IR 05000456/2002009
| ML030280631 | |
| Person / Time | |
|---|---|
| Site: | Braidwood |
| Issue date: | 01/24/2003 |
| From: | Ann Marie Stone NRC/RGN-III |
| To: | Skolds J Exelon Generation Co |
| References | |
| IR-02-009 | |
| Download: ML030280631 (47) | |
Text
January 24, 2003
SUBJECT:
BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 50-456/02-09; 50-457/02-09
Dear Mr. Skolds:
On December 31, 2002, the US Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on January 2, 2003, with Mr. J. von Suskil and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the results of this inspection, the NRC has identified one self-revealing issue that was evaluated under the risk significance determination process as having a very low safety significance (Green). The issue was determined not to involve a violation of NRC requirements.
If you contest the subject or severity of the Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -
Region III, Warrenville Road, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S.
Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector at the Braidwood facility.
Since the terrorist attacks on September 11, 2001, the NRC has issued two Orders (dated February 25, 2002, and January 7, 2003) and several threat advisories to licensees of commercial nuclear power reactors to strengthen licensee capabilities, improve security force readiness, and enhance access authorization. The NRC also issued Temporary Instruction 2515/148 on August 28, 2002, that provided guidance to inspectors to audit and inspect licensee implementation of the interim compensatory measures (ICMs) required by the February 25th Order. Phase 1 of TI 2515/148 was completed at all commercial nuclear power reactors in 2002, and the remaining inspections are scheduled for completion in 2003.
Additionally, table-top security drills were conducted at several licensees to evaluate the impact of expanded adversary characteristics and the ICMs on licensee protection and mitigative strategies. Information gained and discrepancies identified during the audits and drills were reviewed and dispositioned by the Office of Nuclear Security and Incident Response. During 2003, the NRC will continue to monitor overall safeguards and security controls, conduct inspections, and resume force-on-force exercises at selected nuclear power plants. Should threat conditions change, the NRC may issue additional Orders, advisories, and temporary instructions to ensure adequate safety is being maintained at all commercial nuclear power reactors.
In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Ann Marie Stone, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77
Enclosure:
Inspection Report 50-456/02-09; 50-457/02-09 w/Attachments: 1. Supplemental Information 2. Results of Temporary Instruction 2515/149 Inspection See Attached Distribution
DOCUMENT NAME: C:\\MyFiles\\Copies\\ML030280631.wpd To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RIII NAME AMStone:dtp DATE 01/24/03 OFFICIAL RECORD COPY
REGION III==
Docket Nos:
50-456; 50-457 License Nos:
50-456/02-09; 50-457/02-09 Licensee:
Exelon Generation Company, LLC Facility:
Braidwood Station, Units 1 and 2 Location:
35100 S. Route 53 Suite 84 Braceville, IL 60407-9617 Dates:
October 1 through December 31, 2002 Inspectors:
S. Ray, Senior Resident Inspector N. Shah, Resident Inspector S. Burgess, Senior Reactor Analyst D. Chyu, Reactor Inspector D. Funk Jr., Physical Security Inspector D. Nelson, Radiation Specialist H. Peterson, Senior Operations Engineer (Lead Inspector)
T. Ploski, Emergency Preparedness Specialist S. Sanders, Reactor Operations Engineer J. Roman, Illinois Department of Nuclear Safety Approved by:
Ann Marie Stone, Chief Branch 3 Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000456/2002-009, 05000457/2002-009; Exelon Generation Company, LLC; on 10/01-12/31/02, Braidwood Station; Units 1 & 2. Operability Evaluations.
This report covers a 3-month period of baseline resident inspection and an announced baseline inspection on radiation protection, emergency preparedness, and biennial/annual review of the licensed operator requalification program. In addition, generic safety issue inspections in accordance with Temporary Instruction (TI) 2515/148, Inspection of Nuclear Reactor Safeguards Interim Compensatory Measures, Revision 1, and TI 2515/149, Mitigating Systems Performance Index Pilot Verification, were conducted. The inspections were conducted by Region III inspectors, a Region III Senior Reactor Analyst, a Headquarters engineer, and the resident inspectors. One Green finding, which was determined not to involve a violation of NRC requirements, was identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after United States Nuclear Regulatory Commission (NRC)management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.
Inspection Findings
Cornerstone: Initiating Events
- Green.
A finding of very low safety significance was identified through a self-revealing event when the main control room received a low oil level alarm for the 2C turbine-driven feedwater pump. The alarm was caused by an oil drain valve being inadvertently left open by a non-licensed operator during planned maintenance occurring on the previous shift. The primary cause of this finding was related to the cross-cutting area of human performance, in that the plant operator did not use adequate self-checking to verify the oil drain valve was closed.
This finding was more than minor because it increased the likelihood of a reactor trip event due to low steam generator level, and could have affected the availability of the main feedwater mitigating system due to the potential loss of the 2C turbine-driven feedwater pump from low lube oil pressure. The finding was of very low safety significance because the exposure time was short, all other mitigating systems were available, and the main feedwater system could have been recovered by fairly simple operator actions. The finding was not considered a violation of regulatory requirements.
(Section 1R15)
REPORT DETAILS
Summary of Plant Status
Unit 1 operated at or near full power throughout the inspection period, except that power was briefly reduced to about 94 percent on October 17, 2002, for steam generator safety relief valve testing, reduced to about 96 percent on December 4-5, 2002, for load following, and briefly reduced to about 84 percent on December 15, 2002, for turbine steam valve testing.
Unit 2 operated at or near full power throughout the inspection period, except that power was reduced to about 88 percent for a few hours on November 1, 2002, in response to a problem with feedwater heaters, and power was reduced to about 28 percent on November 2 through 3, 2002, to allow testing of feedwater isolation valves. The unit was returned to full power on November 4, 2002. Unit 2 power was also reduced by various small amounts on December 2 and twice on December 3, 2002, for load following. Finally, Unit 2 power was reduced to about 24 percent on December 26, 2002, and the generator was taken off line for generator balancing and other planned maintenance on December 27, 2002. The reactor was maintained critical during the maintenance. The generator was placed back on line on December 30 and the unit returned to full power on December 31,
REACTOR SAFETY
Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
a. Inspection Scope
The inspectors verified that the licensee had completed its seasonal preparations for cold weather in a timely manner before the cold weather actually presented a challenge. The inspectors reviewed the licensees completed freezing temperature annual surveillance and verified that it adequately covered risk-significant equipment and ensured that the equipment was in a condition to meet the requirements of Technical Specifications (TSs),the Technical Requirements Manual (TRM), and the Updated Final Safety Analysis Report (UFSAR) with respect to protection from low temperatures. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action system by reviewing the associated condition reports (CRs). Based on their importance for availability of mitigating systems, the inspectors conducted more detailed system reviews and walkdowns for the following two systems:
- during the week of October 21, 2002, the inspectors walked down the Units 1 and 2 refueling water storage tanks (RWSTs) and the associated heating systems and power supplies; and
- during the week of October 28, 2002, the inspectors walked down the Units 1 and 2 condensate storage tanks and associated heating systems and power supplies.
As part of these inspections, the inspectors reviewed the documents listed in
1.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
.1 Partial Walkdown
a. Inspection Scope
On October 17 and 18, 2002, the inspectors performed a walkdown of the accessible portion of the 2A residual heat removal (RH) system train. This risk-significant mitigating system train was chosen because the redundant 2B RH train was scheduled to be taken out of service for a modification on October 20, 2002. The inspectors utilized the valve and electric breaker checklists listed in Attachment 1 to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders (WOs) and CRs associated with the train to verify that those documents did not reveal issues that could affect train function. The inspectors used the information in the appropriate sections of the TS and UFSAR to determine the functional requirements of the system.
b. Findings
No findings of significance were identified.
.2 Complete Walkdown
a. Inspection Scope
During the week ending October 5, 2002, the inspectors conducted a system alignment inspection of the instrument air system. This system was selected because of its importance in preventing initiating events, its support of several mitigating systems, and the fact that it was a Maintenance Rule (a)(1) category system. The inspection consisted of the following activities:
- a walkdown of the system in the auxiliary building using the mechanical lineup checklist to verify proper alignment, component accessibility, availability, and current condition;
- a review of recent CRs to verify that there were no current operability concerns; and
- a review of open WOs to verify that there were no conditions impacting availability and that deficiencies had been identified.
The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action system. Documents reviewed during this inspection are listed in Attachment 1.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate a plant transient, or their impact on the plants ability to respond to a security event. The inspectors used the documents listed in Attachment 1 to verify that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program.
The following areas were inspected by walkdowns:
- Unit 1 miscellaneous electrical equipment room and safeguards battery rooms on October 15, 2002;
- Unit 2 miscellaneous electrical equipment room and safeguards battery rooms on October 15, 2002;
- Unit 1 diesel generator rooms on October 15, 2002;
- Unit 2 diesel generator rooms on October 17, 2002;
- fire protection system pumps in the lake screenhouse on October 22, 2002;
- Unit 2 emergency lights on December 2, 2002; and
- Unit 1 emergency lights on December 9, 2002.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
.1 Biennial Written Examination and Annual Operating Test Results
a. Inspection Scope
The inspectors reviewed the overall pass/fail results of individual written tests, Job Performance Measure operating tests, and simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee during calender year 2002.
The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609 Appendix I, Operator Requalification Human Performance Significance Determination Process.
b. Findings
No findings of significance were identified.
.2 Quarterly Review of Requalification Testing and/or Training Activities
a. Inspection Scope
On October 16, 2002, the inspectors observed an operating crew during an out-of-the-box requalification examination on the simulator using Scenario BR-10, Respond to a Steam Generator Tube Rupture With Miscellaneous Malfunctions, dated August 29, 2002. The inspectors evaluated crew performance in the areas of:
- clarity and formality of communications;
- ability to take timely actions in the safe direction;
- prioritization, interpretation, and verification of alarms;
- procedure use;
- control board manipulations;
- oversight and direction from supervisors; and
- group dynamics.
Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the following Exelon procedures:
- OP-AA-101-111, Rules and Responsibilities of On-Shift Personnel, Revision 0;
- OP-AA-103-102, Watchstanding Practices, Revision 0;
- OP-AA-103-103, Operation of Plant Equipment, Revision 0;
- OP-AA-103-104, Reactivity Management Controls, Revision 0; and
- OP-AA-104-101, Communications, Revision 0.
The inspectors verified that the crew completed the critical tasks listed in the above simulator guide. The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed the licensee evaluators to verify that they also noted the issues and discussed them in the critique at the end of the session.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
During the weeks of October 28 and November 4, 2002, the inspectors reviewed the licensees overall maintenance effectiveness for the primary containment system on both units. This system was chosen due to it being in the Maintenance Rule (a)(1) category because of previous problems. This evaluation consisted of the following specific activities:
- reviewing the maintenance rule evaluation history for the system for the previous 2 years;
- observing the conduct of surveillance testing activities for stroke timing containment isolation valves;
- reviewing selected CRs, open WOs, and control room log entries in order to identify system deficiencies; and
- a discussion with the system engineer for the system.
The inspectors also reviewed whether the licensee properly implemented the Maintenance Rule, 10 CFR 50.65, for the system. Specifically, the inspectors determined whether:
- the system was scoped in accordance with 10 CFR 50.65;
- performance problems with the system constituted maintenance rule functional failures;
- the system had been assigned the proper safety significance classification;
- the system was properly classified as (a)(1) or (a)(2); and
- the goals and corrective actions for the system were appropriate.
The above aspects were evaluated using the maintenance rule program and other documents listed in Attachment 1. The inspectors also verified that the licensee was appropriately tracking reliability and/or unavailability for the system.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the licensees management of plant risk during emergent maintenance activities or during activities where more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety-significant equipment. The inspections were conducted to verify that evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate.
The licensees daily configuration risk assessments records, observations of operator turnover and plan-of-the-day meetings, and the documents listed in Attachment 1 were used by the inspectors to verify that the equipment configurations were properly listed, that protected equipment were identified and were being controlled where appropriate, and that significant aspects of plant risk were being communicated to the necessary personnel. The inspectors verified that the licensee controlled emergent work in accordance with the expectations in the procedures listed in Attachment 1.
In addition, the inspectors reviewed selected issues that the licensee entered into its corrective action program, including minor issues identified by the inspectors, to verify that identified problems were being entered into the program with the appropriate characterization and significance.
The inspectors reviewed the following activities:
- planned maintenance on the 1B steam generator power operated relief valve in conjunction with planned maintenance on the Unit 1 switchyard, electrical bus tie breaker 3-4, on October 8, 2002;
- planned maintenance on the 2B RH pump, in conjunction with planned maintenance on the Unit 2 station air compressor and 2C heater drain pump, on October 21, 2002;
- planned maintenance on the 1B essential service water pump in conjunction with planned maintenance on the 1A motor driven feedwater pump on October 24, 2002;
- troubleshooting a ground on direct current bus 212 on October 31, 2002, including direct observations of the work by plant electricians;
- planned maintenance on the 2D steam generator power operated relief valve in conjunction with drain down testing on the Unit 0 component cooling heat exchanger and planned maintenance on the 142 station auxiliary transformer on November 7, 2002, including direct observations of the drain down test; and
- planned maintenance on the 2B service water pump in conjunction with Unit 2 switchyard relay testing on November 26, 2002.
b. Findings
No findings of significance were identified.
1R14 Personnel Performance Related to Non-routine Plant Evolutions and Events
a. Inspection Scope
- On November 1, 2002, while the inspectors were performing a plant status walkdown in the control room, Unit 2 experienced an unexpected high-2 level alarm on the 22B, 23B and 24B low pressure feedwater heaters. This resulted in the plant operators having to reduce power in order to isolate the affected heaters and provide for better heater level control. These actions were in accordance with Braidwood Operating Procedure BwOP HD-12, Isolating and Returning to Service at Power Low Pressure Feedwater Heater 22A/B/C Shell Side, Revision
4. The inspectors monitored control room instrumentation to verify that plant
response was as expected and observed operator response in controlling the power reduction. The transient was terminated when the operators isolated the affected heaters and reduced power from 100 percent to 86 percent. As part of this inspection, the inspectors reviewed the documents listed in Attachment 1.
- On December 26, 2002, Unit 2 power was reduced to about 24 percent and on December 27, the generator was taken off line for a preplanned maintenance outage. The reactor was maintained critical during the maintenance, with the rod control system in manual and heat removal through the steam dumps to the main condenser. Maintaining the reactor in this mode for over three days was considered a non-routine evolution. The inspectors observed planning and pre-job briefings for the evolutions and observed portions of the power reduction. In addition, the inspectors observed operators maintaining stable plant conditions with manual rod control and steam dumps and also observed portions of the evolutions of placing the generator back on line and increasing power. The inspectors verified that the operators were following the plant operating procedures listed in Attachment 1. The inspectors also observed shift turnovers to verify that the appropriate information regarding plant status and controls was being communicated. The generator was placed back on line on December 30, and the reactor returned to full power on December 31, 2002.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors evaluated plant conditions and selected CRs for risk-significant components and systems in which operability issues were questioned. These conditions were evaluated to determine whether the operability of components was justified. The inspectors compared the operability and design criteria in the appropriate section of the and UFSAR to the licensees evaluations presented in the CRs and documents listed in 1 to verify that the components or systems were operable.
The inspectors reviewed the following operability evaluations:
- 2A containment spray pump cubicle cooler, and other similar coolers, on October 15, 2002, after low service water flow was noted;
- fire protection system after it failed to meet the acceptance criteria of a surveillance test on October 17, 2002;
- troubleshooting of direct current (DC) bus 211 system grounds on November 20, 2002;
- non safety-related prefilter found installed in 0B main controlled room ventilation system on November 25, 2002;
- low oil reservoir level on the 2C main feedwater pump on November 29, 2002; and
- temporary leakage repair of the Unit 1 pressurizer steam space sample line on December 11, 2002.
b. Findings
Introduction:
A finding of very low safety significance (Green) was identified through a self-revealing event when the main control room received a low oil level alarm for the 2C turbine-driven feedwater pump. The alarm was caused by an oil drain valve being inadvertently left open by a non-licensed operator during planned maintenance occurring on the previous shift. The finding was not considered a violation of regulatory requirements. The finding increased the probability of a reactor transient while also potentially degrading the main feedwater mitigating system.
Description:
On November 29, 2002, the Unit 2 control room received an unexpected annunciator, Feedwater Pump Turbine Bearing Oil Level Low, for the 2C turbine-driven feedwater pump. Subsequently, operators in the field observed that there was no oil in the 2C pump lube oil reservoir sightglass. The operators immediately added oil, verified that the feedwater pump was operable, and initiated a prompt investigation. The investigation identified that the low oil condition was caused by an oil drain valve being inadvertently left open by a non-licensed operator, while performing BwOP TO-10, Turbine Feed Pump Oil Purification System Operation, Revision 8, on the previous shift. The resulting loss of lube oil to the main feedwater pump could have resulted in a pump trip possibly leading to a low steam generator level reactor trip due to the loss of feedwater flow. During the event, the inspectors observed the as-found condition of the oil drain valve, that the motor driven feedwater pump was available, and that the control room staff was preparing for a potential pump trip, by reviewing Braidwood Abnormal Operating Procedure 2BwOA SEC-1, Secondary Pump Trip-Unit 2, Revision 100.
Analysis:
The inspectors determined that the operators action in leaving the oil drain valve open was a performance deficiency warranting a significance evaluation in accordance with Inspection Procedure Manual (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on April 29, 2002. This finding was considered more than minor, because it increased the likelihood of an initiating event (i.e., reactor trip due to low steam generator level) and could have affected the availability of the main feedwater mitigating system (i.e., 2C feedwater pump trip). The inspectors determined that this event also affected the cross-cutting area of Human Performance, because the operator did not perform adequate self-checking to ensure that the oil drain valve was closed.
The inspectors completed a significance determination of this issue, using IMC 0609, Significance Determination Process, dated April 30, 2002, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, dated March 18, 2002.
For the Phase 1 screening, the inspectors answered No to all the questions under the Initiating Event column. This was based on the short exposure time, the availability of all other mitigating systems, and the availability of the motor-driven feedwater pump, which could have been started by fairly simple operator actions. Therefore, this finding (FIN 50-457/02-09-01) is considered of very low safety significance (Green). The finding was assigned to the Initiating Event Cornerstone for Unit 2.
Enforcement:
The inspectors concluded that no violation of regulatory requirements had occurred. The operator was performing activities in accordance with a procedure for a nonsafety-related system. This procedure was not one required by 10 CFR 50, Appendix B. The licensee entered the event into its corrective action system as CR 133502, 2C Feedwater Pump Low Oil Reservoir Level, on November 29, 2002.
1R16 Operator Workarounds
a. Inspection Scope
- On December 9, 2002, the inspectors reviewed several abnormal operating procedures used by the operators for response to certain events. The inspectors looked for steps in the procedures that could be classified as operator workarounds because they directed operators to perform actions or operate equipment in a manner that was not consistent with the current design basis of the plant and that could affect the operators ability to implement the procedures.
Procedures reviewed for this inspection are listed in Attachment 1.
- On December 19, 2002, the inspectors reviewed Operator Workaround 225, 1CB025 Air Regulators Out of Adjustment or Gages Bad May Prevent Valve From Opening on a High 2 Actuation. The inspectors verified that the workaround did not substantially hinder the operators ability to implement abnormal or emergency procedures, that the operators were aware of and trained on the workaround, and that actions had been initiated to return the system to normal operation. Documents reviewed as part of this inspection are listed in
1.
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of important mitigating, barrier integrity, and support systems to ensure that the testing adequately verified system operability and functional capability with consideration of the actual maintenance performed. The inspectors used the appropriate sections of the TS and UFSAR, as well as the documents listed in 1, to evaluate the scope of the maintenance and to verify that the post maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action system.
Testing subsequent to the following activities was observed and evaluated:
- modification of the control board switch for valve 2RH611 on October 21, 2001;
- repair of the head gasket on 1A diesel generator air compressor 1 on October 23, 2002;
- modification of 1A diesel generator air dryer 1 on October 23 and 24, 2002;
- modification of the control board switch for valve 1 RH611 on October 28, 2002;
- testing of the Unit 1 RWST heating pump on November 15, 2002; and
- planned maintenance on the 1A RH pump on December 11, 2002.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors witnessed selected surveillance testing and/or reviewed test data to verify that the equipment tested using the surveillance procedures met the TS, the TRM, the UFSAR, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in verifying mitigating systems capability and barrier integrity.
The inspectors used the documents listed in Attachment 1 to verify that the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded.
The following tests were observed and evaluated:
- calibration of Unit 1 Channel A, delta temperature and average coolant temperature loops on October 16, 2002;
- Unit 1 steam generator safety relief valve TREVI testing on October 17, 2002;
- monthly testing of the 2B diesel-driven auxiliary feedwater pump on October 21, 2002;
- monthly testing of the 2B diesel generator on November 27, 2002; and
- quarterly testing of the 2A motor-driven auxiliary feedwater pump on December 6, 2002.
b. Findings
No findings of significance were identified.
1R23 Temporary Modifications
a. Inspection Scope
- On October 8, 2002, the inspectors reviewed a temporary maintenance alteration to install a freeze seal isolation on the component cooling water supply to the Unit 2 fuel pool heat exchanger. This activity was chosen because a significant problem with the freeze installation could have potentially resulted in a loss of Unit 2 component cooling water which would have resulted in a reactor shutdown due to the loss of cooling water flow to the Unit 2 reactor coolant pumps. This was an installation in support of maintenance and was intended to be in place for less than 90 days, so a formal safety evaluation was not required.
The inspectors reviewed the WO for the job, including the engineering review for the installation, the engineering change to the original review to allow the work to be accomplished during plant operations, and the plant barrier impairment permits. The inspectors also walked down the piping where the freeze was to be installed before the work began, attended the high level awareness briefing, and observed a portion of the work. In addition, the inspectors also reviewed the operations contingency plan for potential failure of the freeze and attended shift turnover meetings where the contingencies were discussed. Finally the inspectors verified that the operations temporary change tracking log was used to record the temporary change as required.
The inspectors verified that problems identified by the licensee during the freeze installation were entered into the corrective action system. As part of this inspection, the inspectors reviewed the documents listed in Attachment 1.
- On October 11, 2002, the inspectors performed a walkdown of the Units 1 and 2 auxiliary building to observe whether there were any installed, unauthorized temporary modifications.
b. Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The inspectors reviewed Revisions 8, 9, and 10 of the Braidwood Station Annex to Exelons Standardized Emergency Plan to determine whether changes identified reduced the effectiveness of the licensees emergency planning, pending onsite inspection of the implementation of these changes.
b. Findings
No findings of significance were identified.
RADIATION SAFETY
Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiologically Significant Areas (71121.01)
Plant Walkdowns, Radiological Boundary Verification, Radiation Work Permit Reviews and Observations of Radiation Worker Performance
a. Inspection Scope
During the week of October 21, 2002, the inspectors conducted walkdowns of selected radiologically controlled areas within the plant to verify the adequacy of radiological boundaries and postings. Specifically, the inspectors walked down several radiologically significant work area boundaries (high and locked high radiation areas) in the Units 1 and 2 auxiliary building, the radwaste building, and the spent fuel pool and performed confirmatory radiation measurements to verify that these areas and selected radiation areas were properly posted and controlled in accordance with 10 CFR Part 20, licensee procedures, and the TRMs. The inspectors also reviewed the radiological conditions within those work areas walked down, to assess the radiological housekeeping and contamination controls.
b. Findings
No findings of significance were identified.
2OS2 As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and Controls (71121.02)
.1 Radiological Work/ALARA Planning
a. Inspection Scope
During the week of October 26, 2002, the inspectors examined the stations procedures for radiological work/ALARA planning and scheduling, and evaluated the dose projection methodologies and practices implemented for the 2002 Unit 2 refueling outage (A2R09),to verify that sound technical bases for outage dose estimates existed.
The inspectors reviewed the exposure results and ALARA post-job reviews for selected A2R09 activities to evaluate the accuracy of exposure estimates in the ALARA plans.
The inspectors compared the actual exposure results versus the initial exposure estimates, the estimated and actual dose rates as well as the estimated and actual man-hours expended. The inspectors reviewed the exposure history for each activity and reviewed management involvement in exposure tracking to assess outage dose performance and dose control practices. The inspectors reviewed selected work-in-progress ALARA reviews and ALARA post-job reviews to determine if additional engineering/dose controls for those activities had been established, and if required corrective documents had been generated. Those work activities included Unit 2 valve work, steam generator project work, reactor head disassembly, installation and removal of insulation, and the assembling and disassembling of scaffolding.
b. Findings
No findings of significance were identified.
.2 Verification of Exposure Estimate Goals and Exposure Tracking System
a. Inspection Scope
During the week of October 26, 2002, the inspectors reviewed the methodology and assumptions used by the licensee for its A2R09 exposure estimates and exposure goals.
Actual job exposure data was compared with estimates to verify that the licensee could project and, thus, control radiological exposure. The inspectors also reviewed the licensees exposure tracking system to verify that the level of exposure tracking detail, exposure report timeliness, and exposure report distribution were sufficient to support control of collective exposures. The inspectors evaluated how the licensee had identified problems with its exposure estimates for some jobs, the processes being utilized to revise dose estimates, and methods to improve its dose forecasting procedures to verify that the licensee could adequately track dose.
b. Findings
No findings of significance were identified.
.3 Identification and Resolution of Problems
a. Inspection Scope
During the week of October 26, 2002, the inspectors reviewed 2002 focus area self-assessments of ALARA Planning and Controls, and High Radiation Area Controls/Posting to evaluate the effectiveness of the self-assessment process to identify, characterize, and prioritize problems. The inspectors also reviewed corrective action documentation to verify that previous access control and ALARA related issues were adequately addressed. The inspectors also selectively reviewed January - October 2002, CRs that addressed access control and ALARA program deficiencies to verify that the licensee had effectively implemented the corrective action program.
b. Findings
No findings of significance were identified.
SAFEGUARDS
Cornerstone: Physical Protection
3PP1 Response to Contingency Events (71130.03)
a. Inspection Scope
On October 15, 2002, the inspectors reviewed the status of security operations and assessed licensee implementation of the protective measures in place as a result of the current, elevated threat environment.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
40A1 Performance Indicator Verification (71151) Cornerstones: Mitigating Systems and Occupational Radiation Safety
.1 Mitigating Systems Performance Indicator Verification
a. Inspection Scope
The inspectors reviewed documents listed in Attachment 1 to verify that the licensee had corrected reported performance indicators data, in accordance with the criteria in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 2. The following performance indicators were reviewed for the period of October 1, 2001, through September 30, 2002:
- safety system unavailability, high pressure safety injection system on November 18, 2002; and
- safety system unavailability, auxiliary feedwater system on December 4, 2002.
b. Findings
No findings of significance were identified.
.2 Occupational Radiation Safety Performance Indicator Verification
a. Inspection Scope
During the week of October 26, 2002, the inspectors verified the licensees assessment of its performance indicator for occupational radiation safety. Since no reportable elements were identified by the licensee for the 4th quarter of 2001 and the first three quarters of 2002, the inspectors selectively reviewed the licensees data elements to verify that there were no occurrences in the occupational radiation safety cornerstone during those quarters.
b. Findings
No findings of significance were identified.
40A2 Identification and Resolution of Problems (71152)
.1 Routine Review of Identification and Resolution of Problems
a. Inspection Scope
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action system at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action system as a result of inspectors observations are generally denoted in the report or in the documents in Attachment 1.
b. Findings
No finding of significance were identified.
.2 Selected Issue Follow-up
Maintenance Effectiveness of Diesel Generator Work Introduction During the 1st two weeks of October 2002, the inspectors reviewed licensee CR 120314, Potential Trend-Maintenance Effectiveness of Diesel Generator Work, dated August 22, 2002. This CR was written to evaluate a potential adverse trend involving planned maintenance on the 2A and B emergency diesel generators occurring between July and August 2002. Individually these events affected the mitigating systems cornerstone, as they potentially affected the availability of the emergency diesel generators.
The licensees evaluation identified two specific common failure modes: inadequate work practices (including human performance) and poor process work management (including work planning and job preparation). The inspectors reviewed this evaluation, including the individual CRs documenting the specific maintenance problems, to determine the adequacy of the licensees problem identification, prioritization and evaluation of issues, and corrective actions.
a.
Effectiveness of Problem Identification
- (1) Inspection Scope The inspectors reviewed CR 120314 and 24 additional CRs generated between July and August 2002, documenting the adverse trend and the specific events comprising the trend. The inspection focused on the licensees threshold for documenting the maintenance problems, the types of events identified, and the circumstances leading to the discovery of the conditions. The inspectors had previously observed portions of the 2A and B diesel generator maintenance activities as documented in Sections 1R12, 1R13 and 1R19 of Inspection Report 50-456/457-02-07. The inspectors also reviewed licensee post job critiques for prior planned work on the 1A and B emergency diesel generators occurring in December 2001 and February 2002, respectively.
- (2) Issues The inspectors concluded that the licensee had effectively identified the maintenance issues associated with the 2A and B emergency diesel generator work. Specifically, the inspectors observed that the licensee had identified the maintenance problems at a low threshold and had correctly entered them into the corrective action program. These problems were either self-revealing or identified through routine maintenance, equipment checks and/or were self-reported events. The majority of the problems were identified and addressed during the respective work windows. During the 1A and B diesel generator work, the licensee had made similar, but fewer observations, regarding the maintenance work. However, the majority of these previous events dealt primarily with minor work planning and scheduling concerns.
b.
Prioritization and Evaluation of Issues
- (1) Inspection Scope The inspectors reviewed the licensees common cause evaluation for those maintenance events documented in CR 120314. Specifically, the inspectors evaluated how the licensee had arrived at the overall conclusions and assessed whether these conclusions were appropriate. The inspectors also reviewed the results of several, recent maintenance self-assessments regarding work conduct and planning. For the common cause evaluation, the inspector referred to licensee procedure LS-AA-125-1002, Common Cause Analysis Manual, Revision 2.
- (2) Issues The licensee identified two common failure modes for these events: inadequate work practices (including human performance); and poor process work management (i.e., work planning and job preparation). These causes were similar to the root causes identified for the individual events and the inspectors noted that the licensees evaluation was performed consistent with the station procedure. Additionally, these conclusions were similar to the findings of the maintenance self-assessments. However, the inspectors noted that the licensee did not interview those workers involved in the 2A and B diesel generator work and did not review related maintenance department self-assessments as part of the common cause evaluation. Although neither action was required by the procedure, the inspectors were concerned that by not performing them other, potentially significant insights may not be identified. The licensee acknowledged the inspectors concerns and was reviewing them for a potential, future revision of the procedure.
c.
Effectiveness of Corrective Actions
- (1) Inspection Scope The inspectors reviewed the licensees corrective actions for the individual 2A and B diesel generator maintenance events and for the common cause evaluation results.
- (2) Issues The inspectors concluded the licensees corrective actions for the individual diesel generator maintenance events were effective. As stated in Section 40A2.2(a), these events were primarily identified and addressed during the respective work windows. However, the inspectors noted that the licensees common cause evaluation did not assess whether the corrective actions for the individual maintenance events were effective. This action was not specifically required by station procedure LS-AA-125-1002. For the events in general, the licensee planned to perform further evaluations of maintenance work practices and work management to identify what additional concerns and associated actions were needed. Although these corrective actions were adequate, the inspectors questioned their effectiveness given that prior maintenance self-assessments of these areas had already been performed. As stated in Section 40A2.2(b), these self-assessments were not reviewed as part of the common cause evaluation. These observations were also provided to the licensee as stated in Section 40A2.2(b).
4OA3 Event Follow-up
.1 (Closed) Licensee Event Report (LER) 50-456/457-2002-003-00:
Isolated Loop Reactor Coolant System Boron Sample Outside of Technical Specification Frequency Requirement Due to Misapplication of the Implementing Procedure.
During refueling outages, isolated loop boron concentration was determined from samples of the water used to fill the reactor coolant loop. Technical Specification 3.4.18.2 required that the boron concentration in the isolated coolant loop be verified to be greater than or equal to the required shutdown margin boron concentration of the unisolated portion of the loop within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> prior to unisolating the loop. However, on September 11, 2002, the licensee identified that these samples were often collected and analyzed greater than 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> before the loop isolation valves were opened. The root cause of the TS non-compliance was the failure to clearly reflect the sampling and analysis requirements in station procedure BwOP RC-8, Restoring a Reactor Coolant System Loop to Service, Revision 3. Because the isolated reactor coolant loops were normally filled with borated water at a concentration higher than the shutdown margin, the failure to meet the TS was minor. Additionally, the inspectors determined that the probability of accidental dilution of the isolated loop boron concentration from leakage past the loop isolation valves, was small. Corrective actions included a planned revision to BwOP RC-8 to clearly reflect the TS requirements and a proposed TS amendment to clarify the sampling requirements. The failure to meet the sampling requirements of TS 3.4.18.2 constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the NRCs Enforcement Policy. The LER was reviewed by the inspectors and no findings of significance were identified. This issue was entered into the licensees corrective action system as CR 122579, Late TS Sample for Surveillance 3.4.18.2, dated September 11, 2002.
.2 Response to Security Events
a. Inspection Scope
The inspectors briefly reviewed the licensees response to security events during the inspection period. This was accomplished by discussions with security management personnel, observations of changes made to the security measures after each event, and reviewing the documents in Attachment 1. Response to the following events were reviewed:
- a trespassing incident in the owner controlled area on December 10, 2002; and
- a trespassing incident in the owner controlled area on December 17, 2002.
b. Findings
No findings of significance were identified.
4OA4 Cross-Cutting Findings
A finding described in Section 1R15 of this report had, as a primary cause, a human performance deficiency in that a plant operator did not perform adequate self-checking to ensure that the 2C turbine-driven feedwater pump oil drain valve was closed following planned maintenance.
4OA5 Other Activities
.1 (Closed) Unresolved Item (URI) 50-456/00-06-02; 50-457/00-06-02:
Licensing requirements reduced for two auxiliary building fire zones.
During the 2000 triennial fire protection inspection, the inspectors determined that the licensee changed Fire Zones 11.5-0 and 11.6-0 (auxiliary building, 401' and 426' elevations, respectively), from fire zones which complied with the guidelines of Branch Technical Position (BTP) Chemical Mechanical Engineering Branch (CMEB) 9.5-1, Section C.5.b.(2).(a), which required separating redundant safe shutdown trains with a 3-hour fire barrier, to areas for which alternative shutdown capability should be provided in accordance with BTP CMEB 9.5-1, Section C.5.b.(3), without providing fixed suppression systems in the fire zones. In addition, during a follow-up inspection to the above issue in October 2001, the inspectors questioned a change in administrative procedures which reduced or eliminated fire watch requirements in areas where suppression systems were inoperable.
During the thermo-lag resolution period, the licensee re-routed redundant power cables out of Fire Zones 11.5-0 and 11.6-0. During this process, the licensee identified that power and control cables for the main control room ventilation system were also present in these fire zones and was unable to reroute these cables. The redundant cables for the control room ventilation system were needed for safe shutdown and were not protected by a 3-hour rated fire barrier. Assuming a loss of control room ventilation, the temperatures in the control room would increase beyond panel qualifications within 2-3 hours. The operators would have to evacuate the control room and take instrument readings at the fire hazards panel. Therefore, the licensee designated the fire zones as areas that utilized alternative shutdown capability.
The purpose of this inspector review was to determine whether there was any adverse effect on safe shutdown capabilities based upon designating these fire zones as requiring alternative shutdown capabilities. The inspectors reviewed Braidwoods licensing basis as discussed in Amendments 3 and 7 to the Fire Protection Report, the Byron Safety Evaluation Report and subsequent supplements (NUREG 876), and the Braidwood Safety Evaluation Report and subsequent supplements (NUREG 1002) to determine the applicability of the requirement for an area-wide suppression system in Fire Zones 11.5-0 and 11.6-0. If the control cables from both redundant trains of equipment were located in the same fire zone, credit would be taken for alternate shutdown via local operation of equipment as specified in various plant procedures (Section 2.4.1.5 of Amendment 3). In addition, deviations for the fire zones not having suppression systems, because the areas were not completely separated from other fire areas, were approved by the NRC.
Based on the level of fire protection features originally approved by the NRC, the inspectors determined that the operators would likely use the control room only as a point of command. Safe shutdown actions would be initiated outside of the control room for a fire in these two areas (demonstrated during Byron Station, Units 1 & 2, triennial fire protection inspection in December 2001). Therefore, this designation change did not adversely affect the methods of achieving and maintaining safe shutdown and was consistent with the licensees licensing basis and the approved fire protection program.
The licensee subsequently changed the area designation back to areas requiring safe shutdown capabilities (meeting requirements of III.G.2) and proceduralized operator actions to be taken in the event of loss of the control room ventilation system.
Therefore, the inspectors determined that the classification change for the two fire zones did not adversely affect the licensees ability to achieve and maintain safe shutdown conditions in the event of a fire. This aspect of the item is closed.
With respect to compensatory measures, the licensee still required continuous fire watches for an inoperable suppression system in areas where redundant systems or components could be damaged, such as in the case of Fire Zone 11.3-0. For all other fire zones, the sprinkler systems were not used to protect redundant safe shutdown functions but to mitigate smoke and heat propagation from one fire area to another.
Furthermore, the purpose of a continuous fire watch was two-fold: to notify the control room; and, to initiate actions to extinguish small fires utilizing available equipment. The function of notifying the control room was replaced by the operable detection systems in the area. For a small fire, after the receipt of the alarm in the control room, an operator would be dispatched immediately to investigate the fire location before dispatching the full team of fire brigade members. For a more severe fire beyond the capability of the fire watch, the expected fire growth would be limited since the purpose of the water suppression system was to control (not to extinguish) the fire until the arrival of fire brigade members. Therefore, this change in fire watch requirements was acceptable.
.2 (Closed) URI 50-456/00-06-01; 50-457/00-06-01:
Equipment Important for Safe Shutdown Not Identified.
Examples identified by the inspectors included the centrifugal charging pump discharge valve, pressurizer auxiliary spray valve, component cooling water thermal barrier cooling isolation valves, and the main steam isolation valves. Since the identified issues concerned the potential effects of fire damage on associated circuits related to safe shutdown components and the resultant spurious actuation of such components, this item will be tracked as a part of URI 50-456/00-06-03; 50-457/00-06-03, Effects of Associated Circuits Not Isolated from Safe Shutdown Equipment.
.3 Pre-Inspection of Appendix A to Temporary Instruction (TI) 2515/148, Inspection of
Nuclear Reactor Safeguards Interim Compensatory Measures, Revision 1 The inspectors completed the pre-inspection audit for interim compensatory measures at nuclear power plants, dated September 13, 2002.
.4 Completion of TI 2515/149, Mitigating System Performance Index (MSPI) Pilot
Verification On November 12, through December 17, 2002, the inspectors completed the requirements of the TI to verify that the licensee had correctly implemented the MSPI pilot guidance for reporting unavailability and unreliability of the monitored safety systems. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action system. Documents reviewed during this inspection are listed in Attachment 1. The detailed results of this inspection are documented in a memorandum included as Attachment 2.
4OA6 Meetings
.1 Exit Meeting
The inspectors presented the inspection results to Mr. J. von Suskil and other members of licensee management at the conclusion of the inspection on January 2, 2003. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
.2 Interim Exit Meetings
The results of the radiation protection inspection were presented to T. Joyce at the conclusion of the inspection on October 24, 2002. The inspectors did not receive any information identified as proprietary during this inspection The results of the safeguards inspection were presented to J. von Suskil at the conclusion of the inspection on October 29, 2002. The inspectors did not receive any information identified as proprietary during this inspection.
The results of the biennial/annual licensed operator requalification review were presented to with D. Burton, Licensed Operator Requalification Training Group Lead on November 4, 2002, via telephone and to D. Myers, Training Director on December 19, 2002, via telephone.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- J. von Suskil, Site Vice President
- T. Joyce, Plant Manager
- J. Bailey, Regulatory Assurance - NRC Coordinator
- G. Baker, Site Security Manager
- R. Blaine, Radiation Protection Manager
- D. Chrzanowski, Inservice Inspection Coordinator
- G. Dudek, Operations Manager
- C. Dunn, Site Engineering Director
- A. Ferko, Regulatory Assurance Manager
- T. Green, Nondestructive Examination Level III Inspector
- P. Hippley, Initial License Operator Training Group Lead
- D. Myers, Dresden Training Director
- G. ODonnell, Engineer
- M. Sears, Engineering Programs
United States Nuclear Regulatory Commission
- M. Chawla, Project Manager, Office of Nuclear Reactor Regulation
- A. Stone, Chief, Reactor Projects Branch 3
LIST OF ITEMS
CLOSED
Opened
50-457/02-09-01 FIN Feedwater oil drain valve inadvertently left open
Closed
50-456/00-06-01; 50-457/00-06-01 URI equipment important for safe shutdown not identified 50-456/00-06-02; 50-457/00-06-02 URI license requirements reduced for two auxiliary building fire zones 50-456/457/02-03-00 LER Isolated Loop Reactor Coolant System Boron Sample Outside of TS Frequency Requirement Due to Misapplication of the Implementing Procedure 50-457/02-09-01 FIN Feedwater oil drain valve inadvertently left open