IR 05000331/2007005

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IR 05000331-07-005, on 10/01/2007 - 12/31/2007; Duane Arnold Energy Center; Access Control to Radiologically Significant Areas and Follow-Up of Events
ML080390306
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 02/08/2008
From: Kenneth Riemer
NRC/RGN-III/DRP/B2
To: Richard Anderson
Duane Arnold
References
IR-07-005
Download: ML080390306 (53)


Text

February 8, 2008

SUBJECT:

DUANE ARNOLD ENERGY CENTER NRC INTEGRATED INSPECTION REPORT 05000331/2007005

Dear Mr. Anderson:

On December 31, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Duane Arnold Energy Center. The enclosed integrated inspection report documents the inspection findings which were discussed on January 17, 2008, with D. Curtland and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, there was one NRC-identified and one self-revealed finding of very low safety significance, both of which involved violations of NRC requirements.

However, because these violations were of very low safety significance and because the issues were entered into your CAP, the NRC is treating these findings and issues as Non-Cited Violations in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Duane Arnold Energy Center. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Docket No. 50-331;72-032 License No. DPR-49

Enclosure:

Inspection Report 05000331/2007005 (w/Attachment: Supplemental Information)

cc w/encl:

M. Nazar, Senior Vice President and Chief Operating Officer J. Stall, Senior Vice President, Nuclear and Chief Nuclear Officer R. Helfrich, Senior Attorney M. Ross, Managing Attorney R. Kundalkar, Vice President, Nuclear Engineering J. Bjorseth, Site Director D. Curtland, Plant Manager S. Catron, Manager, Regulatory Affairs Chief Radiological Emergency Preparedness Section, Dept. Of Homeland Security M. Rasmusson, State Liaison Officer

SUMMARY OF FINDINGS

IR 05000331/2007005; 10/01/2007 - 12/31/2007; Duane Arnold Energy Center. Access Control to Radiologically Significant Areas and Follow-up of Events.

This report covers a three-month period of baseline resident inspection and announced baseline inspections of emergency preparedness, licensed operator requalification program, and radiation protection. The inspections were conducted by Region III reactor inspectors, an emergency preparedness analyst, a health physicist, operations engineers, and the resident inspectors. Two Green findings were identified by the inspectors. The findings were considered Non-Cited Violations of NRC regulations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified and Self-Revealing Findings

Cornerstone: Occupational Radiation Safety

Green.

A self-revealed finding of very low safety significance and an associated Non-Cited Violation (NCV) of Title 10 CFR 20.1501 were identified for failure to adequately survey and evaluate the magnitude and extent of radiation levels to ensure that high radiation areas were adequately posted and controlled. On February 7, 2007, a worker entered into an inadequately posted and controlled area in the Reactor Building 734' West Torus Room, which had radiation levels warranting posting and controls for a high radiation area. Corrective actions taken by the licensee included a change in the procedure to survey the Torus Room in the area of shut-down cooling, specifically after low pressure core injection (LPCI) full flow testing that could result in unexpected high radiation areas. A cross-cutting aspect in human performance was associated with this finding in the area of decision-making. (H.1.a)

The issue was more than minor because it was associated with the Program/Process attribute of the Occupational Radiation Safety Cornerstone and affected the cornerstone objective to ensure adequate protection of worker health and safety from exposure to radiation. The issue represents a finding of very low safety significance because it did not involve As-Low-As-Is-Reasonably-Achievable (ALARA) planning or work controls, there was no overexposure, nor did a substantial potential for an overexposure exist given the radiological conditions in the area and the workers response to the electronic dosimeter alarm. Also, the licensee=s ability to assess worker dose was not compromised. (Section 2OS1.2)

Cornerstone: Mitigating Systems

Green.

A finding of very low safety significance and an associated Severity Level IV NCV of 10 CFR 50.72(b)(3)(v) were identified by the inspectors for the failure of the licensee to make an eight-hour notification to the NRC for the loss of both emergency diesel generators (EDGs). The licensee entered this into their corrective action program (CAP) as CAP 053463 and updated the event notification (EN 43692) to include the loss of safety function resulting from both EDGs being inoperable from 0408 to 0715 on October 5, 2007.

The inspectors determined that the failure to report the loss of safety function of the onsite emergency AC power system in accordance with 10 CFR 50.72(b)(3)(v) was a performance deficiency. The NRC considers the safety implications of non-compliances that may impact the ability to carry out its statutory mission. Non-compliances may be significant because they may challenge the regulatory envelope upon which certain activities were licensed. This issue is greater than minor, because the failure to report the loss of the EDGs affected the NRCs ability to perform a regulatory function.

Because violations of 10 CFR 50.72 are considered to be violations that potentially impede or impact the regulatory process, they are dispositioned using the traditional enforcement process instead of the SDP. However, if possible, the underlying technical issue is evaluated under the SDP to determine the severity of the violation. Using IMC 0609, Significance Determination Process, the inspectors screened this issue as having very low safety significance using the phase 1 screening questions under the Mitigation System Cornerstone. (Section 4OA3.1)

Licensee-Identified Violations

No violations of significance were identified.

REPORT DETAILS

Summary of Plant Status

Duane Arnold Energy Center (DAEC) operated at full power for the entire assessment period except for brief down-power maneuvers to accomplish rod pattern adjustments and to conduct planned surveillance testing activities with the following exception:

  • On October 31, 2007, reactor power was lowered to approximately 55 percent to repair a steam leak, immediately downstream of the B feedwater pump, located on the high point vent from the B feedwater line. The affected piping was replaced and the plant was returned to full power on November 2,

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Winter Seasonal Readiness Preparations

a. Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to verify that the plants design features and implementation of procedures were sufficient to protect mitigating systems from the effects of adverse weather. Documentation for selected risk-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather. During the inspection, the inspectors focused on plant specific design features and the licensees procedures used to mitigate or respond to adverse weather conditions.

Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR)and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant specific procedures. Cold weather protection, such as heat tracing and area heaters, was verified to be in operation where applicable. The inspectors also reviewed CAP items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures.

Specific documents reviewed during this inspection are listed in the Attachment. The inspectors reviews focused specifically on the following plant systems due to their risk significance or susceptibility to cold weather issues:

  • Instrument Air Compressor System.

This inspection constitutes one winter seasonal readiness preparations sample as defined in Inspection Procedure 71111.01-05.

b. Findings

No findings of significance were identified.

.2 Readiness For Impending Adverse Weather Condition - Freezing Rain Conditions

a. Inspection Scope

Since freezing rain conditions were forecast in the vicinity of the facility for the week of December 9, 2007, the inspectors reviewed the licensees overall preparations/protection for the expected weather conditions and also observed the sites response after the freezing rain had passed. The inspectors observed insulation, heat trace circuits, space heater operation, and weatherized enclosures to ensure operability of affected systems. The inspectors reviewed licensee procedures and discussed potential compensatory measures with control room personnel. On December 13, 2007, the inspectors walked down the 161kv/4160kv startup transformer system because its safety-related functions could be affected as a result of the freezing rain conditions present at the facility. The inspectors focused on plant managements actions for implementing the stations procedures for ensuring adequate personnel for safe plant operation and emergency response would be available. This included plant response to ice falling on the startup transformer with the standby transformer out-of-service.

Specific documents reviewed during this inspection are listed in the Attachment.

This inspection constitutes one readiness for impending adverse weather condition sample as defined in Inspection Procedure 71111.01-05.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of accessible portions of trains of risk-significant Mitigating Systems equipment. The documents listed in the Attachment were used by the inspectors to accomplish the objectives of the inspection procedure.

Equipment alignment was reviewed to identify any discrepancies that could impact the function of the system and potentially increase risk. Redundant or backup systems were selected by the inspectors during times when the trains were of increased importance due to the redundant trains of other related equipment being unavailable. Inspection activities included, but were not limited to, a review of the licensees procedures, verification of equipment alignment, and an observation of material condition, including operating parameters of in-service equipment. Identified equipment alignment problems were verified by the inspectors to be properly resolved.

The inspectors selected the following equipment trains to verify operability and proper equipment line-up:

  • B Standby Diesel Generator (SBDG) with A SBDG out-of-service (OOS) for maintenance;
  • Division 2, 125 VDC Power Distribution System with the Division 1, 125 VDC Power Distribution System OOS for maintenance.

These activities constituted three partial system walkdown samples as defined in Inspection Procedure 71111.04-05

b. Findings

No findings of significance were identified.

.2 Semi-Annual Complete System Walkdown

a. Inspection Scope

The inspectors performed a complete system alignment inspection of the RCIC system.

This system was selected because it was considered both safety significant and risk significant in the licensees probabilistic risk assessment. The inspection consisted of a review of plant procedures (including selected abnormal and emergency procedures),drawings, and the UFSAR to identify proper system alignment. The inspectors also reviewed selected issues identified in CAP documents, to determine if they had been properly addressed in the licensees corrective actions program. As part of this inspection, the documents in the Attachment were utilized to evaluate the potential for an inspection finding.

These activities constituted one complete system walkdown sample as defined in Inspection Procedure 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Routine Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk significant plant areas:

  • AFP 10, Main Exhaust Fan Room, Heating Hot Water Pump Room and the Plant Air Supply Fan Room;
  • AFP 11, Reactor Building Laydown Area, Elevation 833-6;
  • AFP 12, Reactor Building Decay Tank and Condensate Phase Separator Rooms;
  • AFP 23, Control Building 1D-2, 1D-4, 1D-1 Battery Rooms and Battery Corridor;
  • AFP 24, Control Building 1-A3, 1-A4 Essential Switchgear Rooms;
  • AFP 29, Pump House Fire Pump and Fire Pump Day Tank Rooms; and
  • AFP 30, Pump House Safety-related Piping Area The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP.

These activities constituted ten quarterly fire protection inspection samples as defined in Inspection Procedure 71111.05AQ-05.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

.1 Heat Sink Performance

a. Inspection Scope

The inspectors performed a review of the licensees bio-fouling and cleanliness inspection of the A reactor building closed cooling water heat exchanger. The inspectors utilized the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspection focused on potential deficiencies that could mask the licensees ability to detect degraded performance, identification of any common cause issues that had the potential to increase risk, and ensuring that the licensee was adequately addressing problems that could result in initiating events that would cause an increase in risk. The inspection activities included, but were not limited to, a review of the licensees observations as compared against acceptance criteria, the correlation of scheduled testing and the frequency of testing, and the impact of instrument inaccuracies on test results. Inspectors also verified that test acceptance criteria considered differences between test conditions, design conditions, and testing criteria.

This inspection constitutes one sample as defined in Inspection Procedure 71111.07-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On October 17, 2007, the inspectors observed a crew of licensed operators in the plants simulator during a licensee evaluated emergency preparedness training drill to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate Technical Specification (TS) actions and Emergency Plan actions and notifications.

The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements.

Additionally, the inspectors observed portions of the licensees instructor training sessions associated with reactor vessel breach and core melt, abnormal event analysis, and mitigating core damage strategies.

These inspection activities constituted one quarterly licensed operator requalification program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings of significance were identified.

.2 Annual Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of Job Performance Measure operating tests, and simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee from October 23 through December 5, 2007. The overall results were compared with the significance determination process in accordance with NRC IMC 0609, Appendix I, Operator Requalification Human Performance SDP. This review represented one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk significant systems:

  • Site Communications; and

The inspectors reviewed plant systems to assess the maintenance effectiveness.

Documents reviewed are listed in the Attachment. The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Inspection activities included, but were not limited to, the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1).

These activities constituted two quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • Work Week 9740;
  • Work Week 9750; and

These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstone. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst, shift technical advisor, or a senior licensed operator, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

These activities constituted three samples as defined in Inspection Procedure 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • Operability Recommendation (OPR) 000367, Damage to 1B42 Bus Bars;
  • OPR 000370, Design Calculations for 161KVA Sources;
  • OPR 000371, Evaluation of Switchyard During Severe Weather; and

The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to the licensees evaluations, to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the

.

These activities constituted four samples as defined in Inspection Procedure 71111.15-05.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

.1 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance testing activities for review to verify that procedures and test activities were adequate to ensure system operability and functional capability:

  • Preventative Work Order (PWO) 1139257, 'A' SBDG 2-Year Maintenance Inspections;
  • Maintenance Work Order (MWO) 1136907, RCIC System Flow Controller Replacement;
  • Corrective Work Order (CWO) A73482 and A73484, Replacement of the A and C RHRSW Motor Cooling Coil; and

These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment.

These activities constituted four samples as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

.1 Routine Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • Surveillance Test Procedure (STP) 3.8.1-03, Standby Diesel Generators Operability Test for the 'B' SBDG;
  • STP 3.3.6.3-03, Low-Low Set Pressure Setpoint Channels Functional Test.

The inspectors observed in-plant activities and reviewed procedures and associated records to determine whether: preconditioning occurred; effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints were within required ranges; the calibration frequency was in accordance with TSs, the UFSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the performance of its safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the CAP. Documents reviewed are listed in the Attachment.

These activities constituted three routine surveillance testing samples as defined in Inspection Procedure 71111.22-05.

b. Findings

No findings of significance were identified.

.2 In-service Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

The inspectors observed in plant activities and reviewed procedures and associated records to determine whether: preconditioning occurred; effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints were within required ranges; the calibration frequency was in accordance with TSs, the UFSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable for in-service testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers Code, and reference values were consistent with the system design basis; where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the performance of its safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the CAP. Documents reviewed are listed in the Attachment.

This inspection constitutes one in-service inspection sample as defined in Inspection Procedure 71111.22-05.

b. Findings

No findings of significance were identified.

.3 Reactor Coolant System Leak Detection Inspection

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • STP 3.4.5-04, Functional Test of Equipment and Floor Drain Sump Flow Timers.

The inspectors observed in plant activities and reviewed procedures and associated records to determine whether: preconditioning occurred; effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints were within required ranges; the calibration frequency was in accordance with TSs, the UFSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the performance of its safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the CAP. Documents reviewed are listed in the Attachment.

This inspection constitutes one reactor coolant system leak detection inspection sample as defined in Inspection Procedure 71111.22-05.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

.1 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the following temporary modification:

  • TM 07-021, GEZIP Feedwater Inboard Isolation Valve (V-07-0247) Furmanite Encapsulation.

The inspectors compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis, the UFSAR, and the TSs, as applicable, to verify that the modification did not affect the operability or availability of the affected system. The inspectors also compared the licensees information to operating experience information to ensure that lessons learned from other utilities had been incorporated into the licensees decision to implement the temporary modification. The inspectors, as applicable, performed field verifications to ensure that the modification was installed as directed; the modification operated as expected; modification testing adequately demonstrated continued system operability, availability, and reliability; and that operation of the modification did not impact the operability of any interfacing systems. Lastly, the inspectors discussed the temporary modification with operations, engineering, and training personnel to ensure that the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance.

This inspection constitutes one sample as defined in Inspection Procedure 71111.23-05.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The inspectors performed a screening review of Sections B and H, Revisions 28 and 25 respectively, and Appendix 6, Revision 25 of the Duane Arnold Energy Center Emergency Plan to determine whether changes identified in the above revisions decreased the effectiveness of the licensees emergency planning for the Duane Arnold Energy Center. This review did not constitute an approval of the changes, and as such, the changes are subject to future NRC inspection to ensure that the emergency plan continues to meet NRC regulations.

These activities completed one inspection sample as defined in Inspection Procedure 71114.04-05.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors reviewed licensee controls and surveys performed during the refueling outage in the following five radiologically significant work areas within radiation areas, high radiation areas, and airborne radioactivity areas in the plant and reviewed work packages, which included associated licensee controls and surveys of these areas to determine if radiological controls including surveys, postings, and barricades were acceptable:

  • Refuel Floor In-Service Inspections activities;
  • Drywell Nozzle In-Service Inspection;
  • Diving Refuel Floor/Reactor Vessel Sparger Repair;
  • Installation and removal of temporary shielding that included N2 window shielding; and
  • Control Rod Drive (CRD) support work including under vessel activities.

The inspectors reviewed the radiation work permits (RWPs) and work packages used to access these five areas and other high radiation work areas to identify the work control instructions and control barriers that had been specified. Electronic dosimeter alarm set points for both integrated dose and dose rate were evaluated for conformity with survey indications and plant policy. The licensee=s staffs were interviewed to verify that they were aware of the actions required when their electronic dosimeters noticeably malfunctioned or alarmed.

The adequacy of the licensee=s internal dose assessment process for analyzing internal exposures that exceed 50 millirem committed effective dose equivalent was assessed to determine if affected personnel would be properly monitored utilizing calibrated equipment, that the data would be analyzed, and that internal exposures would be properly assessed in accordance with licensee procedures.

The inspectors reviewed the licensee=s physical and programmatic controls for highly activated and/or contaminated materials (non-fuel) stored within the spent fuel pool.

These reviews represented two samples as defined in Inspection Procedure 71121.01-05.

b. Findings

No findings of significance were identified.

.2 High Risk Significant, High Dose Rate High Radiation Area and Very High Radiation

Area Controls

a. Inspection Scope

The inspectors held discussions with the Radiation Protection Manager concerning high dose rate/high radiation area and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection, in order to verify that any procedure modifications did not substantially reduce the effectiveness and level of worker protection.

This inspection constitutes one sample as defined by Inspection Procedure 71121.01-05.

The inspectors discussed with Radiation Protection (RP) supervisors the controls that were in place for special areas that had the potential to become very high radiation areas during certain plant operations, to determine if these plant operations required communication beforehand with the RP group, so as to allow corresponding timely actions to properly post and control the radiation hazards.

The inspectors reviewed the licensee=s procedures and discussed with RP staff its practices for access into locked high and very high radiation areas and for areas with the potential for changing radiological conditions such as the drywell and Torus area. In particular, the inspectors reviewed a high radiation area incident that occurred on February 7, 2007. This included review of the circumstances and consequences associated with a worker staging scaffolding in the Torus catwalk area who received a dose rate alarm. These reviews were conducted to determine the adequacy of the radiological controls and the radiological hazards assessment associated with such entries. Work instructions provided in RWPs and in pre-entry briefing documents were discussed with RP staff to determine their adequacy relative to industry practices and NRC Information Notices.

The inspectors also reviewed the licensee=s procedure and generic practices associated with dosimetry placement and the use of multiple whole body dosimetry for work in high radiation areas having significant dose gradients for compliance with the requirements of 10 CFR 20.1201(c) and applicable industry guidelines. Additionally, previously completed work in areas where dose rate gradients were subject to significant variation such as work under-vessel were reviewed to evaluate the licensee=s practices for dosimetry placement.

The inspectors conducted plant walkdowns to verify the posting and locking of entrances to high dose rate high radiation areas and very high radiation areas.

These reviews represented three samples as defined in Inspection Procedure 71121.01-05.

b. Findings

Introduction:

A self-revealed Green finding of very low safety significance and an associated NCV of NRC requirements (10 CFR 20.1501) were identified for the failure to adequately survey and evaluate the magnitude and extent of radiation levels, which resulted in an unposted high radiation area.

Description:

On February 7, 2007, a foreman/worker reported to access control when he received an electronic dosimeter (ED) high dose rate alarm of 81 millirem/hour. The worker was walking on the catwalk of 734' Torus Room at the time of the alarm. The RP staff reviewed the ED records for the worker=s RWP entry and found that the worker=s ED alarmed at 81 millirem/hour. The staff recognized that the recorded radiation level was abnormally high for the Torus catwalk area, which was posted as a radiation area.

The RP staff dispatched a technician to survey the Torus Room where the worker had been on the Torus catwalk. The dose rate surveys indicated that several areas of the Torus Room had elevated dose rates that had apparently resulted from the shut-down cooling system=s low pressure core injection full flow tests that had been performed about two days earlier. The licensee attributed the elevated radiation levels to crud bursts within the system and to the shut-down cooling system not running for a sufficient time to ensure that suspended radioactive materials were cleaned up or removed from the system. The resulting suspension of radioactive material in the coolant increased the radiation dose rate to a maximum 160 millirem/hour at 30 centimeters at the RHR piping at the 734' West Torus Room, which caused the worker=s ED dose rate alarm at 81 millirem/hour. This area of the Torus catwalk location at the Torus Room 734' West was an inadequately posted and controlled area, because the licensee failed to recognize the changing condition and the increasing dose rate trends in the RHR piping during the LPCI full flow tests. Specifically, the licensee performed dose rate surveys during and after the LPCI full flow tests. Surveys indicated that there was an increasing dose rate trend at the RHR piping after the LPCI full flow test; however, the licensee failed to perform additional dose rate surveys in order to fully evaluate the changing condition, which resulted in a high radiation area.

Analysis:

The failure to perform adequate radiological surveys required by 10 CFR 20.1501 to ensure that high radiation areas are properly posted and controlled represents a performance deficiency as defined in NRC IMC 0612, Power Reactor Inspection Reports,@ Appendix B, Issue Screening.@ The inspectors determined that the issue was associated with the Program/Process attribute of the Occupational Radiation Safety Cornerstone and affected the cornerstone objective to ensure adequate protection of worker health and safety from exposure to radiation. Therefore, the issue was more than minor and represented a finding which was evaluated using the SDP.

Since the finding involved a high radiation area radiological control issue, the inspectors utilized IMC 0609, Appendix C, AOccupational Radiation Safety SDP,@ to assess its significance. Based on the radiological conditions in the area coupled with the worker response to the ED alarm, the inspectors determined that no overexposure occurred nor did a substantial potential for an overexposure exist. The licensee=s ability to assess dose was also not compromised for this incident. Consequently, the inspectors concluded that the SDP assessment for this finding was of very low safety significance (Green).

The inspectors identified a cross-cutting aspect in human performance associated with this finding in the area of decision-making, specifically with risk significant decisions using a systematic process. When the licensee was faced with uncertain or unexpected plant conditions, the licensee did not ensure safety was maintained in the work practices component. Specifically, the licensee did not have a systematic process to evaluate the increasing radiation levels caused by shut-down cooling operations such as LPCI flow tests and to perform additional radiation measurements, which resulted in an unposted high radiation area (H.1.a).

Enforcement:

Title 10 CFR 20.1501 requires that each licensee performed radiation surveys that may be necessary for the licensee to comply with the regulations in 10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent of radiation levels, and the potential radiological hazards that could be present. Contrary to the above, as of February 7, 2007, the licensee did not perform dose rate surveys to assure compliance with 10 CFR 20.1902, which limits radiation levels to be less than 100 millirem/hour for radiation area posting requirements. A radiation survey performed in the Torus Room by the RP staff after the event indicated that the dose rates at the RHR piping were nominally at 160 millirem/hour at 30 centimeters.

Corrective actions taken by the licensee included reminding the staff during outage briefings to be aware of changing conditions in regard to operating systems that may change radiation levels in the Torus work areas. Since the licensee documented this issue in its CAP (CAPs 047115, 045132, 047794, and 045375) and completed an Apparent Cause Evaluation (ACE 004858) by February 15, 2007, and because the violation is of very low safety significance, it is being treated as an NCV (NCV 05000331/2007005-01).

2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (71121.02)

.1 Radiological Work Planning.

a. Inspection Scope

The inspectors compared the results achieved including dose rate reductions and person-rem used with the intended dose established in the licensee=s ALARA planning for these five work activities. Reasons for inconsistencies between intended and actual work activity doses were reviewed for:

$

Refuel Floor In-Service Inspections activities;

$

Drywell Nozzle In-Service Inspection;

$

Diving Refuel Floor/Reactor Vessel Sparger Repair;

$

Installation and removal of temporary shielding that included N2 window shielding; and

$

CRD support work including under vessel activities.

These reviews represented one inspection sample as defined in Inspection Procedure 71121.02-05.

b. Findings

No findings of significance were identified.

.2 Declared Pregnant Workers

a. Inspection Scope

The inspectors reviewed dose records of declared pregnant workers for the current assessment period to verify that the exposure results and monitoring controls employed by the licensee complied with the requirements of 10 CFR 20.

This inspection constitutes one sample as defined in Inspection Procedure 71121.02-05.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the fourth Quarter 2007 performance indicators (PIs) for any obvious inconsistencies prior to its public release in accordance with IMC 0608, Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.

b. Findings

No findings of significance were identified.

.2 Safety System Functional Failures

a. Inspection Scope

The inspectors sampled licensee submittals for the Safety System Functional Failures PI for the period from the fourth quarter 2006 through the third quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in revision 5 of the Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73" definitions and guidance were used.

The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, CAP documents, event reports and NRC Integrated Inspection reports for the period from the fourth quarter 2006 through the third quarter 2007 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment to this report.

This inspection constitutes one safety system functional failures sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.3 Mitigating Systems Performance Index - Emergency AC Power System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - Emergency AC Power System PI for the period from the third quarter 2006 through the third quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in revision 5 of the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, were used.

The inspectors reviewed the licensees operator narrative logs, MSPI derivation reports, Corrective Action Process Documents, event reports and NRC Integrated Inspection reports for the period from the third quarter 2006 through the third quarter 2007 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment to this report.

This inspection constitutes one MSPI emergency AC power system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.4 Mitigating Systems Performance Index - High Pressure Injection Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - High Pressure Injection Systems PI for the period from the third quarter 2006 through the third quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in revision 5 of the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, were used. The inspectors reviewed the licensees operator narrative logs, Corrective Action Process Documents, MSPI derivation reports, event reports and NRC Integrated Inspection reports for the period from the third quarter 2006 through the third quarter 2007 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the Attachment to this report.

This inspection constitutes one MSPI high pressure infection system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.5 Mitigating Systems Performance Index - Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for the period from the third quarter 2006 through the third quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in revision 5 of the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, were used. The inspectors reviewed the licensees operator narrative logs, Corrective Action Process Documents, event reports, MSPI derivation reports, and NRC Integrated Inspection reports for the period from the third quarter 2006 through the third quarter to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the Attachment to this report.

This inspection constitutes one MSPI heat removal system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.6 Mitigating Systems Performance Index - Residual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal System PI for the period from the third quarter 2006 through the third quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in revision 5 of the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, were used. The inspectors reviewed the licensees operator narrative logs, Corrective Action Process Documents, MSPI derivation reports, event reports and NRC Integrated Inspection reports for the period from the third quarter 2006 through the third quarter 2007 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the Attachment to this report.

This inspection constitutes one MSPI residual heat removal system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.7 Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems PI for the period from the third quarter 2006 through the third quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in revision 5 of the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, were used. The inspectors reviewed the licensees operator narrative logs, CAP documents, MSPI derivation reports, event reports and NRC Integrated Inspection reports for the period the third quarter 2006 through the third quarter 2007 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment to this report.

This inspection constitutes one MSPI cooling water system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of items Entered Into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations are included in the attached List of Documents Reviewed.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.2 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six month period of July 2007 through December 2007, although some examples expanded beyond those dates where the scope of the trend warranted.

The reviews also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

This review constituted a single semi-annual trend inspection sample as defined in Inspection Procedure 71152-05.

b.

Assessments and Observations As part of this semi-annual trend review, the inspectors performed a focused review of the licensees documentation of an emerging adverse trend affecting on-line work scheduling and risk management processes. On more than three occasions during the fourth calendar quarter of 2007, the licensees weekly on-line risk analysis was revised to reflect an increased change in Probabilistic Risk Assessment (PRA) risk color. Only revisions which were required due to foreseeable risk significant evolutions not being properly characterized or scheduled were reviewed. Specific examples include:

  • Characterized the risk associated with both SBDGs being unavailable during planned maintenance on the A SBDG and performance of the required surveillance testing of the B SBDG as Yellow verses Red;
  • Improperly scheduled duration of the Startup Transformer unavailability during the transformer pit restoration project resulted in risk remaining Yellow three additional days and delayed scheduled DC power battery inspections to prevent entering an Orange risk condition; and
  • Performed an emergent work clearance activity on equipment powered from the B 480 VAC essential bus (1B42) while the A SBDG was unavailable for planned maintenance which, due to known equipment concerns, caused a loss of 1B42 and resulted in an elevated risk condition requiring increased compensatory actions and equipment protective measures.

The licensee entered these issues into their CAP for further evaluation as CAP 053617.

Based upon benchmarking of the FPL fleet and industry peers, the licensee determined that DAECs protected equipment program had not been maintained at a level comparable to industry best practices, which protect the opposite train down to the 480 VAC/ 120 VAC control power systems. New expectations for the protected systems program were established, communicated to all site personnel, and implemented by the recent revision to DAEC Work Planning Guideline-2, On-Line Risk Management Guideline, Attachment 8.

The inspectors reviewed both the licensees immediate corrective actions taken to address identified areas for improvements, and the completed condition evaluation. The inspectors will continue to monitor the licensees performance and progress in the area of on-line work scheduling and risk management.

No findings or significant issues were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion

.1 Loss of 480 Volt AC Essential Bus 1B42

a. Inspection Scope

The inspectors reviewed the plants response to a loss of the 480 Volt AC essential bus 1B42. Documents reviewed in this inspection are listed in the Attachment.

On October 5, 2007, a loss of the 480 Volt AC essential bus 1B42 occurred during a clearance application on breaker 1B4234A. The loss of bus 1B42 resulted in the loss of the B essential service water (ESW) pump, thus resulting in the loss of cooling to the B EDG. At the time of the event, the A EDG was OOS and inoperable for planned maintenance. The A ESW pump was inoperable but available following pre-planned maintenance.

This inspection constitutes one sample as defined in Inspection Procedure 71153-05.

b. Findings

Introduction:

A finding of very low safety significance (Green) and an associated Severity Level IV NCV of 10 CFR 50.72(b)(3)(v) were identified by the inspectors for the failure of the licensee to make an eight hour notification to the NRC for the loss of both EDGs. The licensee entered this into their CAP for resolution.

Description:

At 0408 on October 5, 2007, while applying a clearance (tagout) to breaker 1B4234A, a fault occurred on the Motor Control Center (MCC) dual breaker cubicle 1B4234A/B, resulting in the loss of the 480 Volt AC essential bus 1B42. The loss of bus 1B42 resulted in the loss of the B ESW pump, thus resulting in the loss of cooling to the B EDG. At the time of the event, the A EDG was OOS and inoperable for planned maintenance. The A ESW pump was inoperable but available following pre-planned maintenance. With both the A and B EDGs inoperable, there was a loss of the onsite emergency power safety function. At 0715, power was restored to bus 1B42, and the B ESW pump and B EDG were declared operable. At 1030, DAEC made an event notification (EN 43692) per 10 CFR 50.72(b)(3)(v) to the NRC reporting that a loss of safety function occurred due to a loss of both ESW pumps. There was no report made relative to the loss of safety function associated with both EDGs.

On October 26, 2007, the NRC inspectors questioned the licensee why there was not a concurrent event notification made for a loss of both EDGs. The licensee initiated CAP 053463, NCAQ - Loss of 1B42 and reportability. At 1224, DAEC made an update to EN 43692 to include the loss of safety function resulting from both EDGs being inoperable from 0408 to 0715 on October 5, 2007.

After further review by the licensee, it was determined that while the A ESW pump was inoperable by TS requirements, it was available and could have performed its safety function. On December 4, 2007, EN 43692 was further updated to reflect that there was no loss of safety function for the ESW pumps.

Analysis:

The inspectors determined that the failure to report the loss of safety function of the onsite emergency AC power system in accordance with 10 CFR 50.72(b)(3)(v)was a performance deficiency. The NRC considers the safety implications of non-compliances that may impact the ability to carry out its statutory mission.

Non-compliances may be significant because they may challenge the regulatory envelope upon which certain activities were licensed. This issue is greater than minor, because the failure to report the loss of the EDGs affected the NRCs ability to perform a regulatory function. Because violations of 10 CFR 50.72 are considered to be violations that potentially impede or impact the regulatory process, they are dispositioned using the traditional enforcement process instead of the SDP. However, if possible, the underlying technical issue is evaluated under the SDP to determine the severity of the violation. In this case, only the loss of bus 1B42 (which resulted in the loss of the B EDG) is evaluated. As stated in IMC 0609, Significance Determination Process, Appendix A, 1, Step 1.1, the SDP evaluation should not include any equipment unavailable due to planned maintenance and testing. Therefore, the A EDG OOS due to maintenance is not considered in the assessment. Using IMC 0609, Significance Determination Process, the inspectors screened this issue as having very low safety significance using the phase 1 screening questions under the Mitigation System Cornerstone.

Enforcement:

10 CFR 50.72(b)(3)(v) requires that the licensee shall notify the NRC within eight hours of the occurrence of any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. Contrary to this requirement, on October 5, 2007, the licensee failed to inform the NRC that there was a loss of the onsite emergency power safety function. The result of the violation was determined to be of very low safety significance; therefore, this violation of 10 CFR 50.72(b)(3)(v) was classified as a Severity Level IV violation. Because this violation was of very low safety significance, was not repetitive or willful, and it was entered into the licensees CAP as CAP 053463, this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000331/2007005-02).

.2 Review of Personnel Performance During a Planned Downpower to perform repairs on

the Main Steam Line Drain and Manway for Main Steam Reheater Drain Tank

a. Inspection Scope

The inspectors reviewed personnel performance following a planned downpower to approximately 55 percent reactor power to repair two steam leaks. The inspectors observed the operators performing plant manipulations to reduce reactor power in order to reduce the dose rates in the secondary steam system. A review of the operator logs, associated procedures, briefings, and contingency plans were observed or evaluated by the inspectors. The inspectors observed operator performance during the evolution.

Reviews included, but were not limited to, operator logs, pre-job briefings, instrument recorder data, and procedures. The documents listed in the Attachment were used by the inspectors to accomplish the objectives of the inspection procedure.

This review represented one sample as defined in Inspection Procedure 71153-05.

b. Findings

No findings of significance were identified.

.3 Review of Personnel Performance During an Unplanned Downpower due to a Steam

Leak in the B Reactor Feedwater System

a. Inspection Scope

The inspectors reviewed personnel performance following an unplanned downpower to approximately 55 percent reactor power due to a steam leak in the B Reactor Feedwater system minimum flow line high point vent piping. The inspectors observed the operators performing plant manipulations to reduce reactor power in order to take out-of-service and isolate the B feedwater system to repair the steam leak. A review of the operator logs, associated procedures, briefings, and contingency plans were observed or evaluated by the inspectors. The inspectors observed and reviewed records of operator performance during these evolutions. Reviews included, but were not limited to, operator logs, pre-job briefings, instrument recorder data, and procedures.

The documents listed in the Attachment were used by the inspectors to accomplish the objectives of the inspection procedure.

This review represented one sample as defined in Inspection Procedure 71153-05.

b. Findings

No findings of significance were identified.

.4 (Closed) LER 05000331/2007-009-00: Loss of Essential Bus Resulted in Loss of Safety

Function At 0408 on October 5, 2007, while applying a clearance (tagout) to breaker 1B4234A, a fault occurred on the MCC dual breaker cubicle 1B4234A/B, resulting in the loss of the 480 Volt AC essential bus 1B42. The loss of bus 1B42 resulted in the loss of the B ESW pump, thus resulting in the loss of cooling to the B EDG. At the time of the event, the A EDG was OOS and inoperable for planned maintenance. The A ESW pump was inoperable but available following pre-planned maintenance. With both the A and B EDGs inoperable, there was a loss of the onsite emergency power safety function. At 0715, power was restored to bus 1B42, and the B ESW pump and B EDG were declared operable.

The primary cause of the event was an equipment failure related to an underlying equipment deficiency that was exacerbated by Operator actions. Specifically, the most probable cause of the arc flash was due to the C phase stab for MCC breaker cubicle 1B4234A/B becoming separated from the right C phase bus work. Contributing to the event was the station management teams failure to effectively identify and resolve previously identified issues with MCC breaker cubicle 1B4234A/B.

Section 4OA3.1 describes an NRC-identified finding associated with the closure of this LER. The licensee entered this into their CAP as CAP 053463. Documents reviewed as part of this inspection are listed in the Attachment. This LER is closed.

4OA6 MANAGEMENT MEETINGS

.1

Exit Meeting Summary

On January 17, 2007, the inspector presented the inspection results to Mr. D. Curtland, Plant Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

Access control to radiologically significant areas and the ALARA planning and controls program with Mr. D. Curtland, Plant Manager on November 2, 2007.

Licensed Operator Requalification biannual inspection with Mr. J. Morris, Training Manager, on December 10, 2007.

Emergency Preparedness inspection with Mr. T. MacIntyre on December 19, 2007.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

R. Anderson, Vice-President
D. Curtland, Plant Manager
B. Eckes, NOS Manager
S. Catron, Licensing Manager
J. Cadogan, Engineering Director
B. Kindred, Security Manager
J. Morris, Training Manager
C. Dieckmann, Operations Manager
G. Fuller, Operations Training
G. Pry, Maintenance Manager
J. Windschill, Chemistry & Radiation Protection Manager
P. Sullivan, Emergency Preparedness Manager
T. MacIntyre, Emergency Planning Coordinator
M. Lingenfelter, Design Engineering Manager
S. Huebsch, System Engineering Supervisor
J. Swales, Design Engineering Supervisor
K. Kleinheinz, Program Engineering Manager
R. Porter, General Supervisor Radiation Protection
P. Louis, Health Physics Supervisor
B. Klotz, Program Engineering Supervisor
R. Schlueter, ALARA Coordinator
N. McKenney, General Supervisor Radiation Protection Support
S. Funk, CHP, REMP Program Manager, Sr. Health Physics Coordinator
D. Johnson, Radwaste Operator/Chem Tech, Rad Environmental Technician

Nuclear Regulatory Commission

K. Feintuck, Project Manager, NRR
K. Riemer, Chief, Reactor Projects Branch 2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000331/2007005-01 NCV Failure to Adequately Survey Resulting in Unposted, Uncontrolled High Radiation Area. (Section 2OS1.2)
05000331/2007005-02 NCV Failure to Make an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> Notification to the NRC for Loss of Both EDGs (Section 4OA3.1)

Closed

05000331/2007009-00 LER Loss of Essential Bus Resulted in Loss of Safety Function

LIST OF DOCUMENTS REVIEWED