Failures of RHR Pump Motors and Pump InternalsML031250031 |
Person / Time |
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Site: |
Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, 05000000, 05000115, Zimmer, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant, Skagit, Marble Hill |
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Issue date: |
05/20/1986 |
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From: |
Jordan E NRC/IE |
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To: |
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References |
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IN-86-039, NUDOCS 8605150473 |
Download: ML031250031 (5) |
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Similar Documents at Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, 05000000, 05000115, Zimmer, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant, Skagit, Marble Hill |
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Category:NRC Information Notice
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Mclaughlin on NRC, Regarding NRC Information Notice 2006-13: Groundwater Contamination2006-07-13013 July 2006 E-mail from M. Mclaughlin on NRC, Regarding NRC Information Notice 2006-13: Groundwater Contamination 2020-09-03 The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:05000000]] OR [[:05000115]] OR [[:Zimmer]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] OR [[:Skagit]] OR [[:Marble Hill]] </code>.
[Table view]The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:05000000]] OR [[:05000115]] OR [[:Zimmer]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] OR [[:Skagit]] OR [[:Marble Hill]] </code>. |
SSINS No.: 6835 IN 86-39 UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF INSPECTION AND ENFORCEMENT
Washington, DC 20555 May 20, 1986 IE INFORMATION NOTICE NO. 86-39: FAILURES OF RHR PUMP MOTORS AND
PUMP INTERNALS
Addressees
All nuclear power reactor facilities holding an operating license (OL) or a
construction permit (CP).
Purpose
This notice is provided to alert licensees to serious damage which has occurred
at a licensed nuclear power plant to residual heat removal (RHR) pumps manufac- tured by Bingham-Willamette with motors supplied by General Electric. The damage
identified at the Philadelphia Electric Co. (PECO), Peach Bottom facility involved
failure of motor bearings and/or failure of pump impeller wear rings.
It is expected that recipients will review this notice for applicability to
their facilities and consider actions, if appropriate, to preclude a similar
problem occurring at their facilities. However, suggestions contained in this
notice do not constitute requirements; therefore, no specific action or written
response is required.
Description of Circumstances
On November 2, 1985, during core reload of PECO's Peach Bottom Unit 3, a fire
occurred in the 3C RHR pump motor which totally engulfed the motor and rendered
the pump inoperable. A lower guide bearing high temperature alarm had been
received for 3 days prior to the pump failure, but this warning of potential
pump failure went unnoticed by personnel because of the large number of other
alarms that were received during the shutdown. The motor, a 2000 HP GE verti- cal induction model 5K6348XC29, and pump, a Bingham-Willamette single stage
centrifugal model 18x24x28 CVIC (Figure 1), were uncoupled, disassembled and
inspected for damage. Results of the inspection identified that the motor
lower guide bearing was destroyed, the rotor bars were gouged and scorched, and the stator windings were burned and gouged. The pump internals were found
to have sustained internal damage. Specifically, the lower impeller wear ring
(Figure 1) was separated from the impeller and fused to the casing wear ring.
No other wear surfaces indicated wear or damage. On November 16, 1985, while
replacing the lower pump casing gasket on the 3A RHR pump, PECO personnel
discovered that the lower pump impeller wear ring was separated from the
impeller and cracked in three places. Subsequent inspections of the remaining
two unit 3 RHR pumps and two unit 2 pumps (2A and 2C) revealed similar wear
ring failures in three of the pumps inspected.
8605150473
IN 86-39 May 20, 1986 On December 22, 1985, after several overcurrent alarms with pump 20 from Unit 2, PECO inspected this pump and discovered the lower pump impeller wear ring
separated and cracked, a 6-inch piece of wear ring missing, and the impeller
vanes damaged. Not all failures noted above were as severe as the ones
identified on pumps 3C and 2D. However, the similarity was evident.
The RHR pump impeller wear rings are press fit to the impeller and attached
with eight dowel pins. The wear rings provide a wearing surface on the pump
impeller. The wear rings are 410 stainless steel, A 182 grade F6 with a
Rockwell C hardness of 33 to 39. Metallurgical examinations of the wear ring
fracture surfaces indicate the presence of intergranular stress corrosion
cracking (IGSCC). PECO has classified the wear ring failures as IGSCC. On
November 26, 1985, PECO made an INPO Network notification regarding these RHR
pump failures. PECO has repaired all affected pumps by replacement of damaged
motors and pump internals. Tennessee Valley Authority's Browns Ferry Units 1,
2, and 3 utilize the identical pumps for RHR service. Similar motor and pump
impeller wear ring failures have occurred at these facilities, but not to the
extent identified at Peach Bottom. Pumps of similar design, but different size, are utilized for core spray service both at Peach Bottom and Browns Ferry.
However, these pumps use the "integral" impeller wear ring design, i.e.,
extended impeller part replaces separate wear ring and forms a single unit, and therefore are not susceptible to the type of wear ring failure previously
described.
Discussion:
These multiple events are of concern because of the potential for common- mode failures of all pumps in the same system. At Peach Bottom, six of eight
pumps inspected exhibited degraded pump impeller wear rings and internals.
These flaws could lead to pump hydraulic degradation and, under the worst
conditions, complete pump failure. The motor guide bearing failures are signi- ficant because they could cause failure of the pump motors and pump internal
damage.
The full extent to which this type of pump may be used in safety-related
services at other facilities is not known with complete certainty. According
to information ascertained from Bingham-Williamette records and confirmed by
contact with affected sites, other plants utilizing this type of pump in the
RHR system include the following: Cooper, Pilgrim 1, and Vermont Yankee.
The exact cause of the pump internal failures has not been fully determined, except that there is evidence that IGSCC has contributed to the impeller wear
ring failures. Operating pumps with inadequate flow and lubrication, whereby
high internal temperatures develop, is also a likely contributor, e.g., pump
cavitation. PECO is continuing to pursue root causes and wear ring redesigns
to prevent such occurrences in the future.
IN 86-39 May 20, 1986 No specific action or written response is required by this information notice.
If you have any questions regarding this matter, please contact the Regional
Administrator of the appropriate NRC regional office or the technical contact
listed below.
r Jordan, Director
Division of Emergency Preparedness
and Engineering Response
Office of Inspection and Enforcement
Technical Contact:
Ronald M. Young
(301) 492-8985 Attachments:
1. Figure 1 - Typical CVIC RHR Pump
Sectional Assembly
2. List of Recently Issued IE Information Notices
Attachment 1 IN 86-39 May 20, 1986
Casing Wear Ring
Lower
Impeller Wear Ring
FIGURE 1 - Typical CVIC RHR Pump
Sectional Assembly
Attachment 2 IN 86-39 May 20, 1986 LIST OF RECENTLY ISSUED
IE INFORMATION NOTICES
Information Date of
Notice No. Subject Issue Issued to
86-38 Deficient Operator Actions 5/20/86 All power reactor
Following Dual Function Valve facilities holding
Failures an OL or CP
86-37 Degradation Of Station 5/16/86 All power reactor
Batteries facilities holding
an OL or CP
86-36 Change In NRC Practice 5/16/86 All power reactor
Regarding Issuance Of facilities holding
Confirming Letters To an OL or CP
Principal Contractors
86-35 Fire In Compressible Material 5/15/86 All power reactor
At Dresden Unit 3 facilities holding
an OL or CP
86-34 Improper Assembly, Material 5/13/86 All power reactor
Selection, And Test Of Valves facilities holding
And Their Actuators an OL or CP
86-33 Information For Licensee 5/6/86 Fuel cycle licensees
Regarding The Chernobyl and Priority 1 material
Nuclear Plant Accident licensees
86-32 Request For Collection Of 5/2/86 All power reactor
Licensee Radioactivity facilities holding
Measurements Attributed To an OL or CP
The Chernobyl Nuclear Plant
Accident
86-31 Unauthorized Transfer and 5/6/86 All power reactor
Loss of Control of facilities holding
Industrial Nuclear Gauges an OL or a CP
86-30 Design Limitations of 4/29/86 All power reactor
Gaseous Effluent Monitoring facilities holding
Systems an OL or a CP
OL = Operating License
CP = Construction Permit
|
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list | - Information Notice 1986-01, Failure of Main Feedwater Check Valves Causes Loss of Feedwater System Integrity and Water-Hammer Damage (6 January 1986, Topic: Feedwater Heater)
- Information Notice 1986-02, Failure of Valve Operator Motor During Environmental Qualification Testing (6 January 1986)
- Information Notice 1986-03, Potential Deficiencies in Enviromental Qualification of Limitorque Motor Valve Operator Wiring (14 January 1986)
- Information Notice 1986-04, Transient Due to Loss of Power to Intergrated Control System at a Pressurized Water Reactor Designed by Babcock & Wilcox (31 January 1986)
- Information Notice 1986-05, Main Steam Safety Valve Test Failures and Ring Setting Adjustments (31 January 1986)
- Information Notice 1986-06, Failure of Lifting Rig Attachment, While Lifting Upper Guide Structure at St. Lucie Unit 1 (3 February 1986, Topic: Control of Heavy Loads)
- Information Notice 1986-06, Failure of Lifting Rig Attachment, while Lifting Upper Guide Structure at St. Lucie Unit 1 (3 February 1986)
- Information Notice 1986-07, Lack of Detailed Instruction & Inadequate Observance of Precautions During Maintenance & Testing of Diesel Generator Woodward Governors (3 February 1986, Topic: Overspeed trip, Overspeed)
- Information Notice 1986-08, Licensee Event Report (LER) Format Modification (3 February 1986, Topic: GOTHIC)
- Information Notice 1986-09, Failure of Check & Stop Check Valves Subjected to Low Flow Conditions (3 February 1986)
- Information Notice 1986-10, Degradation of Reactor Coolant System Pressure Boundary Resulting From Boric Acid Corrosion. (5 January 1995, Topic: Boric Acid, Stress corrosion cracking)
- Information Notice 1986-10, Feedwater Line Break (10 November 1988, Topic: Coatings, Anchor Darling)
- Information Notice 1986-10, Degradation of Reactor Coolant System Pressure Boundary Resulting from Boric Acid Corrosion. (5 January 1995, Topic: Boric Acid, Stress corrosion cracking)
- Information Notice 1986-11, Anomalous Behavior of Recirculation Loop Flow in Jet Pump BWR Plants (31 December 1986)
- Information Notice 1986-13, Standby Liquid Control System Squib Valves Failure to Fire (21 February 1986, Topic: Squib)
- Information Notice 1986-13, Standby Liquid Control Squib Valves Failure to Fire (5 August 1986, Topic: Squib)
- Information Notice 1986-14, Overspeed Trips of AFW, HPCI & RCIC Turbines (26 August 1991, Topic: Fire Barrier, Overspeed trip, Overspeed, Water hammer)
- Information Notice 1986-14, Overspeed Trips of Afw, HPCI & RCIC Turbines (26 August 1991, Topic: Overspeed trip)
- Information Notice 1986-15, Loss of Offsite Power Caused by Problems in Fiber Optics Systems (10 March 1986, Topic: Squib)
- Information Notice 1986-16, Failures to Identify Containment Leakage Due to Inadequate Local Testing of BWR Vacuum Relief System Valves (11 March 1986, Topic: Squib, Local Leak Rate Testing, Integrated leak rate test)
- Information Notice 1986-17, Update of Failure of Automatic Sprinkler System Valves to Operate (24 March 1986, Topic: Squib)
- Information Notice 1986-18, NRC On-Scene Response During a Major Emergency (26 March 1986, Topic: Squib, Backfit)
- Information Notice 1986-19, Reactor Coolant Pump Shaft Failure at Crystal River (21 March 1986, Topic: Squib)
- Information Notice 1986-20, Low-Level Radioactive Waste Scaling Factors, 10 CFR Part 61 (28 March 1986, Topic: Squib)
- Information Notice 1986-21, Recognition of American Society of Mechanical Engineers Accreditation Program for N Stamp Holders (31 March 1986, Topic: Squib)
- Information Notice 1986-22, Underresponse of Radiation Survey Instrument to High Radiation Fields (31 March 1986, Topic: High Radiation Area, Squib)
- Information Notice 1986-23, Excessive Skin Exposures Due to Contamination with Hot Particles (9 April 1986)
- Information Notice 1986-23, Excessive Skin Exposures due to Contamination with Hot Particles (9 April 1986)
- Information Notice 1986-24, Respirator Users Notice: Increased Inspection Frequency for Certain Self-Contained Breathing Apparatus Air Cylinders (11 April 1986, Topic: Hydrostatic)
- Information Notice 1986-25, Traceability and Material Control of Material and Equipment, Particularly Fasteners (11 April 1986)
- Information Notice 1986-26, Potential Problems in Generators Manufactured by Electrical Products Incorporated (17 April 1986)
- Information Notice 1986-27, Access Control at Nuclear Facilities (21 April 1986, Topic: Contraband)
- Information Notice 1986-28, Telephone Numbers to the NRC Operations Center and Regional Offices (24 April 1986)
- Information Notice 1986-29, Effects of Changing Valve Moter-Operator Switch Settings (25 April 1986)
- Information Notice 1986-30, Design Limitations of Gaseous Effluent Monitoring Systems (29 April 1986)
- Information Notice 1986-31, Unauthorized Transfer and Loss of Control of Industrial Nuclear Gauges (14 July 1986)
- Information Notice 1986-32, Request for Collection of Licensee Radioactivity Measurements Attributed to Chernobyl Nuclear Plant Accident (2 May 1986, Topic: Chernobyl, Potassium iodide)
- Information Notice 1986-33, Information for Licensee Regarding the Chernobyl Nuclear Plant Accident (6 May 1986, Topic: Chernobyl, Potassium iodide)
- Information Notice 1986-34, Improper Assembly, Material Selection, & Test of Valves & Their Actuators (13 May 1986)
- Information Notice 1986-34, Improper Assembly, Material Selection, & Test of Valves & their Actuators (13 May 1986)
- Information Notice 1986-35, Fire in Compressible Material at Dresden Unit 3 (15 May 1986, Topic: Chernobyl)
- Information Notice 1986-36, Change in NRC Practice Regarding Issuance of Confirming Letters to Principal Contractors (16 May 1986, Topic: Chernobyl)
- Information Notice 1986-37, Degradation of Station Batteries (16 May 1986, Topic: Chernobyl)
- Information Notice 1986-38, Deficient Operator Actions Following Dual Function Valve Failures (20 May 1986, Topic: Chernobyl)
- Information Notice 1986-39, Failures of RHR Pump Motors and Pump Internals (20 May 1986, Topic: Chernobyl)
- Information Notice 1986-40, Degraded Ability to Isolate the Reactor Coolant System from Low-Pressure Coolant Systems in Bwrs (5 June 1986, Topic: Chernobyl)
- Information Notice 1986-40, Degraded Ability to Isolate the Reactor Coolant System from Low-Pressure Coolant Systems in BWRs (5 June 1986, Topic: Chernobyl)
- Information Notice 1986-41, Evaluation of Questionable Exposure Readings of Licensee Personnel Dosimeters (9 June 1986, Topic: Chernobyl)
- Information Notice 1986-42, Improper Maintenance of Radiation Monitoring Systems (9 June 1986, Topic: Temporary Modification, Chernobyl)
- Information Notice 1986-43, Problems with Silver Zeolite Sampling of Airborne Radioiodine (10 June 1986, Topic: Chernobyl)
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