IR 05000321/2019013

From kanterella
(Redirected from IR 05000366/2019013)
Jump to navigation Jump to search
Biennial Problem Identification and Resolution Inspection Report 05000321/2019013 and 05000366/2019013
ML19309C978
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 11/05/2019
From: Alan Blamey
NRC/RGN-II/DRP/RPB2
To: Gayheart C
Southern Nuclear Operating Co
Alan Blamey RGN-II/DRP/RPB2
References
IR 2019013
Download: ML19309C978 (18)


Text

November 5, 2019

SUBJECT:

EDWIN I. HATCH NUCLEAR PLANT - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000321/2019013 AND 05000366/2019013

Dear Ms. Gayheart:

On September 27, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Hatch Nuclear Plant, Units 1 and 2. On September 26, 2019 the NRC inspectors discussed the results of this inspection with Mr. Edwin D. (Sonny) Dean Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the plants corrective action program and the plants implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the plant was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the plants processes for use of industry and NRC operating experience information and the effectiveness of the plants audits and self-assessments. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the plants programs to establish and maintain a safety-conscious work environment and interviewed plant personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment.

Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

The NRC inspectors did not identify any finding or violation of more than minor significance. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Alan J. Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects

Docket Nos. 05000321 and 05000366 License Nos. DPR-57 and NPF-5

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000321 and 05000366

License Numbers:

DPR-57 and NPF-5

Report Numbers:

05000321/2019013 and 05000366/2019013

Enterprise Identifier: I-2019-013-0002

Licensee:

Southern Nuclear Operating Co., Inc.

Facility:

Edwin I. Hatch Nuclear Plant

Location:

Baxley, GA

Inspection Dates:

September 08, 2019 to September 26, 2019

Inspectors:

J. Hickman, Resident Inspector

D. Mas-Penaranda, Project Engineer

C. Stancil, Senior Fuel Facility Inspector

T. Su, Reactor Inspector

Approved By:

Alan J. Blamey, Chief

Reactor Projects Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Edwin I. Hatch Nuclear Plant in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the plants processes for use of operating experience, audits and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the plants programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B

1. Corrective Action Program Effectiveness

Problem Identification: The inspectors determined that the licensee was effective in identifying problems and entering them into the corrective action program and there was a low threshold for entering issues into the corrective action program. This conclusion was based on a review of the requirements for initiating condition reports as described in licensee procedure NMP-GM-002, "Corrective Action Program," and managements expectation that employees were encouraged to initiate condition reports. Additionally, site management was actively involved in the corrective action program and focused appropriate attention on significant plant issues.

Problem Prioritization and Evaluation: Based on the review of condition reports, the inspectors concluded that problems were prioritized and evaluated in accordance with the condition report significance determination guidance in procedure NMP-GM-002. The inspectors determined that adequate consideration was given to system or component operability and associated plant risk. The inspectors determined that plant personnel had conducted cause evaluations in compliance with the licensees corrective action program procedures and cause determinations were appropriate, and considered the significance of the issues being evaluated.

Corrective Actions: Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence. The inspectors reviewed condition reports and effectiveness reviews to verify that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to preclude repetition (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.

Based on the samples reviewed, the team determined that the licensees corrective action program complied with regulatory requirements and self-imposed standards. The licensees implementation of the corrective action program adequately supported nuclear safety.

2. Operating Experience

The inspectors determined that the station's processes for the use of industry and NRC operating experience information and for the performance of audits and self-assessments were effective and complied with all regulatory requirements and licensee standards. The implementation of these programs adequately supported nuclear safety. The inspectors concluded that operating experience was adequately evaluated for applicability and that appropriate actions were implemented to address lessons learned as needed. The inspectors determined that the licensee was effective at performing self-assessments and audits to identify issues at a low level, properly evaluated those issues, and resolved them commensurate with their safety significance.

3. Self-Assessments and Audits

The inspectors determined that the scopes of assessments and audits were adequate. Self-assessments were generally detailed and critical. The inspectors verified that condition reports (CRs) were created to document areas for improvement and findings resulting from self-assessments, and verified that actions had been completed consistent with those recommendations. Audits of the quality assurance program appropriately assessed performance and identified areas for improvement. Generally, the licensee performed evaluations that were technically accurate.

4. Safety Conscious Work Environment

Based on interviews with plant staff and reviews of the latest safety culture survey results to assess the safety conscious work environment on site, the inspectors found no evidence of challenges to the safety conscious work environment. Employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

Minor Violation 71152B Minor Violation: The team identified one minor violation of 10 CFR 54.29 (a)(1), Standards for issuance of a renewed license, which states that managing the effects of aging during the period of extended operation on the functionality of structures and components that have been identified to require review under § 54.21(a)(1) is a requirement. Updated Final Safety Analysis Report (FSAR) chapter 18 discusses how the licensee will meet this requirement. Specifically, section 18.2.16(B), Wetted Cable Activities, discusses the commitment to maintain the water level below the routed cable. The licensees failure to maintain water level below the routed cables as described in FSAR was a performance deficiency (PD).

Contrary to this requirement, multiple condition reports (CR) have identified pull boxes, with safety related cables that were submerged. Pull-boxes PB1-AA, PB1-W, PB1-AE, PB1-AM, PB1-AB and PB1-AJ had high water levels that submerged the cables several times during the time frame from 2012 to 2019. Specially, Plant Service Water cable 1P41C001A and 1P41C001C, which routed through pull box PB1-AA, exhibited cable degradation as indicated by the licensees tan delta (TD) test results.

Screening: The inspectors determined the performance deficiency was minor. The PD was determined to be minor because although the cables were known to be repeatedly submerged, the licensee has implemented a PM program that performs TD test on the cables, to monitor degradation and replace the cable to ensure continued operability and functionality of the cable. Also, the team determine that the performance deficiency would not reasonably be viewed as a precursor to a significant event, if left uncorrected, the performance deficiency would not have the potential to lead to a more significant safety concern, the performance deficiency does not relate to a performance indicator that would not have caused the performance indicator to exceed a threshold, and the performance deficiency would not adversely affect the associated cornerstone objective.

Enforcement:

This failure to comply with 10 CFR 54.29 (a)(1) constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

The licensee initiated CR 10649708 to document the condition.

Observation: Corrective Action Program Effectiveness 71152B Operator Burdens, Workarounds, and Control Room Deficiencies

The inspectors performed a review of Operator Burdens, Workarounds, and Control Room Deficiencies. The inspectors observed that the Operations Performance Indicators for Control Room deficiencies were not meeting the goal of less than or equal to eight deficiencies 97% of the time over the past year. The inspectors observed that there continued to be material problems resulting in compensatory actions affecting Operators, as documented in CRs during this period. Although there were no defined workarounds, there were numerous compensatory action requirements due to plant and control room deficiencies (Unit 1 with 15 and Unit 2 with 16) which created a cumulative impact to the operators. In October of 2018 the Corporate Functional Area Manager identified that Hatch did not perform the quarterly Aggregate Operator Impact review (CR 10546353), which would assess these cumulative impacts. The inspectors reviewed the 2018 fourth quarter Aggregate Operator Impact review and found the assessment conclusions did not detail the nature of the impact, the expected actions that would reduce the impact, or whether the work order priority was raised for four assessment areas rated as Yellow, as required by NMP-OS-006-002, Aggregate Operator Impact Review Instruction Version 2.2. The inspectors review of the 2019 second quarter Aggregate Operator Impact Review identified the licensees review, again did not detail the nature of the impact and actions to reduce the impact for five Yellow and one Red rated assessment areas (CR 10649106). Additionally, a Red rated assessment area also requires a condition report, which was not generated (CR 10647593).

These issues were captured in the licensees corrective action program under the condition reports (CR) listed above.

The inspectors reviewed a cause determination report summary for a Nuclear Safety Review Board area for improvement that created a corrective action to review the Aggregate Operator Impact assessment with the operators monthly (CAR 276602), which should assist in establishing a detailed impact to operators and work order priorities.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On September 26, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Mr. Edwin D. (Sonny) Dean Site Vice President and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective

Action

Documents

Condition Report

(CR) 10322670,

1035672,

10376061,

10382838,

10382949,

10384058,

10394854,

10398751,

10423345,

10436191,

10439652,

10439685,

10440145,

10441129,

10443004,

10445377,

10446627,

10452310,

10455235,

10458608,

10458693,

10460506,

10460865,

10461039,

10462099,

10463114,

10463685,

10471189,

10482986,

10483331,

10490316,

10490318,

10491460,

10494315,

10497330,

10503641,

10504996,

10506730,

10508514,

10509191,

10509236,

10509253,

10509935,

10512351,

10524244,

10525213,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

10525233,

10525236,

10525887,

10526197,

10539657,

10540144,

10546353,

10548933,

10574618,

10574782,

10577264,

10579200,

10579232,

10579960,

10580065,

10582456,

10583074,

10585063,

10585867,

10585783,

10585867,

10586270,

10588709,

10591143,

10591504,

10592769,

10594302,

10594633,

10594635,

10599418,

10594968,

10601829,

10603492,

10603955,

10604132,

10607734,

10610185,

10610186,

10610196,

10611235,

10612038,

10616583,

10617753,

10619230,

10619830,

10620210,

10620226,

10620227,

10625975,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

10627164,

10627536,

10628350,

10634922,

10635643,

10635649,

10635842,

10638972,

10639059,

10641139,

10645239,

10848082

Corrective Action

Reports (CAR)

268718, 272275,

273910, 275619,

275824, 275864,

275939, 275982,

276602

CR 10582457,

10556842

CAR 275228

TE 1030941

Licensee Identified Violation

(LIV) from 4Q18 Integrated

Inspection

CRs: 10443379,

WOs: SNC

896726

Tan Delta Plots:

NMP-ES-051-002,

1C PSW Pump -

1P41C001C New,

1D PSW Pump -

1P41C001D new,

1E11C001A - R22-

S005-ES1-M01,

1E11C001A 2017-

-08-30,

1E11C001B,

1E11C001B - R22-

S0007-ES2-M01,

1E11C001C,

1E11C001C 2019-

05-09,

1E11C001D,

1E11C001D

Withstand,

1E11C002A - R22-

S005-ES1-M05,

1E11C002A 2018-

Pull boxes discovered with

higher than acceptable

water levels during weekly

inspection

2/28/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

01-31,

1E11C002B - R22-

S007-ES2-M05,

1E11C002B 2018-

2-14,

1E11C002C -

R22-S006-ES2-

M07, 1E11C002C

2018-02-01,

1E11C002D -

R22-S006-ES1-

M05, 1E11C002D

2018-02-14,

1E21C001A - R22-

S005-ES1-M07,

1E21C001A 2018-

01-28,

1E21C001B - R22-

S007-ES-M006,

1P41C001A - R22-

S005-ES1-M02,

1P41C001A 2018-

04-10,

1P41C001A 2018-

04-10 Tan Delta,

1P41C001A

Withstand Test,

1P41C001B - R22-

S007-ES2-M03,

1P41C001B - R22-

S007-ES2-M03,

1P41C001C,

1P41C001D,

1E11C001D

Phase B 2018-08-

17, 2E11C001A,

2E11C001C,

2E11C002A -

EAE187M01,

2E11C002A 2019-

01-28,

2E11C002B,

2E11C002BC002B

2019-02-01,

2E11C002C,

2E11C002C 2019-

01-30,

2E11C002D,

2E11C002D 2019-

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2-17,

2E21C001A,

2E21C001A 2019-

01-31,

2E21C001B,

2E21C001B 2019-

2-19,

2P41C001A 2010-

11-29,

2P41C001A 2018-

03-25,

2P41C001C -

PUE137M02,

2P41C001C short,

R22-S007-ES-M02

Phase B,

Corrective

Action

Documents

Resulting from

Inspection

10649708

Cables Submergence in

Various Pull Box

09/26/2019

Condition Report

(CR) 10645352,

10645692,

10647593,

10649106,

10649651

Drawings

B-28015

Unit 1 and 2 Isometric Drain

Lines for Att 5 Racks

Revision 0

B-45555

Seismic Configuration

Control Requirements

Version 3.0

H-16062

Nuclear Boiler System

P&ID

Version

57.0

H-16332

Unit No. 1 HPCI System

P&ID

Version

67.0

H-23352

Single Line Drawing

Emergency Station Service

Ver. 24.0

H-23358

Single Line Diagram 4160 V

Bus 2 G

Revision

21.0

H-23362

Single Line Diagram 600 V

Bus 2C & 2D

Version

39.0

H-26020

Unit No. 2 HPCI System

P&ID

Version

2.0

H26015

RHR System P&ID

Version

60.0

Engineering

Changes

C102092301E001

Secondary Containment

Airlock R311A Door Strike

Minor Modification

Version 1.0

NMP-ES-084-001-

F20

Configuration Change

Evaluation: LED Lighting

Project RX Bldg U1

Version 2.0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Diagonals, 130', 228'

TE 1042135, TE

1042136, TE

1042137, TE

1042138, TE

1042139, TE

1042141, TE

1045856, TE

1048493

(CAR) 275842

Work Orders, SNC

1000764, SNC

1000804, SNC

1000857, SNC

1000858, SBC

1000859, SNC

1000860, SNC

1000861, SNC

1000862, SNC 1---

880, SNC

1001043, SNC

1001132, SNC

1001133

Various TE, CAR and WOs

associated with 2R23-S004

'2D' Bus Tripped

Engineering

Evaluations

TE 1025851, TE

1040661, TE

1039100, TE

1043387, TE

1042852, TE

1044112, TE

1044113, TE

1044114, TE

1044115, TE

1044116, TE

1044118, TE

1044119, TE

1044129, TE

1044131, TE

1044131,

Miscellaneous

Lighting Plan Maintenance

Update

08/20/2019

Maintenance Rule Expert

Panel Meeting Agenda

09/17/2019

CRD Daily Counts

09/24/2019

HPCI System Health Report Current

LER 2018-03

SRV As Found Testing

Results Out of Tolerance

Revision 00

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NL-17-0328

Application to Revise

Technical Specifications to

Adopt TSTIF-542, Reactor

Pressure Vessel Water

Inventory Control

04/20/2017

PMCR 88060

Create storage PM for item

2239

05/25/2017

TE 1042135

Fatigue Management

Program Review

5/6/2019

Operability

Evaluations

PDO 1-10-02

Wetted Cables

Revision 3

PDO 1-17-003/2-

17-004

Prompt Determination of

Operability for 23 Safety

Related Breakers failed to

close on demand

10/24/2018

PDO 1-18-006

Prompt Determination of

Operability for Steam Leak

on 1E41-F003, HPCI Steam

Supply Outboard PCIV

Rev. 0

PDO 2-18-002

Prompt Determination of

Operability of Unit 2 RHR.

while performing 34SV-

E11-001-2, when RHR

pump was started the min

flow valve went closed an

then back open.

2/01/2018

Procedures

31GO-OPS-025

Reactor Pressure Vessel

Water Inventory Control

Version 3.3

34AR-603-902-1

ARP's For Control Panel

1H11-P603

Version No:

20.1

34SO-B21-001-1

Automatic Depressurization

System (ADS)

Version

2.12

2CM-MNT-033-0

BETTIS 522C-SR Actuator

Corrective Maintenance

Version 4.3

2PM-L48-001-1

Unit 1 Secondary

Containment Doors

Preventive Maintenance

Version 9.2

2PM-R24-004-2

Pan Assembly Cleaning

and Inspection

Version 8.5

57CP-C51-001-0

SRM Detector Testing

Version 5.0

57CP-C51-001-0

SRM Detector Testing

Version

%.0

57CP-C51-002-0

IRM Detectpr Testing

Version 3.3

57CP-C51-002-0

IRM Detector Testing

Version 3.3

AG-MGR-01-0783

Processing Administrative

Guidelines and

Departmental Instructions

Version 6.2

AG-MGR-68-

200N

Climbing On Plant

Equipment

Revision 2

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NEI 99-02

Regulatory Assessment

Performance Indicator

Guideline

Revision 7

NMP -AD-006

Infrequently Performed

Tests and Evolutions

Version

2.8

NMP-ES-006

Preventive Maintenance

Implementation and

Continuing Equipment

Reliability Improvement

Version

10.1

NMP-ES-027

Maintenance Rule Program

Version

10.0

NMP-ES-051

Cable Monitoring Program

Version 9.1

NMP-ES-051-004

Pull Box Inspection

Procedure

Version 5.2

NMP-GM-002

Corrective Action Program

Version

15.1

NMP-GM-002-001

Corrective Action Program

Instructions

Version

38.1

NMP-GM-002-002

Effectiveness Review

Instructions

Version 5.2

NMP-GM-002-

GL03

Cause Analysis and

Corrective Actions

Guideline

Version

30.0

NMP-OS-006-002

Aggregate Operator Impact

Review Instruction

Version 2.2

NUMARC 93-01

Industry Guideline for

Monitoring the

Effectiveness of

Maintenance at Nuclear

Power Plants

Revision

4A

OS-BP-001

Operations Performance

Indicators

Version 4.6

Self-

Assessments

HNP Aggregate Impact

Review for 4th Quarter

2018

Version 0

HNP Aggregate Impact

Review for 2nd Quarter

2019

Version 0

Work Orders

SNC1024503

Repair leak on HPCI Room

cooler

06/03/2019

SNC440323

Secondary Containment

Airlock R311A Door Strike

Modification

10/28/2019

SNC841609

Secondary Containment

Airlock R311A Horn and

MCR Alarm

08/03/2017

SNC880463

Secondary Containment

Airlock R311A Lights

01/25/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Malfunctioning

SNC891848

Tech Spec 3.3.5.1-1(3d)

has been identified as non-

conservative, CST Level

Switch (Swapover)

08/28/2017

SNC922120

Investigate Unit 2 "A" RHR

Minimum Flow Valve

09/27/2018

SNC926414

Secondary Containment

Airlock R311A Door Won't

Stay Closed, Failed

Interlock

07/21/2018

SNC947221

Repair Concrete Removed

for UT Inspection around

U1 Core Spray Suction Line

at CST

5/22/2018

SNC955966

Repair of Insulation near

1E41F3025