IR 05000338/2019002

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Integrated Inspection Report 05000338/2019002 and 05000339/2019002; 07200056/2019001
ML19217A249
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 08/05/2019
From: Bradley Davis
NRC/RGN-II/DRP/RPB4
To: Stoddard D
Virginia Electric & Power Co (VEPCO)
Geanette D
References
IR 2019001, IR 2019002
Download: ML19217A249 (17)


Text

August 5, 2019

SUBJECT:

NORTH ANNA POWER STATION - INTEGRATED INSPECTION REPORT 05000338/2019002 AND 05000339/2019002; 07200056/2019001

Dear Mr. Stoddard:

On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at North Anna Power Station. On July 17, 2019, the NRC inspectors discussed the results of this inspection with Mr. Larry Lane and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspectors did not identify any finding or violation of more than minor significance.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Bradley J. Davis, Chief Reactor Projects Branch 4 Division of Reactor Projects

Docket Nos. 05000338 and 05000339

07200056 License Nos. NPF-4 and NPF-7

SNM-2507

Enclosure:

Inspection Report 05000338/2019002; 05000339/2019002;

and 07200056/2019001

Inspection Report

Docket Numbers:

05000338 and 05000339

07200056

License Numbers:

NPF-4 and NPF-7

SNM-2507

Report Numbers:

05000338/2019002 and 05000339/2019002

07200056/2019001

Enterprise Identifier: I-2019-002-0029

I-2019-001-0119

Licensee:

Virginia Electric & Power Co.

Facility:

North Anna Power Station

Location:

Mineral, VA

Inspection Dates:

April 1, 2019 to June 30, 2019

Inspectors:

M. Tobin, Senior Resident Inspector

G. Eatmon, Resident Inspector

R. Carrion, Senior Reactor Inspector

C. Fontana, Emergency Preparedness Inspector

R. Kellner, Senior Health Physicist

S. Sanchez, Senior Emergency Preparedness Inspector

J. Tornow, Physical Security Inspector

Approved By:

Bradley J. Davis, Chief

Reactor Projects Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a integrated inspection at North Anna Power Station in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Failure to Adequately Implement the Equipment Clearance Procedure Cornerstone Significance Cross-cutting Aspect Report Section Not Applicable NOV 05000338/2019001-01 Closed EA-18-159 Not Applicable Not Applicable A licensee-identified Severity Level IV violation (NOV) of TS 5.4.1.a, Procedures, was identified when the licensee failed to adequately implement licensee procedure OP-AA-200,

Equipment Clearance.

PLANT STATUS

Unit 1 operated at or near rated thermal power for the entire inspection period.

Unit 2 began the inspection period at zero percent power for a planned refueling outage. On April 12, 2019, the unit was returned to rated thermal power. On June 25, 2019, the unit was downpowered to 8 percent thermal power due to a hotspot in the transformer yard, was returned to rated thermal power on June 29, 2019 following repairs, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated readiness to cope with external flooding for the following areas on May 23, 2019:
  • General site area
  • Safeguards buildings

Impending Severe Weather Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated readiness for impending adverse weather conditions for high winds and severe thunderstorms on May 22, 2019.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1, emergency diesel generator starting air, 'H' and 'J' EDG, train 'A' and 'B' on April 26, 2019.
(2) Units 1 & 2 fire water system main header loop on May 8, 2019.
(3) Units 1 & 2 safety related portions of the instrument air system on June 14, 2019.
(4) Unit 2, quench spray system, train B on June 16, 2019.

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 2 emergency switchgear instrument rack and air conditioning rooms on April 10, 2019
(2) Unit 2 Auxiliary Feedwater Pumphouses on April 10, 2019
(3) Spent fuel storage area on June 13, 2019
(4) Unit 2 quench spray pump house on June 16, 2019
(5) Unit 1 and 2 auxiliary feedwater pump house on June 18, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during risk significant plant conditions such as power changes, completed on June 27, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated simulator control room activities during a station emergency preparedness drill on May 14, 2019.

71111.12 - Maintenance Effectiveness

Quality Control (IP Section 02.02) (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

(1) Diesel fire pump failure on June 9, 2019

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Required seals on building roofs and groundwater inleakage control in the safeguards building following a sump pump failure on May 7, 2019.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2 elevated risk due to lifting and rigging associated with condensate pump 'A' motor replacement and Unit 2 startup concluding on April 26, 2019
(2) Units 1 and 2 protected equipment with the C station reserve transformer out of service for transformer replacement on May 15, 2019
(3) Fire drill being conducted in the emergency switchgear room during cable pulls for the C station reserve transformer replacement on May 17, 2019.
(4) Cable manhole inspection periodicity going from periodic to on-demand on May 13, 2019
(5) Unit 2 emergent work control for hot spot identified on main transformer 'C' bushing and associated down power with 'B' Service water header out of service on June 25, 2019
(6) Diesel fire pump failure requiring replacement and station priorities during pump outage on June 20, 2019.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 1 and Unit 2, updated margin for unqualified coatings in containment on May 15, 2019
(2) Boric acid tank operability with non-functional heat trace on the tank on May 10, 2019
(3) Part-21 notice for Hytork Actuators on May 30, 2019
(4) Unit 1 charging pump 'C' inoperable due to temperature indicting controller failure for the pump lube oil cooler on June 16, 2019
(5) Unit 2 seal water injection valve leaking on June 20, 2019

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Unit 2 outside recirculation spray pump 'A' seal replacement, 2-RS-P-2A completed on April 26, 2019
(2) Units 1 and 2 EDG coolant changeout using bleed and feed method completed on May 26, 2019
(3) Unit 1 main control room chiller 'A' maintenance, 1-HV-E-4A, completed on June 14, 2019
(4) Unit 2 rod control cabinet 2BD non-urgent failure alarm on June 21, 2019
(5) Unit 2 exciter field breaker 2-EP-BKR-41 replacement and testing using 2-OP-15.2, Main Generator Operation, on June 27, 2019
(6) Unit 2 component cooling water heat exchanger testing following tube cleaning with non-standard cleaning tools on June 20, 2019
(7) Unit 2 N42 power range instrument was declared inoperable and replaced on June 26, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated refueling outage 2R26 activities from April 1, 2019, to April 9, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Inservice Testing (IP Section 03.01)

(1) Unit 1, Charging pump 'C' (1-CH-P-1C), on June 14, 2019

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1) Unit 2 Degraded voltage/loss of voltage operational and Emergency Safeguards Function response time test: 2J bus on April 18, 2019
(2) Unit 2 rod drop timing test on May 7, 2019
(3) Unit 2 A train containment air recirculation fan inside isolation air return valve stroke time test on May 30, 2019

71114.02 - Alert and Notification System Testing

Inspection Review (IP Section 02.01-02.04) (1 Sample)

(1) The inspectors evaluated the maintenance and testing of the alert and notification system during the week of June 10, 2019

71114.03 - Emergency Response Organization Staffing and Augmentation System

Inspection Review (IP Section 02.01-02.02) (1 Sample)

(1) The inspectors evaluated the readiness of the Emergency Response Organization during the week of June 10, 2019

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated submitted Emergency Action Level, Emergency Plan, and Emergency Plan Implementing Procedure changes during the week of June 10, 2019. This evaluation does not constitute NRC approval.

71114.05 - Maintenance of Emergency Preparedness

Inspection Review (IP Section 02.01 - 02.11) (1 Sample)

(1) The inspectors evaluated the maintenance of the emergency preparedness program during the week of June 10, 2019

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Licensee drill and notification procedure performance on May 14,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI02: RCS Leak Rate Sample (IP Section 02.11)===

(1) Unit 1 (June 2018 - March 2019)
(2) Unit 2 (June 2018 - March 2019)

EP01: Drill/Exercise Performance (IP Section 02.12) (1 Sample)

(1) EP01: Drill & Exercise Performance for the period July 1, 2018, through March 31, 2019

EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)

(1) EP02: Emergency Response Organization Drill Participation for the period July 1, 2018, through March 31, 2019

EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)

(1) EP03: Alert & Notification System Reliability for the period July 1, 2018, through March 31, 2019

MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)

(1) Unit 1 (June 2018 - March 2019)
(2) Unit 2 (June 2018 - March 2019)

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 (June 2018 - March 2019)
(2) Unit 2 (June 2018 - March 2019)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Appendix R fire cooldown methodology

NRC inspectors reviewed condition report CR1123506, which identified the station's concerns with the current Appendix R cooldown methodology. Specifically, the licensee questioned if the procedures in place for postulated fires in the Unit 1 and Unit 2 emergency switchgear rooms, Unit 1 and Unit 2 cable vault and tunnels, Unit 1 and Unit 2 containment buildings, and the main control room would have successfully allowed the unit to cool down to cold shutdown conditions within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> as required by Appendix R. As a compensatory measure while the calculations are being reworked, the licensee established hourly roving fire watches for the affected areas, and established an interim process to inform the emergency response teams on site of the potential to not be able to meet the requirements using existing procedural guidance. The site continues to have the ability to achieve and maintain safe and stable conditions following any postulated fire.

(2) Safety Conscious Work Environment

NRC inspectors reviewed the stations programs to establish and maintain a safety-conscious work environment (SCWE), and interviewed station personnel to evaluate the effectiveness of these programs specifically in the licensees physical security department. During the inspection, inspectors assessed whether issues exist that may represent challenges to the free flow of information, and whether underlying factors exist that would produce a reluctance to raise nuclear safety concerns. Based on insights obtained from safety culture interviews, and discussions with management and Employee Concerns Program (ECP) personnel, the inspectors found no evidence of challenges to the organizations safety-conscious work environment. Most personnel were comfortable using the corrective action program, and appeared willing to raise nuclear safety concerns through at least one of the several means available.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants Operation of an Independent Spent Fuel Storage Installation at Operating Plants

(1) The inspectors evaluated the licensees independent spent fuel storage installation (ISFSI) cask loadings from April 29 through May 2, 2019. Specifically, the inspectors reviewed the normal operation of the ISFSI as the licensee loaded dry shielded canister (DSC) 062 and transferred it to horizontal storage module (HSM) 31 on the ISFSI pad. The inspectors reviewed evaluations required by 10 CFR 72.212(b), 10 CFR 50.59, and 10 CFR 72.48 and changes made to the ISFSI program and associated procedures to verify that changes were consistent with the license or CoC and did not reduce the effectiveness of the program and that the procedures continued to fulfill the commitments and requirements specified in the SAR, SER, CoC, 10 CFR Part 72, and the general license. The inspectors verified that the loading activities and transfer activities to the pad were performed in a safe manner and in compliance with approved procedures and that surveillance activities have been conducted at the specified periods. The inspectors verified that the licensee identified each fuel assembly placed in the ISFSI, recorded the parameters and characteristics of each fuel assembly, and maintained a record of each fuel assembly as a controlled document. The inspectors evaluated the effectiveness of the licensees management oversight and QA assessments of ISFSI activities for the loading operations and transfer activities to the pad.

During the course of the loading activities, the inspectors observed the following;

  • Heavy load movement of the Transfer Cask (TC) loaded with DSC 062
  • Drying and backfill evolutions
  • Closure welding and non-destructive weld evaluations
  • Transfer and transport evolutions
  • Radiological field surveys

The inspectors also evaluated the following corrective action documents:

  • CA 7590652, Review the Requirements for Building Inspection Along the Haul Path
  • CR 1082061, TN-32 Cask Lifting Procedures Need Additional Content for NUREG-0612 Heavy Loads Commitments
  • CR 1112483, Plant Equipment Modified without Required Design Change Documentation
  • CR 1122388, NRC Question Regarding Spent Fuel Cask Haul Route

INSPECTION RESULTS

Assessment - NOV 05000338/2019001-01 Closure

The inspectors reviewed the licensees response to NOV 05000338/2019001-01 and determined that the reason, corrective actions taken to address recurrence, and the date when full compliance was achieved for this violation is adequately addressed and captured on the docket. This closes NOV 05000338/2019001-01.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On July 17, 2019, the inspectors presented the integrated inspection results to Mr. Larry Lane and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

60855.1

Calculations

Calculation

Number SF-0005

Standoff Distances for Gasoline Use at the ISFSI

Revision 0

Corrective Action

Documents

CA 7590652

Review the Requirements for Building Inspection Along the

Haul Path

CR 1082061

TN-32 Cask Lifting Procedures Need Additional Content for

NUREG-0612 Heavy Loads Commitments

CR 1112483

Plant Equipment Modified without Required Design Change

Documentation

Corrective Action

Documents

Resulting from

Inspection

CR 1122388

NRC Question Regarding Spent Fuel Cask Haul Route

CR 1122397

NRC Observations during ISFSI Inspection

Engineering

Changes

Design Change

No.07-017

Haul Route Assessment/NAPS/Units 1 and 2

February 8,

2011

Engineering

Evaluations

ETE-NAF-2010-

0003

North Anna Power Station Independent Spent Fuel Storage

Installation 10 CFR 72.212 Evaluation Report

Revision 5

Miscellaneous

Virginia Electric

and Power

Company Letter

18-108

Virginia Electric and Power Company Letter 18-108, sending

CFR 72.48 Evaluation NAPS 0-EVAL-2017-0012 for

bolting of cask lid of High Burn-up Demonstration (HBU)

cask to the NRC

March 28,

2018

Virginia Electric

and Power

Company Letter

19-177

Virginia Electric and Power Company Letter 19-177, sending

the Annual Radiological Environmental Operating Report for

North Anna Power Station Unit Nos. 1 and 2 and the

Independent Spent Fuel Storage Installation (ISFSI) to the

NRC

April 26,

2019

Procedures

0-OP-4.5

NUHOMS32 PTH Shielded Canister Loading and Handling

Revision 14

0-OP-4.52

NUHOMS Vacuum Drying System Operation

Revision 14

0-OP-4.54

Transfer Cask/Dry Shielded Canister Transfer to ISFSI and

Dry Shielded Canister Transfer from Transfer Cask to

Horizontal Storage Module

Revision 10

GQP-9.2-10

High Temperature Liquid Penetrant Examination and

Acceptance Standards for Welds, Base Materials and

Revision 0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Cladding

GQP-9.6-18

Visual Examination of Welds

Revision 0

NF-AA-NSF-601

NUHOMS HD Transfer Haul Route Walkdown

Revision 4

PI-CNSTR-OP-

DOM-T-01-04

Closure Welding of Transnuclear NUHOMS Dry Shielded

Canisters for Dominion Nuclear at the Millstone, North Anna

& Surry Power Stations

Revision 0

71111.01

Corrective Action

Documents

Resulting from

Inspection

CR1123832

CR1125869

Procedures

0-PT-9.4

Inspection of Roof Drains, Yard Drains, and Roofs

71111.04

Calibration

Records

01-EG-RV-601HA

Relief/Safety Valve Database

4/17/2019

01-EG-RV-601JB

Relief/Safety Valve Database

4/17/2019

01-EG-RV-602HA

Relief/Safety Valve Database

4/17/2019

01-EG-RV-602JB

Relief/Safety Valve Database

4/17/2019

Corrective Action

Documents

CR1089958

Minor boric acid discovered on 2-QS-17

2/14/2018

CR1117219

Safety Valve Manual Lifting Levers are not in Compliance

with Code Requirements

3/4/2019

Corrective Action

Documents

Resulting from

Inspection

CR1120555

NRC Identified - Relief Valve Handles Secured Down

4/12/2019

CR1121268

2-QS-P-1B boric acid leak

4/19/2019

Drawings

11715-FB-101E

Valve Operating Numbers Underground Fire Protection

System Warehouse 5 and Training Center Area

11715-FM

Flow/Valve Operating Numbers Diagram Compressed Air

System

Miscellaneous

1-EG-TK-1HA

Certificate of Inspection

2/1/2017

1-EG-TK-1HB

Certificate of Inspection

2/1/2017

Procedures

0-PT-100.3

Fire Protection Valve Verification

1-OP-6.7A

Operating Procedure - Valve Checkoff Diesel Starting Air

2-OP-7.4A

Operating Procedure - Valve Checkoff - Quench Spray

System

71111.04S

Drawings

11715-FB-101A

Valve Operating Numbers Diagram Underground Yard

Water and Fire Protection

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.05Q Corrective Action

Documents

Resulting from

Inspection

CR1125934

NRC issue of concern for discrepancies in pre-fire plans for

U2 QSPH and ASWPH

6/27/2019

Engineering

Evaluations

NA-2011-0021

Evaluation of Permanently Stored Combustible Material

Fire Plans

1-FS-ASWP-1

Aux. Service Water Pumphouse

10/3/1994

2-FS-QS-1

Quench Spray Building 274' Safe shutdown Equipment

5/28/1992

Procedures

CM-AA-FPA-100

Fire Protection/Appendix R (Fire Safe Shutdown) Program

ETE-NA-2011-

21

Evaluation of Permanently Stored Combustible Material

71111.11Q

2-OP-2.1

Unit Startup from Mode 2 to Mode 1

28

2-OP-2.2

Unit Power Operation from Mode 1 to Mode 2

NMAY19FD

Emergency Plan Drill

71111.12

Corrective Action

Documents

CA7594994

CA7594994

CA7618752

CR1069331

CR1076213

CR1122557

CR1122557

CR1124204

CR1124441

CR1124509

CR1124544

Work Orders

WO59203291251

WO59203292806

71111.13

Corrective Action

Documents

CR1122475

CR1125681

Unit 2 "C" Main TX H2 (Neutral) connection hotspot

6/24/2019

Corrective Action

Documents

Resulting from

Inspection

CR1121700

NRC question the rigor involved in determining whether a

scaffold would interfere with BDB equipment

4/24/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Miscellaneous

"B" SW header outage plan

6/25/2019

High Risk Plan Actions for 2-CN-P-1A - Upper motor bearing

failure

4/9/2019

"B" SW header outage plan

6/28/2019

2-EP-MT-1C

Forced Outage plan

6/28/2019

2-EP-MT-1C

Forced outage plan

6/25/2019

ODM CA7566215

Operational Decision Making for 02-CN-P-1A

4/10/2019

P-NANN-427513

Manhole - Pumping

04/05/2017

Procedures

2-AP-2.2

Fast Load Reduction

2-AP-31

Loss of Main Feedwater

ER-AA-PRS-1011

Just in Time Preventive Maintenance Review Process

MA-AA-105

Scaffolding

WM-AA-301

Operational Risk Assessment

Work Orders

203289710

Scaffolding Order

4/9/2019

71111.15

Calculations

ME-0780

Post LOCA Debris Transport to Containment Sump Strainer

for Resolution of GSI-191

Corrective Action

Documents

21529

2-CH-22d reachrod may have come disconnected from

actual valve handwheel

4/22/2019

CA7605926

Level of Effort for failed 1-SW-TIC-102C, "C" charging pump

temperature indicating controller

6/12/2019

CR1118930

CR1121553

4B seal water injection vent valve 2-CH-225

4/23/2019

CR1122181

CR1122216

CR1122241

CR1122304

CR1123245

1-SW-TI-103C pegged high

5/13/2019

CR1123471

CR1123644

Engineering

Changes

DC-07-172

PREACS Bypass Damper Replacements/NAPS/Units 1&2

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Engineering

Evaluations

Engineering

Transmittal SE

97-055

Charging Pump Lube Oil Temperature Low Limit

4/9/1997

ETE-NA-2014-

0046

Updated Margin for Unqualified Coatings in Containment

4/29/2019

Miscellaneous

Technical Report

No NAN2-34325-

TR-001

Reduced-Scale Testing for North Anna 1 and 2

Replacement Containment Sump Strainers

2/28/2009

Procedures

1-AR-33

North Anna Power Station Annunciator Response; Heat

Tracing Annunciator 1-LOG-4

C CH PP Low CLR SW Out Temperature

3/27/2015

2-AR-A-D1

Rod Control Urgent Failure

2-LOG-20

ECCS Leakage Log

4/23/2019

2-PT-59.3

Heat Tracing Operational Test

CM-AA-CTG-101

Coating Service Level 1 Application

Work Orders

WO59203279108

WO59203291877

Installation of Brace Kits for PREACS Bypass Dampers

WO59203291879

WO59203291929

Installation of Brace Kits for PREACS Bypass Dampers

71111.19

Corrective Action

Documents

CR1121154

Received annunciator 2A-D2 (rod control non-urgent failure)

4/18/2019

CR1125524

Received Annunciator 2A-D2 (rod control non-urgent failure)

6/21/2019

CR1125775

N42 indication erratic

6/26/2019

CR1125777

Found U2 PCS point N00044A with security level zero

6/26/2019

Procedures

2-OP-15.2

Main Generator Operation

0-MOP-49.30

Draining SW from CC Heat Exchangers

1-MOP-6.94

1J EDG Coolant Changeout Using Bleed and Feed Method

1-MOP-6.95

1H EDG Coolant Changeout Using Bleed and Feed Method

1-PT-77.11A

Control Room Chiller 1-HV-E-4A Pump and Valve Test

6/14/2019

2-AP-4.3

Malfunction of Nuclear Instrumentation (Power Range)

2-AR-A-D2

Rod Control Non-Urgent Failure

Work Orders

59101675190

2-RS-P-2A-Pump Seal Replacement

3/29/2019

203290549

6/21/2019

203293442

6/26/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.22

Calculations

CALC-59-01-PT-

14.3-08

Charging pump 1-CH-P-1C revise acceptance criteria for

hydraulic and vibration data

7/29/2011

Engineering

Changes

ET NAF-2003-

0005

Elimination of Seismic Allowance from Control Rod Drop

Times, North Anna Power Station, Units 1 and 2

01/16/2003

TSCR N-008

Bases for SR 3.1.4, Rod Group Alignment Limits

06/11/2002

Miscellaneous

1-CH-P-1C

Normal

Machine History Report

6/27/2019

IST Program

Basis Document,

Int 4

Inservice Testing (IST) Program Basis Interval 4

6/9/2017

Procedures

1-PT-14.3

Operating Periodic Test, Charging Pump 1-CH-P-1C

2-PT-36.11J

Degraded Voltage/Loss of Voltage Operational and ESF

Response Time Test: 2J Bus

2-PT-83.12J

2J Diesel Generator Test (Start by ESF Actuation) Followed

by 24-Hour Run and Hot Restart Test

71114.06

NMAY19FD

Emergency Plan Drill

71152

Calculations

SM-1841

Appendix R Emergency Switchgear Room (ESGR) Fire

Natural Circulation Cooldown for NAPS

Corrective Action

Documents

CR1092157

CR1123506

Procedures

1-FCA-2

Emergency Switchgear Room Fire

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