IR 05000395/1985042

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Insp Rept 50-395/85-42 on 851101-30.No Violations or Deviations Noted.Major Areas Inspected:Followup on Nonroutine Events & Repts,Surveillance Observations of safety-related Sys & Observations of Maint Activities
ML20138N324
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 12/06/1985
From: Cantrell F, Hopkins P, Prevatte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20138N323 List:
References
50-395-85-42, NUDOCS 8512230492
Download: ML20138N324 (8)


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, Report No.: 50-395/85-42 Licensee: South Carolina. Electric and Gas Company Columbia, SC 29218 Docket No.: 50-395 License-No.: NPF-12 Facility =Name: V. C. Summer Inspection Conducted: November- 1 - 30, 1985 Inspectors: h mu b M -

4R/0/RS Richardg.Prevatte Q) Q- Dafe S'igned OhLOA A Jn

ta/6)ts Perry C.[fiopkins ~ l/ Date 61gned Approved by: d 12/4 d FToyd S. Cantrell, pgn Chief Date 61gned Division of Reactor ef6jects

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SUMMARY Scope: .This' routine, announced inspection involved 236 resident inspector hours on - site in the areas. of followup on nonroutine events. and reports, surveillance observations of safety related systems, observation of maintenance activities, followup of operational events, refueling activities, operational safety

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verifications, preparation for refueling, engineered safety systems,

-organizational and administrative activitie Results: Of the areas inspected, no violations or deviations were identifie ,

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s REPORT DETAILS u Persons Contacted -

Licensee. Employees D. Nauman,.Vice President, Nuclear Operations , .

0.' Bradham,' Director, Nuclear Plant Operations J. Connelly, Deputy Director,.0perations and Maintenance K. Woodward, Manager, Operations-

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B. Croley,.Gr6up. Manager,. Technical and Support Services M. Quinton, Manager, Maintenance Services M.' Browne, Manager,. Technical Support G. Putt, Manager,'Schedulitg and Materials Management

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M. Williams, Manager, Nuclear Education and Training L. Blue, Manager,'. Support Services S.iHunt, Associate Manager, Qu'ality Assurance Surveillance Systems A. Koon, Associate Manager, Regulatory Compliance J. Sefick, ~ Associate Manager, Station Security B.-Williams, Supervisor, Operations

Other licensee employees _ contacted included engineers, technicians,

-operators, mechanics, security force members, and office. personne . ' Exit Interview (30702,30703).

The inspection scope and findings were summa"ized on December 2,.1985, with those persons indicated in, paragraph 1.above. The inspector described the areas inspected and discuss 3d thi inspection findings. -The licensee did not identify as proprietary any of the materials provided 'to or reviewed by the

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inspectors during:the-inspectio . Onsite ' Followup of Events .and Subsequent Written Reports of Nonroutine-Events at Power Reactor Facilities (92700, 90714, 93792)',

For ' nonroutine : events selected for onsite followup, the inspectors

' determined that the licensee had taken corrective action (s) as stated in written' reports of the events and that these responses to the events were adequate and met regulatory requirements, license . conditions, and commitments. During the reporting period, the inspectors selected the following nonroutine events for onsite followup:

-(Closed) IFI 84-37-02 " COMMITMENT TO IMPLEMENT PROCEDURE CHANGE TO REQUIRE VERIFICATION OF ALL AUTO START / BLOCK FUNCTIONS OF LOAD SEQUENCERS." The Licensee implemented STP 125-011 and STP 125-010 to replace the old ST These new procedures verify the capability of load sequencer to energize component cooling pump "A" and to block auto start of certain " swing" pumps, (i.e. component cooling pump "C", service water pump "C" and charging pump

"C"). The corrective action appears to be adequate to satisfactorily-address the event and prevent recurrence. This item close .

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(Closed) LER 83-133 " BORON INJECTION! TANK DILUTED TO 19,700 PARTS /MILLION

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DUE TO-LIFTING OF RELIEF VALVE XVR-8925 DURING TEST." The Licensee reported this event to Region II on December 22,_1983. The inspector reviewed the

licensee's . report, commitments, corrective : action and associated documentatio The corrective action appears to be adequate to_ satis-factorily address this event and prevent recurrenc This item close (Closed) SPR'85-008 " APPENDIX R FIRE WATCH." .The Licensee made a special report to Region II on July 3, 1985. The inspectors reviewed the licensee's report, commitments, corrective action and associated documentation. The corrective action appears to _ be adequate to satisfactorily address this event to prevent recurrence. This item close (Closed) LER 83-074 " DIESEL GENERATOR OUTPUT BREAKER TRIPPED OPEN'DUE TO AN ELECTRICAL SURGE FROM A LIGHTNING STORM." The licensee reported this event to Region II on July 29, 1983. The inspector reviewed the licensee's reports, commitments, corrective action and associated documentation. The corrective . action appears to be adequate to satisfactorily address this Jevent and to prevent recurrence. This item close (Closed) LER 85-07 " DIESEL GENERATOR SEISMICITY, DUE TO PERSONNEL ERROR IN

'SCAFFOLO INSTALLATION." The licensee reported this event to Region II on April 19, 198 The inspectors reviewed the licensee's reports, commitments, corrective action and associated documentation. The corrective action appears: to be . adequate to satisfactorily address this event and to prevent recurrence. This item close (Closed) SPR 85-011 " REACTOR BUILDING PURGE EXHAUST AND SUPPLY SYSTEM MONITOR." The licensee made a Special Report to Region II on September 12, 198 The inspectors reviewed the licensee's report, commitments, corrective action and associated documentatio The corrective action appears to be adequate to satisfactorily address this event to prevent recurrence. -This item close (Closed) SPR 84-016 and SPR 85-012 " STEAM GENERATOR TUBE EDDY CURRENT

EXAMINATIONS." The licensee made Special Reports to Region II on November 14, 1984 and September 20, 1985, respectively. The inspectors reviewed the licensee's reports, commitments, -corrective action and associated documentatio The corrective action appears to be adequate to satisfactorily address this event to prevent recurrenc These items close . Monthly Surveillance Observation (61726)

The inspectors observed surveillance activities of safety-related systems

'and components to ascertain that these activities were conducted in accordance with license requirements. The inspectors observed portions of selected surveillance tests including all aspects of one major surveillance test' involving safety-related systems. The inspectors determined that the

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surveillance test ~ procedure conformed to Technical Specifications (TS)

requirements and verified that Limiting Conditions for Operations (LCO's)

.were met. a'nd ' that the surveillance test -was completed at the required frequency. The ) inspectors also verified that the required administrative approvals and t'agouts were obtained prior _to initiating the test, that the testing was ' accomplished by qualified -personnel in accordance with an a approved test procedure and that any required test instrumentation was properly calibrated. Upon completion of the testing, the inspectors observed that the~ recorded test data was accurate, complete and met TS requirements; verified any test discrepancies were properly rectified, and; independently verified that the systems were properly returned to service. The following specific surveillance activities were observed:

STP 445.007 -

MOVATS Testin STP 125.011 -

Train "B" Intergraded Safeguards Tes Within the areas inspected, no violations or deviations were identifie . Monthly Mainteriance Observation (62703)

-The inspectors observed maintenance activities of safety-related systems and components .to ascertain that these activities were conducted in accordance withf approved procedures, Technical Specifications (TS) and appropriate *

industry codes and standards. The inspectors determined that these activities were not violating Limiting Conditions for Operations (LCO's) and that redundant components were operable. The inspectors also determined (1)

that the procedures used were adequate to-control the activity, (2) that QC

hold -pointx were established where required, (3) that required administra-

.tive approvals and tagouts were obtained prior to work initiation, (4) that

_ proper radiological and appropriate ignition / fire prevention controls were implemented, and (5) that replacement r'r and materials used were properly

. certified. The inspectors verified teit t ese activities were accomplished by qualified personnel using al'reve, procedure The inspectors independently verified that equw;r unt s. properly tested before being returned U to service. Additionally, the inspectors reviewed several outstanding job orders to determine that the licensee was giving priority to safety-related maintenance and a backlog which might affect its performance was not developing on a - given system. The following specific maintenance activities were observed:

MWR 83H00308 -

Drain RHR Hx "A" And Tagout For Repai MWR 20481001 -

Piping And Hanger Modifications Associated With BIT Remova MWR 83H0031 -

Leak Test RHR Hx "A" Head After Repai MRF 20811k' -

Diesel Building "B" Train HVAC Damper MRF 208918c -

Rotopeening Of Steam Generators "A", "B" and "C" MWR'8501982 -

Rework Of CVCS Valves 8105. (RCP Seal Water Header

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< Isolation Valve).

R & R 850679 -

Component Cooling Wate Within the areas' inspected, no violations or deviations were identifie y <

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!6.1 ;0nsite followup-of; Events at-Operating Reactors"(93702)

J L .On" October 6,1985,- with sthe plant- in Hot Standby and preparing for -

refueling ~ shutdown,Ttheelicenseek performed STP 401.002, " Main: Steam

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yf , - Lin'e; Code: Safety Valves," ASME Section XI: Test." During this test. the

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licensee Jdiscovered .that -ten of fifteen valves exce'eded -the + 1%

^ tolerance' allowed by : Technical Specification -'3.7.1.1. The effected ivalves were : readjusted 'to meet the. required tolerance and tested .

satisfactorily. .The;1icensee has submitted LER 85-030 and is. currently .

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performing:and engineering evaluation of thisievent.

$ ' On T A'ugustL 19, 1985, Anchor / Darling i sent',a ' letter to South Carolina

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Electric and Gas _ identifying safety concerns ~ associated with missing

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lock welds on swing check valves ' installed at another utilit . .

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This;correspondenceznoted'that-most 150 lb. and 300 lb. pressure' class-

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Anchor /Darlingfswing? check valves utilize a L set screw in
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v 1 support for. Lthe purpose of. keeping Ethe hinge -pin from rotating. On

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_ some designs, this= set screw also prevents: the hinge pin from - sliding

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fout of the hinge support. The set: screw is required' to be lock welded to - prevent,it' from backing out in _- service. The~:' absence of this lock

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tweld is a safety concern since the set screw'could conceivably back out

in ' service' allowing the hinge pin. to slide ~out of the hinge supportE Lthus causing a loss of-valve operabilit ~

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'At the aff'ecte'd. utility, the disc nut pin on several check valves-'was

'not lock welded. This':, lock weld .is -necessary to ' retain the disc nut

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pin:which: prevents the disc nut from uacking off_the disc and rendering;

=the? valve in_ operable. As- an alternate 'to the lock weld, Anchor / Darling currently recommends-peening the pin'to_ hold it in plac The-licensee has identified 64. valves of this -type at the Summer Plan Inspections / evaluations.. have been7 performed on 63. valves as to .dat *

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Twelve (12) 'are pressure seal style valves l (900'lbs - 1200 lbs) and

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Valves that failed

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fifty-one (51) are 150lbs -' 300 lbs class valve' initial-inspections'had.one or more of the-following deficiencie's:

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(1) ' Set' screw tack welded 5- satisfactory 44 unsatisfactor (2) ' Cap screws tack welded 4- satisfactory '45 unsatisfactor .

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(3) Hinge support ' tack welded - 44- satisfactory 5 unsatis-

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.(4) Disc : Pin peened or' tack welded _ 32 satisfactory 15 P r unsati sfactor Rework / Repairs have been performed . on the above sixty-three. (63)

valves. . The ' remaining valve to be_ checked (XVC - 1900 MU) is a three inch check valve- in . the fill and recirculation line to the Reactor ( '

Makeup ' Water; Storage Tank. This valve will be inspected during the next scheduled outage. of sufficient duration to permit tank draining b

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and valve inspection. An engineering evaluation is currently being performed by .the licensee _ to allow continued operation of the -system until'this inspection can be accomplished. This item will be further evaluated by the- resident inspectors upon completion of the Part 21 Reportability - Evaluation by the licensee and inspection of the

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remaining valve. This item is identified as an inspector followup item (IFI). " Anchor / Darling Check Valves" IFI 395/85-42-0 ' On November 24, 1985, 9:15 p.m. ~with .the plant in mode 5, while -

performing STP 125.008 "A" Diesel Generator Refueling Operability Test,

number. 8 cylinder seized up, causing the diesel to fail. The diesel has'been repaired and tested satisfactorily. The licensee is presently performing an'indepth evaluation. A -special report will be submitted by the licensee on this event. The resident inspectors will evaluate this item in a subsequent repor . Refueling Activities (60710)

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The-inspectors reviewed licensee progress _to ascertain whether pre-refueling activities specified in the Technical Specifications (TS) have 'been completed and whether refueling activities are being conducted as required by TS or approved procedures. Specifically, the inspectors.(1) verit'ied that all surveillance testing required by_the TS and licensee procedures for fuel handling had been ' completed prior to the handling of fuel in the core, (2)_

verified that the periodic testing of refueling related ' equipment is being

. performed as . required by TS or- licensee administrative procedures, (3)

witnessed two shifts of fuel handling operations (removal, inspection,

_ sipping- and insertion) and other ongoing activities at the facility and

' verified that all - such activities were performed in accordance with TS requirements- and approved Lprocedures, (4) verified that containment-integrity was maintained as requi. red by TS; (5) verified by observation that the-licensee maintained good housekeeping in the refueling area, and (6)

. verified by observation that the licensee's staffing during refueling was in accordance with TS and approved procedure STP 131.001 -

Manipulator Crane Tes 'STP 125.008A -

Diesel Generator Refueling Operability Tes STP 125.0098 -

Diesel-Generator Refueling Operability Tes STP 555.001 -

Spent Fuel Pool Ventilation Canister Tes STP 555.002 -

Spent Fuel Pool Ventilation Systems Performance Tes Tech. Spec. 4.9.6.1. - Reviewed to insure that STP reflected and 4.9. T.S. requiitment STP 360.003 -

Reactor Building Manipulator Crane Area Radiation Monitors (RM G17A G178) Calibratio :Within the areas inspected, no violations or deviations were identified.

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6 ESF System Walkdown (71710)

The inspectors verified the operability of an engineered safety features (ESF) system by- performing a-walkdown of the accessible portions of the

- systems listed below. The inspectors confirmed that the licensee's system

. lineup procedures matched plant drawings and the as-built configuration. The inspectors looked for equipment conditions and items that might degrade performance (hangers and supports were operable, housekeeping, etc.) and

_ inspected the interiors of _ electrical and instrumentation cabinets for l debris, . loose material, jumpers, evidence of rodents, etc. The inspectors verified- that valves, including _ instrumentation isolation valves, were ;in

. proper position, power was available, and valves were locked as appropriat The inspectors compared both local and remote position indication , SOP 106 -

Reactor Makeup Wate Within the areas inspected, no violations or deviations were identifie . Operational Safety Verification (71707)

The inspectors observed licensee activities to ascertain that the facility-was being operated safely and in conformance with regulatory requirements, and'that the licensee's management control system is effectively-discharging its responsibilities for continued safe operation by direct observation of ~

activities,Ltours of the facility, interviews and discussions with licensee personnel , ; independent verification of safety system status- and limiting conditions for operation, and reviewing facility record STP 128.004 -

Diesel Fire Pum STP 122.001 -

Component ~ Cooling Water Valve Verificatio STP 115.012 -

Penetration Test Valve Line-Up Shee Within the areas inspected, no violations or deviations were identifie . Preparation for Refueling (60705)

The inspectors reviewed licensee preparations for refueling including the adequacy of procedures and administrative controls for the refueling activities / outage and for the receipt of new fuel. As part of this activity, the inspectors verified that technically adequate, approved procedures were available covering (1) the receipt, inspection and storage of new fuel, (2)

fuel handling, transfers and core verification, (3) the inspection of fuel to be reused, and (4) the handling and inspection of any other core internal ,

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Specifically, the following procedures were. reviewed in detail:

STP~110.001- -

Pre-Core' Alterations / Verificatio STP-118.006 -

' R. B. Purge.And Exhaust Tes STP 147.001- -

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B. Penetration Tes STP'360.034 -

'RM - A2 Operational-_ Tes 'Within the areasiinspected,'no violations or deviations were identifie <

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