained flooded through November 3, 2016. The chart below represents a comparison of the RF20 leakage to that of the RF19 and RF18 leakage, where the X-axis represents days following flood up and theY-axis represents cumulative gallons leaked.
' RF20 20.00 -~----
RF19 5.00 0.0 1.0 2.0 2.5 3.0 3 .5 4.0 5.0 6.0 7.0 7.5 !tO 8.5 9.0 10.011.012.0
- RF20 - RF19 RF18 The data for RF18 and RF20 is similar. Leakage was first observed during RF20 after one day flooded up versus two days for RF18. The durations of the leakage for RF18 and RF20, however, were similar. The RF18 data versus RF20 data indicates a potential increase in leakage. The difference in leakage between RF18 and RF20 is very small (5 gallons total) and, overall, the total leakage continues to remain low.
No leakage was observed from any other air gap penetrations, and there was no sign of leakage from the end of the other three air gap drains (at 80, 160 and 340 degree azimuths), or from the excavated tunnels at 250, 290, 155 and 115 degree azimuths.
The Reactor Cavity to Drywell Seal Rupture Drain Alarm (HC.OP-AR.ZZ-0024, Alarm point 03837) did not actuate at any time while the reactor cavity was flooded up. All leakage from the penetrations stopped before draining of the reactor cavity.
B. UT Measurements (License Condition 2.C. (27) c.)
The Ultrasonic Thickness (UT) measurements prescribed by license condition 2.C. (27)
- c. were performed during RF20. Based on the consistency of the UT measurements with those taken in previous outages, PSEG has concluded that no significant corrosion is occurring on the drywell shell.
UT measurements were performed on the drywall shell at the 225 degree azimuth between 86'-11" and 93'-0" elevation (below the J13 penetration group). The lowest UT
LR-N17-0036 Page 4 of 5 Hope Creek Generating Station License Renewal Commitment Implementation 90-Day Report for Refueling Outage 20 measurements occurred on a plate below the J13 penetration group and measured 1.475" in RF16, 1.470" in RF17, 1.477" in RF18, 1.490" in RF19, and 1.482" in RF20.
Note that these readings were not at the same measurement point but were the lowest of all recorded readings taken during the respective outages. Comparing the lowest reading of 1.470" (from RF17) to the analysis limit of 1.4375" proves that at least 0.0325" thickness margin remains. Further, the consistency of the thickness measurements proves that no corrosion to the drywell shell is occurring below the J 13 penetration group. It should be noted that during development of the Hope Creek license renewal application, PSEG concluded that the cause of the lower readings on this plate were due to the plate's construction tolerances being at the lower end, but acceptable for use.
UT measurements were also performed for the full circumference of the drywell shell between elevations 86'-11" and 88'-0". The bottom of the drywell air gap is on the outside of the drywell shell between these elevations. The lowest UT measurements at the bottom of the drywell were 1.480" in RF16, 1.477" in RF17, 1.471" in RF18, 1.475" in RF19, and 1.481" in RF20. Note that these readings were not at the same measurement point but were the lowest of all recorded readings taken during the respective outages. Comparing the lowest reading of 1.471" (from RF18) to the analysis limit of 1.4375" shows that 0.0335" thickness margin remains. Based on the consistency of these UT measurements, PSEG has concluded that no corrosion is occurring in the drywell shell at the bottom of the drywell air gap.
Readings were also taken on the weld located above penetrations J-14 and J-24. The lowest reading observed on this weld was 1.460" in RF20. Readings at this point in previous outages were as follows: 1.518" in RF16, 1.579" in RF17, 1.584" in RF18, and 1.583" in RF19. This location's surface condition and geometry, however, is not conducive to consistent data.
Nevertheless, even if a very conservative corrosion rate of 0.006" per cycle were to be assumed, the analysis limit of 1.4375" would not be reached for at least 3 cycles.
The UT measurement activities required to be completed during RF20 by license condition 2.C. (27) c. were completed as described above. License condition 2.C. (27) c requires these UT measurement activities for the three refueling outages following establishment of drainage capability from the bottom of the drywell air gap.
RF20 is the third of these outages. The results of the RF20 UT measurements were compared to the previous UT measurements. No corrosion has been observed based on the data. Using a conservative corrosion rate, the analysis limit of 1.4375" would not be reached for 3 cycles. The UT measurements are being incorporated into the 3rd Interval IWE inspections, under category E-C, Item Number E4.12, to be performed once per period (every other outage) in accordance with ASME Section XI, 2007 edition, 2008 addenda.
LR-N 17-0036 Page 5 of 5 Hope Creek Generating Station License Renewal Commitment Implementation 90-Day Report for Refueling Outage 20 C. Corrective Actions The reactor cavity leakage continues to be monitored and documented in the Corrective Action Program (CAP). While the reactor cavity leakage continues to exist, the leakage monitoring actions prescribed by License Condition 2.C. (27) and UFSAR Section A.5, Commitment No 28; Sub-commitment 10 (Pages A-70 & 71) will be performed. UT measurements will be performed in accordance with the 3rd Interval Containment In-Service Inspection Long-Term Plan. There were no additional corrective actions as a result of the activities in RF20.
==
Conclusion:==
Activities associated with the Hope Creek renewed operating license condition 2.C. (27) that were required to be completed during the RF20 refueling outage were completed. License Condition 2.C. (27) a. was satisfied through submittal of PSEG Letter No. LR-N12-0212 on July 19, 2012. License conditions 2.C. (27) b. and 2.C. (27) c were satisfied during RF18 as documented in LR-N14-0029, for RF19 as documented in LR-N15-0147, and for RF20 as discussed above. This report satisfies the reporting requirements of 2.C. (27) c.