IR 05000334/2017003

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Integrated Inspection Report 05000334/2017003 and 05000412/2017003
ML17305B003
Person / Time
Site: Beaver Valley
Issue date: 10/26/2017
From: Silas Kennedy
Division Reactor Projects I
To: Bologna R
FirstEnergy Nuclear Operating Co
Kennedy S
References
EA-17-045 IR 2017003
Download: ML17305B003 (26)


Text

October 26, 2017

SUBJECT:

BEAVER VALLEY POWER STATION - INTEGRATED INSPECTION REPORT 05000334/2017003 AND 05000412/2017003

Dear Mr. Bologna:

On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Beaver Valley Power Station, Units 1 and 2. On October 17, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented a violation of FirstEnergy Nuclear Operating Company (FENOCs)

site-specific licensing basis for tornado-generated missile protection. Because this violation was identified during the discretion period covered by Enforcement Guidance Memorandum 15-002 Revision 1, Enforcement Discretion for Tornado Missile Protection Non-compliance (ML16355A286)1 and because FENOC is implementing compensatory measures, the NRC is exercising enforcement discretion by not issuing an enforcement action and is allowing continued reactor operation.

If you contest the violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Beaver Valley Power Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document

Sincerely,

/RA/

Silas R. Kennedy, Branch Chief Division of Reactor Projects

1 Designation in parentheses refers to the Agencywide Documents Access and Management System (ADAMS) Accession Number.

Documents referenced in this letter are publicly-available using the Accession Number in ADAMS. Docket Nos.

50-334 and 50-412 License Nos. DPR-66 and NPF-73

Enclosure:

Inspection Report 05000334/2017003 and 05000412/2017003 w/Attachment: Supplementary Information

REGION I==

Docket Nos.:

50-334 and 50-412

License Nos.:

DPR-66 and NPF-73

Report No.:

05000334/2017003 and 05000412/2017003

Licensee:

FirstEnergy Nuclear Operating Company (FENOC)

Facility:

Beaver Valley Power Station (BVPS), Units 1 and 2

Location:

Shippingport, PA 15077

Dates:

July 1, 2017 through September 30, 2017

Inspectors:

J. Krafty, Senior Resident Inspector

S. Horvitz, Resident Inspector

`

T. Fish, Senior Operations Engineer

T. Hedigan, Operations Engineer

Approved By:

Silas R. Kennedy, Chief

Reactor Projects Branch 6

Division of Reactor Projects

SUMMARY

Inspection Report 05000334/2017003 and 05000412/2017003; 07/01/2017-09/30/2017; BVPS

Units 1 and 2; Integrated Inspection Report.

This report covered a three-month period of inspection by resident inspectors and announced baseline inspections performed by regional inspectors. The Nuclear Regulatory Commissions (NRCs) program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.

No findings were identified.

REPORT DETAILS

Summary of Plant Status

Unit 1 and Unit 2 operated at or near 100 percent power for the entire inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

==1R04 Equipment Alignment

==

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

  • Unit 2 service water (SW) system power supply during A SW pump maintenance on August 16, 2017

The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the Updated Final Safety Analysis Report (UFSAR), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted the systems performance of its intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether FENOC staff had properly identified equipment issues and entered them into the corrective action program (CAP) for resolution with the appropriate significance characterization. Documents reviewed for each section of this inspection report are listed in the Attachment.

b. Findings

No findings were identified.

.2 Full System Walkdown

a. Inspection Scope

On August 10, 2017, the inspectors performed a complete system walkdown of accessible portions of the Unit 1 river water (RW) system to verify the existing equipment lineup was correct. The inspectors reviewed drawings, equipment line-up check-off lists, and the UFSAR to verify the system was aligned to perform its required safety functions.

The inspectors also reviewed electrical power availability, component lubrication and equipment cooling, hanger and support functionality, and operability of support systems.

The inspectors performed field walkdowns of accessible portions of the systems to verify as-built system configuration matched plant documentation, and that system components and support equipment remained operable. The inspectors confirmed that systems and components were aligned correctly, free from interference from temporary services or isolation boundaries, environmentally qualified, and protected from external threats. The inspectors also examined the material condition of the components for degradation and observed operating parameters of equipment to verify that there were no deficiencies. For identified degradation the inspectors confirmed the degradation was appropriately managed by the applicable aging management program. Additionally, the inspectors reviewed a sample of related condition reports and work orders to ensure FENOC appropriately evaluated and resolved any deficiencies.

b. Findings

No findings were identified.

==1R05 Fire Protection

Resident Inspector Quarterly Walkdowns (71111.05Q - 4 samples)

==

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that FENOC controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment were available for use as specified in the area pre-fire plan and that passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

  • Unit 1 storeroom, Fire Area WH-1 and WH-2, on July 11, 2017
  • Unit 2 turbine building, Fire Area TB-1, on August 21, 2017
  • Unit 2 battery room 2-6, Fire Area TB-2, on August 24, 2017
  • Unit 1 transformers, Fire Area TR-1, 2, 3, 4, and 5, on August 29, 2017

b. Findings

No findings were identified.

1R06 Flood Protection Measures

Internal Flooding Review

a. Inspection Scope

The inspectors reviewed the internal flooding analysis and plant procedures to identify internal flooding susceptibilities for the site. The inspectors review focused on the Unit 1 safeguards area pipe tunnel. It assessed the adequacy of door seals, common drain lines and sumps, sump pumps, level alarms, and appropriate preventive maintenance activities. It assessed the adequacy of FENOCs procedures used to identify flooding in this area and also reviewed the CAP to determine if FENOC was identifying and correcting problems associated with both flood mitigation features and site procedures for responding to flooding.

b. Findings

No findings were identified.

==1R11 Licensed Operator Requalification Program and Licensed Operator Performance

==

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

(71111.11Q - 1 sample)

a. Inspection Scope

The inspectors observed Unit 2 licensed operator annual simulator examination on August 1, 2017, which included two scenarios:

(1) an anticipated transient without a scram with a main turbine trip failure, a faulted steam generator, and an AFW regulating valve failing open and
(2) a feedwater regulating valve failing closed requiring a manual reactor trip, a loss of the DF 4160 volts alternating current (VAC) safety bus, a failure of the 2-2 EDG to start, and a ruptured steam generator. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the technical specification (TS) action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

(71111.11Q - 1 sample)

a. Inspection Scope

The inspectors observed the Unit 2 control rod F10 digital rod position indication (DRPI)verification during the control rod partial movement test on August 25, 2017, and the Unit 1 EDG 1-1 surveillance test on September 6, 2017. The inspectors observed the briefings for the surveillance tests to determine if the review and coordination of the surveillances were given the appropriate level of attention for the limited use change to the procedure. The inspectors observed shift turnover briefings, pre-job briefings, and reactivity control briefings to verify that the briefings met the criteria specified in FENOCs Procedure NOP-OP-1002, Conduct of Operations, Revision 12. Additionally, the inspectors observed test performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.

b. Findings

No findings were identified.

.3 Annual Review of Requalification Examination Results

a. Inspection Scope

The inspectors conducted an in-office review of results of licensee-administered annual operating tests for 2017, Beaver Valley, Unit 1 operators. There were no Unit 1 written exams this year. The inspection assessed whether pass/fail rates were consistent with the guidance of NRC Inspection Manual Chapter (IMC) 0609, Appendix I, Licensed Operator Requalification Significance Determination Process (SDP).

The review verified that the individual failure rate did not exceed 20 percent.

  • 0 out of 29 operators failed at least one section of the annual exam. The overall individual failure rate was 0 percent.
  • 0 out of 8 crews failed the simulator test. The crew failure rate was 0 percent.

b. Findings

No findings were identified.

.4 Annual Review of Requalification Examination Results

a. Inspection Scope

The inspectors conducted an in-office review of results of licensee-administered comprehensive written exams for 2017, Beaver Valley, Unit 2 operators. The comprehensive written exams were administered in the first quarter of 2017. The inspection assessed whether pass/fail rates were consistent with the guidance of IMC 0609, Appendix I, Licensed Operator Requalification Significance Determination Process (SDP). The review verified that the individual failure rate did not exceed 20 percent.

  • 0 out of 35 operators failed the comprehensive written exam. The overall individual failure rate was 0 percent.

b. Findings

No findings were identified.

.5 Biennial Review During Requalification Examinations

a. Inspection Scope

The following inspection activities were performed using NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision 11, and Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program and Licensed Operator Performance.

Examination Results

The operating tests for the week of July 24, 2017, were reviewed for quality and performance.

On August 28, 2017, the results of the annual operating tests were reviewed to determine if pass/fail rates were consistent with the guidance of NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision 11, and IMC 0609, Appendix I, Licensed Operator Requalification Significance Determination Process (SDP). The review verified that the failure rate (individual or crew) did not exceed 20 percent.

  • 0 out of 35 operators failed at least one section of the annual exam. The overall individual failure rate was 0 percent.
  • 0 out of 9 crews failed the simulator test. The crew failure rate was 0 percent.

Written Examination Quality

The inspectors reviewed four written examinations previously administered during the February - March 2017 examination cycle for qualitative and quantitative attributes as specified in Appendix B of IP 71111.11, Licensed Operator Requalification Program and Licensed Operator Performance.

Operating Test Quality

Five job performance measures (JPMs) and two scenarios were reviewed for qualitative and quantitative attributes as specified in Appendix C of IP 71111.11, Licensed Operator Requalification Program and Licensed Operator Performance.

Licensee Administration of Operating Tests

Observations were made of the dynamic simulator exams and JPMs administered during the week of July 24, 2017. These observations included facility evaluations of crew and individual performance during the dynamic simulator exams and individual performance of JPMs.

Examination Security

The inspectors assessed whether facility staff properly safeguarded exam material.

JPMs, scenarios, and written examinations were checked for excessive overlap of test items.

Remedial Training and Re-Examinations

The remediation plans for one crew dynamic simulator failure (from the 2016 annual operating exam) was reviewed to assess the effectiveness of the remedial training.

Remediation for the individuals was processed in accordance with site procedures.

Conformance with Operator License Conditions

Medical records for three Senior Reactor Operator licenses and two Reactor Operator licenses were reviewed to assess conformance with license conditions. All records reviewed were satisfactory.

Proficiency watch standing records were reviewed for the first three quarters of 2017. All active licensed operators met the watch standing requirements to maintain an active license.

The reactivation plan for one licensed operator was reviewed to assess the effectiveness of the reactivation process. The reactivation was successfully processed in accordance with site procedures.

Records for the participation of licensed operators in the requalification program from January 2016 through July 2017 were reviewed. Records for the performance of licensed operators on annual requalification operating test and biennial requalification written exams were reviewed.

Simulator Performance

Simulator performance and fidelity was reviewed for conformance to the reference plant control room. A sample of simulator deficiency reports was also reviewed to ensure facility staff addressed identified modeling problems. Simulator test documentation was also reviewed.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system, or component (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, and maintenance rule basis documents to ensure that FENOC was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with Title 10 of the Code of Federal Regulations (CFR)50.65 and verified that the (a)(2) performance criteria established by FENOC staff was reasonable. As applicable, for SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2). Additionally, the inspectors ensured that FENOC staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.

  • Unit 2 480 VAC station service system on August 9, 2017
  • Control of quality parts during the mechanical seal replacement of the Unit 2 A charging pump on August 17, 2017 (quality control)

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that FENOC performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that FENOC personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When FENOC performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the stations probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

  • Unit 2 A SW strainer emergent work on August 1, 2017
  • Unit 2 yellow risk for system station service transformer (SSST) 2A out of service for schedule maintenance on an upstream line on August 14, 2017
  • Unit 1 yellow risk for racking B RW pump breaker onto DF 4160 VAC bus on August 23, 2017

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-conforming conditions based on the risk significance of the associated components and systems:

  • Unit 1 fire protection system functionality during a fire water header break on July 20, 2017
  • Impact on Unit 1 SSST 1A from nearby fire water header break on July 20, 2017
  • Unit 1 EDG 1-2 building exhaust damper missing louver on September 22, 2017

The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject SSC remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to FENOCs evaluations to determine whether the SSCs were operable. The inspectors confirmed, where appropriate, compliance with bounding limitations associated with the evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by FENOC.

b. Findings

10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that the applicable regulatory requirements and the design basis for SSCs are correctly translated into specifications, drawing, procedures, and instructions. Contrary to the above, FENOC failed to correctly translate the design basis for protection against tornado generated missiles into their specifications and procedures. Specifically, FENOC did not adequately protect Unit 1 EDGs exhausts from tornado generated missiles. FENOC documented the condition adverse to quality in their CAP under condition report 2017-07550 and took immediate compensatory actions. The inspectors evaluated FENOCs immediate compensatory measures, which included verifying that procedures are in place and training is current for performing actions in response to a tornado. Because this violation was identified during the discretion period covered by Enforcement Guidance Memorandum 15-002, Revision 1, Enforcement Discretion for Tornado Missile Protection Non-compliance (ML16355A286) and because FENOC has implemented compensatory measures, the NRC is exercising enforcement discretion and is not issuing enforcement action and is allowing continued reactor operation.

1R18 Plant Modifications

Permanent Modifications

a. Inspection Scope

The inspectors evaluated a modification to the Unit 1 SSST 1A implemented by engineering change package 17-0169, Replace the Damaged #10 AWG Wire with #6 AWG wire on Unit 1 SST TR-1A from the Control Panel A to AT-1 & AT-2. The modification was implemented to replace wire that had been previously damaged so that the degraded transformer could be restored to full capability. The inspectors verified that the design bases, licensing bases, and performance capability of the affected systems were not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design change. The inspectors also interviewed maintenance personnel and reviewed the post maintenance test to verify that the testing was appropriate for the maintenance performed.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with the information in the applicable licensing basis and/or design basis documents, and that the test results were properly reviewed and accepted and problems were appropriately documented. The inspectors also walked down the affected job site, observed the pre-job brief, confirmed work site cleanliness was maintained, witnessed the test or reviewed test data to verify quality control hold points were performed and checked, and verified that results adequately demonstrated restoration of the affected safety functions.

  • Unit 2 C charging pump motor oil change on July 12, 2017
  • Unit 1 B reactor coolant loop average temperature, summator and lead/lag card, T-RC-422, replacement on July 14, 2017
  • Calibration of the tap changer for the Unit 2 SSST 2B due to an out of tolerance surveillance on July 28, 2017
  • Control room air exhaust damper maintenance on August 3, 2017
  • Unit 2 A train SW strainer, 2SWS-STRM47, troubleshooting and repair on August 4, 2017
  • Unit 2 A charging pump mechanical seal replacement on August 18, 2017
  • Replacement of capacitors in Unit 2 uninterruptible power supply number 4, UPS-VITBS2-4, on August 29, 2017

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR, and FENOC procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied.

Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:

  • 1OST-15.3, C Reactor Plant Component Cooling Water Pump Test on July 18, 2017
  • 1OM-54.3.PAB1, Primary Auxiliary Building Log Readings on July 27, 2017
  • 1OM-54.3.L5, Surveillance Verification Log on July 27, 2017

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine FENOC emergency drill on July 20, 2017, to identify any weaknesses and deficiencies in the classification, notification, and protective action recommendation development activities.

The inspectors observed emergency response operations in the simulator, technical support center, and emergency offsite facility to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the station drill critique to compare inspector observations with those identified by FENOC staff in order to evaluate FENOCs critique and to verify whether the FENOC staff were properly identifying weaknesses and entering them into the CAP.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

Mitigating Systems Performance Index (6 samples)

a. Inspection Scope

The inspectors reviewed FENOCs submittal of the Mitigating Systems Performance Index for the following systems for the period of July 1, 2016, through June 30, 2017:

  • Unit 1 Heat Removal System (AFW)
  • Unit 2 Heat Removal System (AFW)
  • Unit 1 Cooling Water System (RW)
  • Unit 2 Cooling Water System (SW)

To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7. The inspectors also reviewed FENOCs operator narrative logs, maintenance rule records, condition reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by IP 71152, Problem Identification and Resolution, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify FENOC entered issues into the CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends.

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP and periodically attended condition report screening meetings.

b. Findings

No findings were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a semi-annual review of site issues to identify trends that might indicate the existence of more significant safety concerns. The inspectors reviewed FENOCs CAP database for the first and second quarters of 2017 to assess condition reports written in various subject areas (equipment problems, human performance issues, etc.), as well as individual issues identified during the inspectors daily condition report review (Section 4OA2.1) and condition reports related to components found out of tolerance for January 1, 2014 through June 30, 2017. The inspectors also reviewed the FENOC Fleet Oversight Performance Gap Reports for February 2017 through June 2017, conducted under NOBP-LP-2023, Performance Assessment, to verify that FENOC personnel were appropriately evaluating and trending adverse conditions in accordance with applicable procedures.

b. Findings and Observations

No findings were identified.

The inspectors did not identify any adverse trends that had not been previously identified by FENOC in their review of condition reports generated over the past two quarters.

However, the inspectors noted that there were more than 100 condition reports documenting instances of equipment found out of tolerance over the past six months, so an in depth review was conducted for the past three years. Further review identified that there have been more than 50 conditions reports documenting equipment found out of tolerance each quarter since 2014 and two issues were identified. In 2012, CR-2012-03539 documented that the pressure switch for the EDG 2-1 crankcase high alarm was found out of tolerance and exceeded its measured maintenance data (MMD)drift limit. This was evaluated by engineering and had a corrective action to remove this pressure switch from the MMD program. This corrective action was not implemented as required by NOP-LP-2001, Corrective Action Program. Additionally, in 2016, CR-2016-02864 documented that the pressure switch for the EDG 2-1 crankcase high alarm was again found out of tolerance and exceeded its MMD drift limit. An engineering evaluation was requested, but no evaluation was performed as required by NOBP-ER-3914, Measured Maintenance Data (MMD) Program Requirements. The inspectors determined that FENOC failed to perform the corrective actions to remove the pressure switch from the MMD program and perform an engineering evaluation for the out of tolerance pressure switch. In accordance with IMC 0612, Power Reactor Inspection Reports, the inspectors determined that these performance deficiencies were minor because they had no safety impact. Specifically, the crankcase pressure switchs function is limited to alarm only indication with no link to the safety analysis, design basis, or licensing basis requirements and the drift value was based on conservative engineering judgment as opposed to instrument uncertainty. FENOC documented this issue in CR-2017-09947.

4OA6 Meetings, Including Exit

On October 17, 2017, the inspectors presented the inspection results to Mr. Richard Bologna, Site Vice President, and other members of the BVPS staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

R. Bologna, Site Vice President
J. Grabnar, General Plant Manager
S. Baldwin, Supervisor, Mechanical Maintenance
C. Battistone, Fleet Oversight Supervisor
M. Belculfine, Supervisor, Mechanical Maintenance
T. Boyda, Maintenance Technician
A. Crotty, Manager, Plant Engineering
F. Etzel, Analytical Methods Engineer
R. Ferrie, Supervisor, Electrical Maintenance
T. Gaydosik, Fleet Exam Development Lead
J. Iliff, Supervisor, Licensed Operator Continuing Training
M. Jansto, System Engineer
M. Kienzle, System Engineer
R. Klindworth, Unit Supervisor
R. Kuhn, Mechanical Maintenance Consulting Engineer
M. Mayer, Staff Nuclear Engineering Specialist
S. Mercer, System Engineer
J. Miller, Fire Marshal
T. OLeary, Shift Manager
P. Pauvlinch, Design Engineering Manager
D. Ronnenberg, Operations Training Superintendent
H. Scott, Supervisor, FIN Maintenance
J. Snyder, System Engineer
E. Thomas, Supervisor, Nuclear Compliance
D. Tiberio, Simulator Support Supervisor
M. Unfried, Engineering Analysis Engineer
M. Wimmel, MOV Program Engineer
T. Winfield, Relay Supervisor

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

None.

LIST OF DOCUMENTS REVIEWED