Information Notice 1987-25, Potentially Significant Problems Resulting from Human Error Involving Wrong Unit, Wrong Train, or Wrong Component Events

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Potentially Significant Problems Resulting from Human Error Involving Wrong Unit, Wrong Train, or Wrong Component Events
ML031130574
Person / Time
Issue date: 06/11/1987
From: Rossi C
Office of Nuclear Reactor Regulation
To:
References
IN-87-025, NUDOCS 9706050211
Download: ML031130574 (6)


SSINS No.: 6835 IN 87-25 UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555 June 11, 1987 NRC INFORMATION NOTICE NO. 87-25: POTENTIALLY SIGNIFICANT PROBLEMS RESULTING

FROM HUMAN ERROR INVOLVING WRONG UNIT,

WRONG TRAIN, OR WRONG COMPONENT EVENTS

Addressees

or a

All nuclear power reactor facilities holding an operating license (OL)

construction permit (CP).

Purpose

signif- This information notice is provided to inform recipients of potentiallytrain, or

icant problems resulting from human error involving wrong unit, wrong

infor- wrong component events. It is expected that recipients will review the

mation for applicability and consider actions, if appropriate, to preclude

in

similar problems from occurring at their facilities. Suggestions contained action

this notice do not constitute NRC requirements; therefore, no specific

or written response is required.

Description of Circumstances

terminal

On April 14, 1987, with Calvert Cliffs Unit, 1 in Mode 5 and electrical to

boxes open for equipment qualification work, plant personnel were attempting

use a portion of the containment spray system to fill the safety injection

1 tanks. In preparation for this, an operator had been sent to close a Unit

containment spray valve. However, the operator mistakenly closed the corre- sponding Unit 2 containment spray valve. The inadvertent containment spray

actuation resulted in approximately 4000 gallons of borated water being in- jected into the Unit 1 containment and created the potential for electrical

equipment degradation due to wetting by borated water (boric acid intrusion).

Discussion:

A large number of reports have been made to the NRC that describe events wrong

resulting from human error involving actions performed on the wrong unit, Office

train, or wrong component. A study published in January 1984 by the NRC

for Analysis and Evaluation of Operational Data, "Human Error in Events Involv- ing Wrong Unit or Wrong Train," and supplementary reports on August 8, 1984, more

February 13, 1986, September 19, 1986, and May 20, 1987, have identified indi- than 200 events of this nature that have occurred since 1981. The data

cate that there does not appear to be any substantial change in the rate of

occurrence in events per reactor year, and that the rate of these events at

87000

IN 87-25 June 11, 1987 plants with little operating experience seems to be higher than that at plants

with more experience. Examples of recent events caused by human error involv- ing the wrong unit, wrong train, or wrong component are described below.

A study performed by the Office of Nuclear Reactor Regulation and reported in

NUREG-1192, "An Investigation of the Contributors to Wrong Unit or Wrong Train

Events," indicates that some of the primary causes of the events studied were

inadequate labeling of plant equipment, components, and areas; inadequate personnel

training and experience; and inadequate procedures. Examples of actions taken

by licensees to help prevent recurrence of these types of events are also given.

Adequate procedures, planning, labeling, and training of personnel usually

prevent such events from happening. In addition, an independent verification

program can assist in promptly identifying and correcting the misalignment of

plant systems. The frequency and number of such events being reported to the

NRC suggest that industry needs to increase its attention in these areas.

Additional Events:

On May 13, 1986, with Kewaunee at power, personnel were performing a surveil- lance procedure on the power range nuclear instrumentation. The protection

signal bistables had been tripped to test Channel N44; however, a test signal

simulating an increased power level was inadvertently input to Channel N43.

This created the necessay 2 out of 4 coincidence logicand the reactor tripped

on simulated overpower AT.

On January 11, 1986, with St. Lucie 2 at power, an operator was performing the

weekly turbine overspeed surveillance. A manual turbine trip (and subsequent

reactor trip) occurred when the operator inadvertently actuated the turbine

trip lever instead of the test lever.

On March 18, 1985, with Surry 1 and 2 at power, an operator assigned to "lock

out" the automatic initiation of CO2 portion of the fire protection system for

Fire Zone #8 (the Unit 2 containment penetration area) to facilitate construc- tion activities, mistakenly "locked out" the CO2 for Fire Zone #5 (the Unit 1 cable vault). This error went undetected for approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> and

resulted in a violation of the Technical Specifications (no fire watch in

affected area).

References:

Information on independent verification programs is provided by IE Information

Notice 84-51, "Independent Verification." Information regarding inadvertent

defeat of safety function caused by human error involving wrong unit, wrong

train, or wrong component events is provided by IE Information Notice 84-58,

"Inadvertent Defeat of Safety Function Caused by Human Error Involving Wrong

Unit, Wrong Train, or Wrong System."

IN 87-25 June 11, 1987 No specific action or written response is required by this information notice.

If you have any questions about this matter, please contact the Regional

Administrator of the appropriate regional office or this office.

h/ar szE.Rossi, Director

Division of Operational Events Assessment

Office of Nuclear Reactor Regulation

Technical Contact:

Jack Ramsey, NRR

(301) 492-9081 Attachment: List of Recently Issued NRC Information Notices

---

Attachment 2 IN 17-13 Jlune U, no

LIST OP RECENTLY ISSUED

INFORMPATION NOTICES 1987

, AnTor2n%10f Date of

Netfice No. Sublect tssuenci I ?glued to -

J7-24 Operational Exprienceo 1/4/17 All nuclear power

Involving Lossos of reactor facilities

Elct rcal Inverters holding an OL or CP.

87-S3 Loss of Decay Heat Removal 5/27/87 All PWl facilities

During Low Reactor Coolant holding an OL or CP.

Level Operation

J7-22 Operator Licensing Requal- 5/22/87 All research and

fication Exuainations at nonpower reactor

Nenpower Reactors facilities.

  • 7-21 Shutdown Order Issued Because 51/2187 All nuclear power

Licensed Operators Asleep facilities holding

While on Duty an OL or CP and all

licensed operators.

87-20 Hydrogen Leak In Auxiliary 4/20/87 All nuclear power

Building facilities holding

an OL or CP

85-108 Degradation of Reactor 4/20/87 All PWR facilities

Sup. 1 Coolant System Pressure holding an OL or CP.

Boundary Resulting from

Boric Acid Corrosion

864 Deficiencies In Upgrade 4/20/87 All nuclear power

Sup. 1 Program for Plant facilities holding

Emergency Operating a CP or OL.

Procedures.

85-61 Nisadministrations to 4/15/87 All licensees

Sup. 1 Patients Undergoing Thyroid authorized to use

Scans byproduct material

87-19 Perforation and Cracking of 4/9/87 All Westinghouse

Rod Cluit roC-ntrol Asseoblies power PWNfadTit..

holding an OL or CP

87-18 Unauthorized Service on 4/8/87 All NRClicensees

Telatherapy Units by Non- authorized to use

licensed maintenance Personnel radioactive material

in toletherapy units

OL

  • Operating License

CP - Construction Pemit

UNITED STATES

NUCLEAR REGULATORY COMMISSION FIRST CLASS MAIL

WASHINGTON, D.C. 20556 POSTAGE & FEES PAID

USNRC

WASH. D.C.

OFFICIAL BUSINESS PERMIT No. G4n

PENALTY FOR PRIVATE USE. S300

IN 87-25 June 11, 1987 No specific action or written response is required by this information notice.

If you have any questions about this matter, please contact the Regional

Administrator of the appropriate regional office or this office.

Charles E. Rossi, Director

Division of Operational Events Assessment

Office of Nuclear Reactor Regulation

Technical Contact:

Jack Ramsey, NRR

(301) 492-9081 Attachment: List of Recently Issued NRC Information Notices

  • See Previous Concurrence

OGCB:DOEA:NRR* PPMB:ARM* C/OGCB:DOEA:NRR*

JRamsey MHarwell CHBerlinger CERossi

06/4/87 06/4/87 06/4/87 06/,5/87

IN 87-XX

June xx, 1987 No specific action or written response is required by this information notice.

If you have any questions about this matter, please contact the Regional

Administrator of the appropriate regional office or this office.

Charles E. Rossi, Director

Division of Operational Events Assessment

Office of Nuclear Reactor Regulation

Technical Contact:

Jack Ramsey, NRR

(301) 492-9081 Attachment: List of Recently Issued NRC Information Notices

OGC BOEA:NRR PP RM C/ aPEA:NRR

JRamsey MHPrwell CHBerlinger

06/fI /87 06/ 1/87 06/ /87 06 " 87